implementation of a novel technology for the … implementation of a novel technology for the...

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i Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals Plc, Zambia IME Process Metallurgy and Metal Recycling, RWTH Aachen University, Germany Abstract In January 2001, Chambishi Metals commissioned a 40MW DC arc furnace using selective carbothermic reduction for processing reverberatory furnace slag stockpile of 20 million tons containing 0.34 to 4.5% cobalt, and an average of 1.1% copper. Cobalt occurs as faylite whereas copper occurs as oxide and sulphide. An atomizer unit to atomize furnace product, molten Co/Cu/Fe alloy, and a pressure oxidation leach process to leach cobalt and copper and separate iron as goethite was also commissioned. Cobalt and copper containing solution is processed in the refinery for production of metals. The commissioning and ramp up period was much longer than projected due to premature failure of the hearth and other operational problems associated with the feed system, cooling system and power control. Furnace availability was low and affected the throughput and metal production. This had put tremendous pressure on the company due to poor cash flow and non repayment of the capital resulting in sale of 100% of its share in July 2003. A systematical analysis initiated then, to de- bottleneck the furnace operation, was successful, resulting in attainment of design throughputs. The Plant Historian Database (PHD) was used for the analysis. Commercial application of the DC arc furnace on smelting of copper smelter slag was unique and therefore required extensive literature search to broaden the knowledge of the theory and the practice. The thesis shows improvements and modifications carried out on feed system to create charge bank, selection of flux to modify the slag chemistry, modification of alloy chemistry, re-configuration of the power control system and increased atomization

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Page 1: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

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Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals Plc, Zambia IME Process Metallurgy and Metal Recycling,

RWTH Aachen University, Germany Abstract In January 2001, Chambishi Metals commissioned a 40MW DC arc furnace using

selective carbothermic reduction for processing reverberatory furnace slag stockpile

of 20 million tons containing 0.34 to 4.5% cobalt, and an average of 1.1% copper.

Cobalt occurs as faylite whereas copper occurs as oxide and sulphide. An atomizer

unit to atomize furnace product, molten Co/Cu/Fe alloy, and a pressure oxidation

leach process to leach cobalt and copper and separate iron as goethite was also

commissioned. Cobalt and copper containing solution is processed in the refinery for

production of metals.

The commissioning and ramp up period was much longer than projected due to

premature failure of the hearth and other operational problems associated with the

feed system, cooling system and power control. Furnace availability was low and

affected the throughput and metal production. This had put tremendous pressure on

the company due to poor cash flow and non repayment of the capital resulting in sale

of 100% of its share in July 2003. A systematical analysis initiated then, to de-

bottleneck the furnace operation, was successful, resulting in attainment of design

throughputs. The Plant Historian Database (PHD) was used for the analysis.

Commercial application of the DC arc furnace on smelting of copper smelter slag was

unique and therefore required extensive literature search to broaden the knowledge of

the theory and the practice.

The thesis shows improvements and modifications carried out on feed system to

create charge bank, selection of flux to modify the slag chemistry, modification of alloy

chemistry, re-configuration of the power control system and increased atomization

Page 2: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

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capacity. Following the implementation of these, the furnace performance attained

design levels.

Extended Abstract

1.0 Introduction

After 1991, at the time of the commencement of the privatization process of the

mining conglomerate “Zambia Consolidated Copper Mines”, Chambishi Cobalt Plant

was packaged with the 20 million tonnes slag stockpile. The cobalt grade of the slag

ranged from 0.34% to 4.5% where as copper averaged 1.2%.The stockpile was

created over a period of 60 years since 1935 by dumping the slag generated from the

Rokana Copper Smelter. Anglovaal Mining of South Africa purchased this package in

1998. Due to declining production of Cu/Co sulphide concentrates which was the

traditional feed to the plant, an addition of a process for treatment of slag for

production of cobalt and copper, to sustain Chambishi’s viability, became essential.

Carbothermic reduction was selected to be an economically viable option. Pilot scale

test work was conducted at Mintek, RSA, using a DC arc furnace for determination of

the operating parameters. The project was then executed and a 40MW DC furnace

was commissioned in 2001.

