improving overall efficiency of the cutting machines by impletation of pillars of tpm

Upload: harshads

Post on 30-May-2018

219 views

Category:

Documents


0 download

TRANSCRIPT

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    1/29

    MPROVING OVERALLEFFICIENCYF THE CUTTING MACHINES BY

    MPLEMENTATION OF PILLARS.F TPM

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    2/29

    MPROVING OVERALL EFFICIENCY OF THEUTTING MACHINES BY IMPLEMENTATION OF

    ILLARS OF TPM

    PREPARED BY

    Name of the studentsq Yashraj.V.Rane.q Harshad.V.Suryawanshi.q

    Kalpesh.D.Khochare.q Amol.P.Shetke.q Dhiraj.B.Waghmare.

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    3/29

    Pillars of TPM

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    4/29

    PILLAR 1 - JISHU HOZEN (Autonomous maintenance):

    This pillar is geared towards developing operators to be able to take care of small maintenancetasks, thus freeing up the skilled maintenance people to spend time on more value added activityand technical repairs. The operators are responsible for upkeep of their equipment to prevent itfrom deteriorating.

    PILLAR 2 KOBETSU KAIZEN:

    "Kai" means change, and "Zen" means good (for the better). Basically kaizen is for smallimprovements, but carried out on a continual basis and involve all people in the organization.Kaizen is opposite to big spectacular innovations. Kaizen requires no or little investment. Theprinciple behind is that "a very large number of small improvements are move effective in anorganizational environment than a few improvements of large value. This pillar is aimed atreducing losses in the workplace that affect our efficiencies. By using a detailed and thoroughprocedure we eliminate losses in a systematic method using various Kaizen tools. These activitiesare not limited to production areas and can be implemented in administrative areas as well.

    TPM Pillars ToImplement

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    5/29

    Why Kobetsu Kiazen?

    1. Easy to implement.2. It can be more cost effective compared to other

    three processes.3. Everyone is involved during KK activity i.e. frommanager to shop floor worker

    So that every operator gets the feel of experiment4. More operators friendly.

    5. It can be done with less cost.

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    6/29

    Why Jishu Hozen?

    1.Easy to implement.

    2.Uninterrupted operation of equipments.3.Flexible operators to operate and maintain other

    equipments.4.Eliminating the defects at source through active

    employee participation.

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    7/29

    Behringer Band SawCutting M/C Losses

    SR.NO. ACTIVITY TIME in min %

    1. Setting if JOB 115 19.79

    2. Measurement 83 14.28

    3. Operator nonavailability

    35 4.30

    4. Crane waiting time 15 2.58

    5. M/C down time 313 53.87

    6. Tool changing time 30 5.16

    TOTAL 581 100

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    8/29

    Behringer Band SawCutting M/C Losses

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    9/29

    Three Major Lossesin Behringer:-

    1.

    M/C Down Time.

    Setting Time.

    Measurement.

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    10/29

    1. M/C Down Time

    REASON

    Maintenance

    SOLUTION

    Preventive Maintenance of M/C to be done ontime to avoid maintenance while M/C is inproduction.

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    11/29

    2.Setting time

    REASON Fatigue to Operator in Setting the Job.

    SOLUTION Sensors are to be employed on machine for

    measurement purpose.

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    12/29

    3. Measurement

    REASON Presently measurement is done manually by

    operator.

    New measurement type equipment must beprocured to minimize measurement time.

    SOLUTION Sensors (stops)assembly has to be done near

    to the machine blade so measurement

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    13/29

    CNC Suag Cutting M/CLosses

    SR.NO. ACTIVITY TIME inmin

    %

    1. Scheduled/Planned Stoppages 698 49.75

    2. Setting Time 17 1.223. Start-up Losses[mock-up] 288 20.52

    4. Minor Stoppage[Time Loss] 20 1.42

    5. Non Availability of Material 340 24.24

    6. Non Availability of Operator 40 2.85

    TOTAL 1403 100

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    14/29

    CNC Suag Cutting M/CLosses

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    15/29

    Three Major Losses inCNC Suag:-

    Scheduled/Planned Stoppages.Non Availability of Material.Start up Loss[mock-up].

