improving overall efficiency of the cutting machines by impletation of pillars of tpm
TRANSCRIPT
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
1/29
MPROVING OVERALLEFFICIENCYF THE CUTTING MACHINES BY
MPLEMENTATION OF PILLARS.F TPM
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
2/29
MPROVING OVERALL EFFICIENCY OF THEUTTING MACHINES BY IMPLEMENTATION OF
ILLARS OF TPM
PREPARED BY
Name of the studentsq Yashraj.V.Rane.q Harshad.V.Suryawanshi.q
Kalpesh.D.Khochare.q Amol.P.Shetke.q Dhiraj.B.Waghmare.
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
3/29
Pillars of TPM
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
4/29
PILLAR 1 - JISHU HOZEN (Autonomous maintenance):
This pillar is geared towards developing operators to be able to take care of small maintenancetasks, thus freeing up the skilled maintenance people to spend time on more value added activityand technical repairs. The operators are responsible for upkeep of their equipment to prevent itfrom deteriorating.
PILLAR 2 KOBETSU KAIZEN:
"Kai" means change, and "Zen" means good (for the better). Basically kaizen is for smallimprovements, but carried out on a continual basis and involve all people in the organization.Kaizen is opposite to big spectacular innovations. Kaizen requires no or little investment. Theprinciple behind is that "a very large number of small improvements are move effective in anorganizational environment than a few improvements of large value. This pillar is aimed atreducing losses in the workplace that affect our efficiencies. By using a detailed and thoroughprocedure we eliminate losses in a systematic method using various Kaizen tools. These activitiesare not limited to production areas and can be implemented in administrative areas as well.
TPM Pillars ToImplement
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
5/29
Why Kobetsu Kiazen?
1. Easy to implement.2. It can be more cost effective compared to other
three processes.3. Everyone is involved during KK activity i.e. frommanager to shop floor worker
So that every operator gets the feel of experiment4. More operators friendly.
5. It can be done with less cost.
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
6/29
Why Jishu Hozen?
1.Easy to implement.
2.Uninterrupted operation of equipments.3.Flexible operators to operate and maintain other
equipments.4.Eliminating the defects at source through active
employee participation.
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
7/29
Behringer Band SawCutting M/C Losses
SR.NO. ACTIVITY TIME in min %
1. Setting if JOB 115 19.79
2. Measurement 83 14.28
3. Operator nonavailability
35 4.30
4. Crane waiting time 15 2.58
5. M/C down time 313 53.87
6. Tool changing time 30 5.16
TOTAL 581 100
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
8/29
Behringer Band SawCutting M/C Losses
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
9/29
Three Major Lossesin Behringer:-
1.
M/C Down Time.
Setting Time.
Measurement.
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
10/29
1. M/C Down Time
REASON
Maintenance
SOLUTION
Preventive Maintenance of M/C to be done ontime to avoid maintenance while M/C is inproduction.
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
11/29
2.Setting time
REASON Fatigue to Operator in Setting the Job.
SOLUTION Sensors are to be employed on machine for
measurement purpose.
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
12/29
3. Measurement
REASON Presently measurement is done manually by
operator.
New measurement type equipment must beprocured to minimize measurement time.
SOLUTION Sensors (stops)assembly has to be done near
to the machine blade so measurement
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
13/29
CNC Suag Cutting M/CLosses
SR.NO. ACTIVITY TIME inmin
%
1. Scheduled/Planned Stoppages 698 49.75
2. Setting Time 17 1.223. Start-up Losses[mock-up] 288 20.52
4. Minor Stoppage[Time Loss] 20 1.42
5. Non Availability of Material 340 24.24
6. Non Availability of Operator 40 2.85
TOTAL 1403 100
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
14/29
CNC Suag Cutting M/CLosses
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
15/29
Three Major Losses inCNC Suag:-
Scheduled/Planned Stoppages.Non Availability of Material.Start up Loss[mock-up].
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
16/29
Scheduled/PlannedStoppages REASON Loading Time Of Plate Is Too High.Time consumed for Setting the Job Plate.
SOLUTIONS Loading Time Should Be Minimized By OfflineSetting Of Plate.
Special fixture to be Designed for Quick Setting ofJob Plate.
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
17/29
on va a y o a er a
REASON Improper & Unplanned Stacking of Plates.
SOLUTIONS
Proper stacking of plates as per priority.Proper proactive planning to feed the m/c
as per plan.
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
18/29
Start up Loss[mock-up]
REASON No cleaning before Operator reports the
machine. Major time consumed in Test Run.
SOLUTIONS Special Cleaning staff to be provided for
cleaning of the m/c before operatorreports on the m/c during each shift.
Special Fixture to be made to avoid Test Run.
es gn pro a e so on
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
19/29
es gn pro a e so u onfor Behringer Band Saw
Cutting M/C
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
20/29
Actual implementationof scale
es gn pro a e so u on
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
21/29
es gn pro a e so u onfor CNC (Suag) Saw
Cutting M/C
c ua os on ng
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
22/29
c ua os on ngPlate For Reducing time
For Transportation
RE ULT BEF RE
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
23/29
RE ULT BEF REIMPLEMENTATION FOR BEHRINGER
BANDSAW CUTTING MACHINE.ATE OF PERFORMANCE EASUREMENT TIME/ /4 9 2009 20
/ /11 9 2010 30
RESULTS AFTER IMPLEMENTATION
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
24/29
RESULTS AFTER IMPLEMENTATIONFOR BEHRINGER BANDSAWCUTTING MACHINE.
ATE OF PERFORMANCE EASUREMENT TIME/ /22 04 2010 15
/ /23 04 2010 24
RESULTS BEFORE
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
25/29
RESULTS BEFOREIMPLEMENTATION FOR CNC GASCUTTING MACHINE - SUAG.
ATE OF PERFORMANCE VAILABILITY OF MATERIAL/ /11 9 2009 30
/ /25 09 2009 20
RESULTS AFTER IMPLEMENTATION
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
26/29
RESULTS AFTER IMPLEMENTATIONFOR CNC GAS CUTTING MACHINE -SUAG.
ATE OF PERFORMANCE VAILABILITY OF MATERIAL/ /22 04 2010 12
/ /23 04 2010 15
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
27/29
CONCLUSION
O. E. E. IMPROVED FOR BEHRINGERBANDSAW CUTTING MACHINE:-
DATE - / /efore 04 09 2009- / /fter 22 04 2010 - / /efore 11 9 2009- / /fter 23 04 2010
BEFORE O.E.E. .90 34 .48 86
AFTER O.E.E. .92 30 .60 87
. . .FROM ABOVE RESULTS IT CAN BE SEEN THAT O E E HAS BEEN IMPROVED BY% % .ALMOST 3 TO 15 AFTER THE IMPLEMENTATION OF TPM
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
28/29
CONCLUSION
O. E. E. IMPROVED FOR CNC GASCUTTING MACHINE CUTTINGMACHINE - SUAG:-DATE - / /efore 11 09 2009
- / /fter 22 04 2010 - / /efore 25 9 2009- / /fter 23 04 2010BEFORE O.E.E. .84 1 .78 3
AFTER O.E.E. .91 3 83
. . .FROM ABOVE RESULTS IT CAN BE SEEN THAT O E E HAS BEEN IMPROVED BY% % .ALMOST 3 TO 7 AFTER THE IMPLEMENTATION OF TPM
-
8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM
29/29
.HANK YOU.HANK YOU