The commissioning period was much longer than projection of three months. Until

July 2003, only 50% of the annual throughput target rate of 300000 tonnes could be

achieved. The furnace suffered failures of hearth lining, upper sidewall lining and

copper cooling elements in the slag/metal zone. These major failures restricted the

de-bottlenecking of the operation.

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In July 2003, the ownership changed to Enya Holding when a systematical analysis

was undertaken for de-bottlenecking, the throughput started approaching target levels

almost immediately. Extensive literature search was carried out to study all aspects of

smelting operation and relate those to the plant data extracted from Plant Historian

Datasheet (PHD). Several improvements in the operations and the modifications

carried out are discussed.

2.0 Mineralogy of the Slag

Mineralogical analysis of the slag carried out by MINTEK, RSA, is shown in the table

1, indicate that the cobalt is present as faylite (Iron Silicate Matrix) where as copper is

present as oxide, sulphide and metal. Presence of significant level of sulphide and

metallic copper are due to entrained losses.

Table-1: Mineralogical composition of the Rokana Reverberatory Slag

Group Total Co

Mineral Phases % of Total Cu % of Total Co

Slag Fe, Ca, Al (Mg, K, Co, Cu) - Silicates 46.6 94.6

Spinel Fe(Al, Cr, Ti, Ca, Co, Cu) - Oxides 1.1 5.2

Sulphide Cu(Co, Fe) - Sulphide 39.3 0.2

Metal Cu(Co, Fe) - Metal 13.0 <0.1

Total 100.0 100.0

Figure 1 below is the picture of the Rokana slag dump. The cobalt grade varied

significantly as shown in figure 2. The tonnages and the grades were estimated using

metallurgical accounting records of Rokana copper smelter. Few drill samples were

taken for chemical analysis due to cost and time constraints. The chemical analysis of

those samples indicated resemblance with the analysis obtained from the smelter

records.

Page 4: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

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Fig.1: Picture of the Rokana Slag Dump- View from Ndola-Kitwe Road Side

0

1000

2000

3000

4000

5000

6000

7000

8000

4.5 1.33 0.91 0.75 0.68 0.56 0.46 0.34

%Co

ton

nes

, (0

00)

Fig.2: Estimated Tonnage and Grade Distribution on the Rokana Slag Dump

The cobalt grades were as high as 4.5% reducing to 0.34%. Majority of the slag

averaged 0.7% Co. The variations were due to variations in the concentrates feed mix

to the Rokana Copper Smelting furnaces.

3.0 Theory of Carbothermic Reduction

The chemical reactions occurring in metallurgical processes such as reduction of

metal oxides can be explained in terms of free energy in thermodynamics. The

reduction of metal oxides is obtained using carbon which is available cheaply in

Page 5: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

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reduced form as coal / coke. Moreover, when carbon reacts with oxygen, it forms

gaseous oxides i.e. Carbon monoxide and carbon dioxide, therefore the dynamics of

its oxidation is different from that of metals whose oxidation has a more negative ∆G

at higher temperatures. Carbon is therefore acts as reductive agent both in element

phase and in monoxide phase.

Figure 3, Ellingham Diagram, shows the conditions under which a metal oxide can be

reduced to a metal. The standard Gibbs free energy of formation of the oxide is

considered, for example, M+½O2 → MO The value of ΔG is plotted against

temperature. In general, the result is a straight line. In some cases, there is an abrupt

change in the line’s slope at a point because of a phase change. The value of ΔG for

the reducing agent is also plotted. For example, if the reducing agent is carbon

forming carbon dioxide, it is ΔG for the reaction C+O2 → CO2. Reduction can occur in

the range of temperatures in which the carbon curve is lower than the metal curve.

Fig.3: Gibb’s Free Energy-Temperature Diagram (Ellingham Diagram) Jones, et el (7,47) developed relationship between carbon addition and nickel, cobalt

and iron recoveries. Taking advantage of the finding that the cobalt reduction is much

faster than iron, a relationship between % iron reduction and cobalt recovery was

developed as shown in figure 4.