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    16/29

    Scheduled/PlannedStoppages REASON Loading Time Of Plate Is Too High.Time consumed for Setting the Job Plate.

    SOLUTIONS Loading Time Should Be Minimized By OfflineSetting Of Plate.

    Special fixture to be Designed for Quick Setting ofJob Plate.

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    17/29

    on va a y o a er a

    REASON Improper & Unplanned Stacking of Plates.

    SOLUTIONS

    Proper stacking of plates as per priority.Proper proactive planning to feed the m/c

    as per plan.

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    18/29

    Start up Loss[mock-up]

    REASON No cleaning before Operator reports the

    machine. Major time consumed in Test Run.

    SOLUTIONS Special Cleaning staff to be provided for

    cleaning of the m/c before operatorreports on the m/c during each shift.

    Special Fixture to be made to avoid Test Run.

    es gn pro a e so on

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    19/29

    es gn pro a e so u onfor Behringer Band Saw

    Cutting M/C

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    20/29

    Actual implementationof scale

    es gn pro a e so u on

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    21/29

    es gn pro a e so u onfor CNC (Suag) Saw

    Cutting M/C

    c ua os on ng

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    22/29

    c ua os on ngPlate For Reducing time

    For Transportation

    RE ULT BEF RE

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    23/29

    RE ULT BEF REIMPLEMENTATION FOR BEHRINGER

    BANDSAW CUTTING MACHINE.ATE OF PERFORMANCE EASUREMENT TIME/ /4 9 2009 20

    / /11 9 2010 30

    RESULTS AFTER IMPLEMENTATION

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    24/29

    RESULTS AFTER IMPLEMENTATIONFOR BEHRINGER BANDSAWCUTTING MACHINE.

    ATE OF PERFORMANCE EASUREMENT TIME/ /22 04 2010 15

    / /23 04 2010 24

    RESULTS BEFORE

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    25/29

    RESULTS BEFOREIMPLEMENTATION FOR CNC GASCUTTING MACHINE - SUAG.

    ATE OF PERFORMANCE VAILABILITY OF MATERIAL/ /11 9 2009 30

    / /25 09 2009 20

    RESULTS AFTER IMPLEMENTATION

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    26/29

    RESULTS AFTER IMPLEMENTATIONFOR CNC GAS CUTTING MACHINE -SUAG.

    ATE OF PERFORMANCE VAILABILITY OF MATERIAL/ /22 04 2010 12

    / /23 04 2010 15

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    27/29

    CONCLUSION

    O. E. E. IMPROVED FOR BEHRINGERBANDSAW CUTTING MACHINE:-

    DATE - / /efore 04 09 2009- / /fter 22 04 2010 - / /efore 11 9 2009- / /fter 23 04 2010

    BEFORE O.E.E. .90 34 .48 86

    AFTER O.E.E. .92 30 .60 87

    . . .FROM ABOVE RESULTS IT CAN BE SEEN THAT O E E HAS BEEN IMPROVED BY% % .ALMOST 3 TO 15 AFTER THE IMPLEMENTATION OF TPM

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    28/29

    CONCLUSION

    O. E. E. IMPROVED FOR CNC GASCUTTING MACHINE CUTTINGMACHINE - SUAG:-DATE - / /efore 11 09 2009

    - / /fter 22 04 2010 - / /efore 25 9 2009- / /fter 23 04 2010BEFORE O.E.E. .84 1 .78 3

    AFTER O.E.E. .91 3 83

    . . .FROM ABOVE RESULTS IT CAN BE SEEN THAT O E E HAS BEEN IMPROVED BY% % .ALMOST 3 TO 7 AFTER THE IMPLEMENTATION OF TPM

  • 8/9/2019 IMPROVING OVERALL EFFICIENCY OF THE CUTTING MACHINES BY IMPLETATION OF PILLARS OF TPM

    29/29

    .HANK YOU.HANK YOU