Page 6: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

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% Fe Reduction

Fig.4: % Fe Reduction vs. % Cobalt Recovery In order to maximize cobalt recovery and minimize iron recovery, this work became

the basis of optimal coal addition. Coal addition rate to achieve 56% iron recovery to

the alloy, almost 90% cobalt recovery was achieved. It was necessary to optimize

down stream processing plant size and efficiency. Higher iron content in the product

would increase the cobalt losses through the residue, goethite.

4.0 Process Description Following commissioning of the 40 MW DC Arc furnace in the year 2001, the

Chambishi operation’s flow sheet is shown in figure 5.

Slag from

Dump

Crushing/ Screening

Magnetic Separation

Drying

40 MW

DC Arc

Furnace

Plasma

Heating

Atomization

Size < 150,

micron

High Pressure/

Oxidation LeachCobalt

RefineryCobalt &

Copper

Metal

Fig.5: Simplified Flow Chart of Chambishi Operation after 2001.

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The slag excavated from the dump, crushed and screened to +6, -16mm particle size,

beneficiated to high grade the furnace feed by 15 – 20%, dried to reduce moisture to

<1%, is fed to the furnace. Furnace product is an alloy of cobalt, copper and iron.

Molten alloy is tapped and atomized to <150 micron particle size which is pumped to

the pressure/oxidation leach plant for leaching cobalt and separating iron as goethite.

The leach solution containing cobalt, copper and other trace impurity elements is

processed in cobalt refinery for cobalt and copper metal production.

5.0 Commissioning and Ramp Up Figure 6 indicate that the projected furnace power was only attained in the year 2003.

The attainment of design power level of 40MW was the first necessary step to achieve

design throughput. The projected total energy consumption was only attained after

July 2003 with the start of systematical analysis and de-bottlenecking. With the

progress of improvements, the furnace power exceeded the projected levels.

-

5

10

15

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45

Jan'0

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Apr'06

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Oct'06

Furnace Energy kWh Actual Expected Energy Consumption kWh

Projected Power MW Actual Power (MW)

Fig.6: Furnace Power – Actual vs Projected Prior to the year 2003, major change undertaken, was the replacement of copper

cooling elements in the slag/metal bath in the year 2002. The original Fuch’s coolers

(fig.7) were replaced with Hatch coolers (fig.8). Fuch’s coolers had single water

cooling circuit with the flat copper plate facing the molten slag/alloy whereas Hatch

coolers had double cooling circuit with waffles. The waffles helped in an efficient

Page 8: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

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formation of the freeze layer as well as retained it firmly to protect the cooling

element. Despite this change, the furnace performance did not improve significantly

as shown in figure 9. Even at lower furnace power, the heat flux on the copper cooling

elements were very high at 4 - 5MW against design of 2 - 2.5 MW causing stoppages.

Continued exposure of copper coolers to heat could have resulted in catastrophic

failure, water ingress in the molten bath and therefore explosions. The downward

trend only started after July 2003 when the improvements commenced. The high heat

flux, sensed by the rate of change of water temperature was causing furnace

stoppages due to safety reasons. A systematical analysis was then initiated for de-

bottlenecking.

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Fig.7: Sketch of the Fuch’s Coolers Fig.8: Sketch of the Hatch Coolers

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Page 10: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

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Fig.9: Furnace power vs. Copper Coolers total Heat Flux. 6.0 De-bottlenecking De-bottlenecking commenced with the analysis of the root causes of the furnace

stoppages. The analysis of maintenance and operational activities (fig.10) clearly

indicated that main reasons for furnace stoppages were operational.

Fig. 10: Furnace Stoppage due to Maintenance Activities

The analysis of the operational activities (Figure 11) shows the major causes for

furnace stoppages as:

0

2000

4000

6000

8000

10000

12000

14000

16000

18000

Operations Power Outage Instrumentation Mechanical Electrical P.M.

Min

ute

s

Page 11: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

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1. Power trip outs due to copper coolers experiencing high heat flux above set

point.

2. Plasma torch failures/maintenance causing alloy tapping constraint which

resulted in high level in the furnace and necessitated feed reduction/ power

off.

3. Faster wear out of the feed pipes resulting in feed slag spillages on the dome

and roof panels needed frequent and longer stoppages for replacement.

Fume duct blockages and inspections were considered necessary activities to ensure

timely corrective action for safety of the furnace. Stoppage for electrode addition was

a routine and standard requirement.

In view of the above analysis, the focus was to enhance protection of the copper

coolers from heat, increase plasma heating capacity and replacement of feed pipes

with stronger wear resistant material. Later on, cooling of the roof panels was also

improved.

Fig.11: Furnace Stoppage due to Operational Activities

0

500

1000

1500

2000

2500

3000

3500

4000

Fume Duct

Blockage

Copper

Coolers

Furnace

Inspection

Electrode

Addition

Plasma

Torch

Feed

Pipes

Roof Panel

Min

ute

s

2003 2005

Page 12: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xii

It can be clearly seen that by the year 2005, there was a significant reduction in the

furnace stoppages which consequently increased throughput.

6.1. Rearrangement of the Feed Points Rearrangement of the feed points was the quickest medication which resulted in

quenching the bath in front of the copper coolers and reducing the radiant heat on the

upper side wall. In the original design, the feed points were located around the inner

periphery (fig.12-A). Due to slow flow of the slag towards the arc and not totally

shrouding it, the intense radiant heat was damaging the side wall brick work and the

shell. Furnace roof was then modified to open feed points around the electrode

(fig.12-B) to feed 100% of the material to ensure that the arc is totally shrouded. This

had an additional advantage of faster melting rate because of all the material directly

entering the arc. The radiant heat, still, could not be contained due to open arc

operation and damage to the furnace wall continued resulting in long stoppages. The

submerged arc operation was not possible due to Fuch’s copper coolers not able to

retain freeze layer resulting in high heat flux on them posing safety risks.

In July 2003, the closed feed points on the inner periphery were re-opened and the

10% of the feed was directed through those, keeping 90% through the points around

the electrode (fig.12-C). This improved the protection on the side wall resulting in

increased furnace availability.

Page 13: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xiii

A – Original Design B – Changed in Yr.2001 C – Changed in Yr.2003

(100% Feed in Front of- (100% Feed around the- (Split Feed – Current)

Copper Coolers) Electrodes)

Fig. 12: Furnace Feed Configurations (Feed Ports shown as Circles-Electrode in the

Centre)

6.2 Replacement of Feed Pipes

After the feed ports were reconfigured, the throughput increased but the increased

wear rate of the feed pipes resulted in furnace stoppages for clearing spillages and

replacements of pipes. A trial on the use of ceramic lined pipes was successful.

Photographs of the original wear resistant pipes and the ceramic lined pipes are

shown in figure 13.

Page 14: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xiv

(A)-4 inch I.D., Original Abrasion Resistant (B)-5 inch I.D., Ceramic Lined Pipes

Pipes

Fig.13: Furnace Feed Pipes

Page 15: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xv

6.3 Stabilization of the Furnace Power Furnace was experiencing severe power fluctuations which caused erratic feed rates.

This resulted in difficulties in controlling slag bath temperature to 1500 – 15500C.

Overfeeding was causing cooling of the bath whereas underfeeding causing high

temperature, both changing the resistance. This frequent swing in the bath resistance

triggered the electrode movement to maintain power set point, causing power

fluctuations. Figure 14 gives the circuit control diagram originally built in PLC. The

power fluctuations were experienced due to a sudden drop in resistance causing the

power to begin to drop. The controller would try to compensate by increasing the

current, thus maintaining the power at the set point, until it eventually reached a

maximum limit for the tap position. Once the current reached the maximum limit then

the power would fall in line with the resistance. Under these circumstances the tap

changer should tap down, thus increasing the allowable current. The ABB controller

prevented the transformer from tapping down below tap 10. This was designed to limit

the maximum current such that the current density remained under 300A/m2,

specified by the supplier. The ABB was convinced to remove the tap changer control

from their custom PLC. Chambishi then engineered this functionality into the

PlantScape control system.

Page 16: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xvi

Delta rectifier

Star rectifier

(-ve)

Vdc

Electrode

Idc Idc

Resistance

(+ve)

On load Tapchanger on the

HV side taps 1 - 15

Reactor

ABB Control

Unit

Electrode movement

control feed

Current and voltage

feed

Transformer and

rectifier operation

feed

Fig.14: Schematic electrical/control diagram for electrode movement for power control

The advantage of this change was that Chambishi had the flexibility to alter the

philosophy whilst retaining the integrity of the safety features built into the ABB control

system. The PlantScape system requests a tap change from the ABB system, which

executes it if it is safe to do so. The maximum limit for current was set at 70 kA

(250A/m2). This meant that the tap setting could safely go down to position 3 (fig. 15)

with no safety risks to electrical equipment.

Page 17: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xvii

0

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1 2 3 4 5 6 7 8 9 10 11 12 13 14 15

Tap Position

Vol

ts

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400

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600

700

800

900

Am

ps x

100

DC Volts DC Amps

Fig 15: Voltage and Current limits for Tap Positions, 1 – 15.

After this change was made to stabilize the power, the standard deviation improved to

0.84 from 1.6 in the year 2005, indicating a significant improvement as shown in

figure 16. The standard deviation improved from 1.6 to 0.847 by the end of the year

2006. The standard deviations are calculated for 6 monthly averages at 40MW power

only.

1.577 1.595

1.219 1.208

0.847

34.0

35.0

36.0

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38.0

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n-0

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p-0

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[MW

]

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0.6

0.8

1

1.2

1.4

1.6

Std

Devia

tion

Pow er Setpoint [MW] Actual Pow er [MW] Std Deviation at 40 MW Yrs 2004,2005 & 2006 (6 Monthly Intervals)

Fig.16: Furnace power set point vs. Actual power (Jan’04 – Jan’07)

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xviii

6.4 Selection of Flux Due to availability locally and low price, burnt lime (CaO) was being used to flux iron

oxide and silica. The lower melting temperature of the resultant slag, CaO-FeO-SiO2,

at the operating temperature, the formation of the freeze layer was not sufficient for

the protection of the Hatch copper coolers. The substitution of the burnt lime with

burnt magnesite (MgO) gave adequate freeze layer. The slag MgO-CaO-FeO-SiO2

has a higher melting temperature spinel phase (16000C). At an operating temperature

of 1500 – 15500C, the change in the slag chemistry assisted in efficient formation of

freeze layer as the same cooling water flow rates to the coolers. Due to the waffle on

the Hatch coolers (17-A) the freeze layer is retained securely (fig.17-B), providing

better protection against heat flux from the molten bath. Figure 9 clearly shows the

benefit of this that the heat fluxes on the copper coolers came down to the 2MW

levels which was the specified limit for operation at 40MW power levels.

A- New Hatch Coolers B- Picture of the Hatch Cooler,

Showing Freeze Layer

Fig.17: Hatch Waffle Coolers

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xix

6.5 Changing Chemical Composition of the alloy

Due to the slag temperature of 1500 – 15500C and alloy temperature of 1220 -

12400C, it was also necessary to modify the chemical composition of the alloy as well

such that the tapping is smooth and the atomization is efficient. At lower

temperatures, the tapping was difficult resulting in high levels in the furnace and

excessive skull formation in the launder and in the atomization unit. Alloy therefore

had to be sufficiently fluid to minimize such problem. Mintek, through the test work

developed an empirical relationship between the chemical composition and the alloy

liquidus as follows:

Liquidus Temperature, 0C = N – 1.6[ %Cu – 10 ] – 26[ %S ] –80[ %C ] –8.5[%Si ]

Where, N is 1474 for Cu < 12% and 1435 for Cu equal to or greater than 12%. This

suggested that higher the copper, lower will be the liquidus.

It was therefore necessary to keep Cu levels above 12% to lower the liquidus such

that the plasma heating time is reduced. This eventually reduced tap to tap time and

increased furnace out put. It was not commercially recommended to exceed copper

concentration beyond 12% because of additional costs. Additionally, there is also a

loss of copper through the furnace waste slag. The option of increasing alloy

temperature in the furnace by operating at higher slag temperature would not only

have adversely affected the productivity but also would have increased wear rate of

the lining.

6.6 Installation of the Second Plasma Heating and Atomizer Stations The second plasma heating and the atomizer station was incorporated to provide

flexibility for maintenance such the one unit was always available for operation. This

improved tapping from 5 taps a day to 14 taps a day as shown in figures 18 and 19

and completely removed the tapping constraint.

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xx

Fig.18: Alloy tapping profile with one plasma torch station and one atomizer (25/12/2005)

Fig.19: Alloy tapping profile with two plasma torches and two atomizer stations (15/11/2006)

Torching and Atomising Cycles - Date: 25th Dec 2005

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1800

2000

Pla

sm

a t

orc

h c

urr

en

t, A

mp

s

Atomiser 1 Slurry temp Plasma Torch current

Torching and Atomising Cycles - Date: 25th Nov 2006

0

10

20

30

40

50

60

70

80

90

100

6:0

0:0

0 A

M

6:4

1:1

5 A

M

7:2

2:3

0 A

M

8:0

3:4

5 A

M

8:4

5:0

0 A

M

9:2

6:1

5 A

M

10:0

7:3

0 A

M

10:4

8:4

5 A

M

11:3

0:0

0 A

M

12:1

1:1

5 P

M

12:5

2:3

0 P

M

1:3

3:4

5 P

M

2:1

5:0

0 P

M

2:5

6:1

5 P

M

3:3

7:3

0 P

M

4:1

8:4

5 P

M

5:0

0:0

0 P

M

5:4

1:1

5 P

M

6:2

2:3

0 P

M

7:0

3:4

5 P

M

7:4

5:0

0 P

M

8:2

6:1

5 P

M

9:0

7:3

0 P

M

9:4

8:4

5 P

M

10:3

0:0

0 P

M

11:1

1:1

5 P

M

11:5

2:3

0 P

M

12:3

3:4

5 A

M

1:1

5:0

0 A

M

1:5

6:1

5 A

M

2:3

7:3

0 A

M

3:1

8:4

5 A

M

4:0

0:0

0 A

M

4:4

1:1

5 A

M

Slu

rry

tem

p,

oC

0

200

400

600

800

1000

1200

1400

1600

1800

2000

Pla

sm

a t

orch

cu

rren

t, A

mp

s

Atomiser 1 Slurry temp Atomiser 2 Slurry temp

Plasma Torch current Plasma Torch current

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xxi

6.7 Improvements in Roof Panels and Electrode Cooling The original roof panels had single cooling coil. The brush arc mode of operation was

casing burning of the refractory and the cooling coil due to flames which resulted in

frequent furnace stoppages for replacements. In 2005, the panels were redesigned to

have twin cooling coils. The advantage of this was the much longer operating life of

panels due to improved cooling and also the flexibility of a planned replacement in the

event of failures which avoided unplanned stoppages. The flames were damaging the

electrode sealing ring and the dome bricks resulting in premature failures of the dome.

Replacement of the dome required extended furnace stoppage. Water cooling around

the electrode, above the sealing ring was introduced. This increased the life of the

electrode seal and therefore less wear and tear on the dome bricks. The dome

replacement frequency was reduced significantly as shown in figure 18. The first

replacement was in 2004 after the power was ramped up to 40MW in the later half of

the year 2003. There were two replacements in 2004 reducing to one in 2005 and nil

after that.

0

1

2

3

2001 2002 2003 2004 2005 2006 2007 2008

No.

of

Repla

cem

ents

Fig.20: Furnace Dome replacements frequencies from 2001 to 2008

Page 22: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xxii

7.0 Fume Extraction The performance of the fume extraction system improved after power stabilization

and the improved integrity of the roof panels and the electrode seal due to improved

cooling. Damages to the roof panels and the electrode seal caused air ingress in the

furnace resulting in increased gas volume which posed gas handling capacity

constraint. This resulted in furnace pressurization and reduced feed for safety and

environment controls. The performance further improved by selection of coal which

had lower volatiles.

8.0. Results 8.1 Energy Utilization and Throughput

The de-bottlenecking exercise resulted in increase in energy utilization ratio due to

improved furnace utilization which eventually increased throughput to design levels as

shown in figures 21 and 22.

0

10

20

30

40

50

60

70

80

90

2001 2002 2003 2004 2005 2006 2007 2008

%

Fig.21: Yearly Energy Utilization Ratios

The energy utilization ratio increased from 50% in 2001 to 80% in the year 2003.

Even when there were stoppages in the years 2007 and 2008, the energy utilization

still remained at 80% level.

Page 23: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xxiii

Fig.22: Yearly furnace throughput

Throughput in the year 2005 was marginally affected by a 3 week shut down of the

pressure leach plant for relining of the autoclaves. In the year 2007, the hearth lining

failure in January which required relining in a 5 weeks shut down affected the

throughput whereas in the year 2008, the furnace was stopped in November due to

economic down turn and crash in the metal prices making the operation unviable.

8.2 Electrode Consumption

The graphite electrode consumption improved from 2.2 kg/t of slag feed to 0.7 kg/t, a

68% reduction as shown in figure 23 due to stability in furnace power.

0.0

0.5

1.0

1.5

2.0

2.5

2002 2003 2004 2005 2006 2007 2008

Kg/

Ton

Feed

Fig.23: Yearly Graphite Electrode Consumption

0

50000

100000

150000

200000

250000

300000

350000

400000

Yr.'01 Yr.'02 Yr.'03 Yr.'04 Yr.'05 Yr.'06 Yr.'07 Yr.'08

Furnace Feed, t Alloy Tapped, t

Page 24: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xxiv

8.3 Furnace Campaign Life The furnace campaign life is defined as the operating time between the two furnace

rebuilds. It is the indicator of the productivity of the furnace as well as safe operating

practices. The history of the furnace campaign is as follows:

Commissioned Failed Life (Years)

First Lining January 2001 April 2001 0.3

Second Lining July 2001 July 2002* 1.0

Third Lining October 2002 January 2007 4.3

Fourth Lining February 2007 to-date

* the lining was modified to incorporate Hatch Waffle Coolers.

Although the campaign life of 4.3 years achieved is the highest so far, it is lower than

the standard 7 – 8 years being achieved in the steel industry. The reason for shorter

life was the failure of the hearth lining due to massive volume of water ingress in the

furnace caused by failure of two copper coolers in November 2005. The skew bricks

underwent thermal shock resulting in gradual washing away of lining below the

copper coolers. Furnace operated for another 14 months before the lining gave way

resulting in a run away from a point about 400mm below the metal tap hole.

9.0 Conclusions A systematical approach to de-bottleneck furnace operation was successful in

attaining furnace throughput to design levels. Despite extensive pilot test work was

conducted at Mintek, all the information regarding the applicability could not be

established. The extrapolation of the information to the commercial unit was difficult.

There was no such process existed worldwide to gain experience. The learning time

therefore was too long. Such unique technology for which no operating knowledge

available, involvement of all the specialist institutions engaged in electric arc furnace

smelting could have been very useful to gather technical and operating experiences

before even design stage.

Page 25: Implementation of a Novel Technology for the … Implementation of a Novel Technology for the Recovery of Cobalt from Copper Smelter Slags Hira Singh, Bernd Friedrich, Chambishi Metals

xxv

Abbreviations

Aq. - Aqueous

AVMIN - Anglovaal Mining

Cons - Concentrates

CRU - Copper Research Unit

DTA - Differential Thermal Analysis

g/t - gram per tonne

HS - High Speed

I.D. - Internal Diameter

IX - Ion Exchange

LIM - Low Intensity Magnetics

ml/s - Milliliter per second

Pptn - Precipitation

SX - Solvent Extraction

TPA - Tonne per annum

TPD - Tonne per day

TPM - Tonne per month

R.L.E. - Roast Leach Electrowin

RSA - Republic of South Africa

XRD - X-Ray Diffraction