docket ho. 50-366 date 01-10-80 telephone ( 912 ) 367-7781

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. -- (% (4 * r3 OPERATING DATA REPORT . DOCKET HO. 50-366 r DATE 01-10-80 COMPLETED BY J.M. KAMISHLIAH , TELEPHONE ( 912 ) 367-7781 x 203 OPERATIHC STATUS ******************************************************* * Notes 1. Unit Hanet E.I. Hatch Huclear # tant Unit 2 * * 2. Reporting Periodt 12-80 * * 3. Licensed Thernal Power (MWt): 2436 * * 4. Haneplate Rating (Cross MUe)s 817.0 * * 5. Design Electrical Rating (Het MWe): 784.0 * * 6. Maxinun Dapendable Capacity (Cross MWe)I 805.7 * * . 7. Maxinun Dependable Capacity (Het MWe): 772.7 ******************************************************* * 8 If Changes Occur, in Capacity Ratings (Itens Henber 3 Through 7) Since Last Report, CIve Reasonst * \ 9. Pouer Level To Which Restricted, If Ang (Het NWe): 10 Reasons For Restrictions, If Anyt ! . This Month Yr.-to-Date Cunulative it. Hours In Reporting Period 744 8784 11617 12. Hunber Of Hours Reactor Was Critical 0.0 5570.3 8233.8 13. Reactor Reserve Shutdown Hours 0.0 0.0 0.0 14 Hours Generator On-Line 0.0 5273.8 7688.3 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 16. Cross Thernal Energy Generated (MWH) 0 11603836 17097898 17. Cross Electrical Energy.Cenerated (MWH) 0 3831320 5667280 18. Het Electrical Energy Generated (MWH) -2412 3644977 5402114 19. Unit Service Factor ' 0.0 60.0 66.2 , 20. Unit Availability Factor' O.0 60.0 66.2 21. Unit Capacity Factor (Using MDC Het) -0.4 53.7 60.2 22. Unit Capacity Factor ( Usi ng DER Het) -0.4 52.9 59.3 23. Unit Forced Outage Rate 0.0 12.4 11.8 24. Shutdouns Scheduled Over Hext 6 Months (Type, Date, and Duration of Each): Tw c4 25. If Shut Down At End or Report Period, Estinated Date of Startupt Ek 26. Units In Test Status (Prior to Connercial Operation)8 Forecast Achieved '[ v INITIAL CRITICALITY CI IHITIAL ELECTRICITY _______________ _______________ _______________ '" COMMERCIAL OPERATIDH _______________ C; _______________ _______________ m - (9/77) 00 - : . , . _ __ ._ _ _ _ _ - _ _ _ . _ _ . . _ . - _ - _ - - - -

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Monthly operating rept for Dec 1980.,
* Notes1. Unit Hanet E.I. Hatch Huclear # tant Unit 2 * *
2. Reporting Periodt 12-80 * *
5. Design Electrical Rating (Het MWe): 784.0 * *
6. Maxinun Dapendable Capacity (Cross MWe)I 805.7 * *.
7. Maxinun Dependable Capacity (Het MWe): 772.7 ******************************************************* *
8 If Changes Occur, in Capacity Ratings (Itens Henber 3 Through 7) Since Last Report, CIve Reasonst *
\ 9. Pouer Level To Which Restricted, If Ang (Het NWe):
10 Reasons For Restrictions, If Anyt
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This Month Yr.-to-Date Cunulative it. Hours In Reporting Period 744 8784 1161712. Hunber Of Hours Reactor Was Critical 0.0 5570.3 8233.813. Reactor Reserve Shutdown Hours 0.0 0.0 0.014 Hours Generator On-Line 0.0 5273.8 7688.315. Unit Reserve Shutdown Hours 0.0 0.0 0.016. Cross Thernal Energy Generated (MWH) 0 11603836 1709789817. Cross Electrical Energy.Cenerated (MWH) 0 3831320 566728018. Het Electrical Energy Generated (MWH) -2412 3644977 540211419. Unit Service Factor '
0.0 60.0 66.2 ,
20. Unit Availability Factor' O.0 60.0 66.221. Unit Capacity Factor (Using MDC Het) -0.4 53.7 60.222. Unit Capacity Factor ( Usi ng DER Het) -0.4 52.9 59.323. Unit Forced Outage Rate 0.0 12.4 11.824. Shutdouns Scheduled Over Hext 6 Months (Type, Date, and Duration of Each): Tw c4
25. If Shut Down At End or Report Period, Estinated Date of Startupt Ek26. Units In Test Status (Prior to Connercial Operation)8 Forecast Achieved '[v
INITIAL CRITICALITY CIIHITIAL ELECTRICITY _______________ _______________ _______________ '"COMMERCIAL OPERATIDH _______________
C;_______________ _______________
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COMPLETED BY J.H. KAMISHLIAH ,
MONTH 12-80
DAY AVERACE DAILY POWER LEVEL DAY AVERACE DAILY POWER LEVEL (MUe-Met) { (MUe-Het)
1 -3 17 -4 ,
2 -3 ' 18 -3*
3 -3 19 -3 4 -3 20 -3 5 -3 21 -3 6 -3 1 22 - -3 7 -3 23 -3 3 -3 24 -3+
9 -3 25 -3 to -4 j 26 -3
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UNIT N AME llatch 2 DATE l-10-81.
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COMPLETED BY J. f1 Kami5hIian REPORT MONTH December TELEPilONE 912-367-7781
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80-54 801201 - S 744 C 1 NA 'ZZ ZZZZZZ Shutdown for refueling 4
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F: Forced Reason: Method: Exhibit C Instruction
5: Scheduled A Eiguipment Failure (Explain) 1 Manust for Preparation of Data,
B41aintenance of Test 2 Manual Scram. Entry Sheets for Licenser
C Refueling 3 Automatic Scram. Event Report (LERI File (NUREG- .
D Regulatory Restriction 4 -Continuations 0161)*
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NUMBER DATE COMPLETED DESCRIPTION 80-2949 11-21-80 Replaced SBM switch stop plates
on valves 2BM-F022A-D, 2B21-F028A-D,, and PN22-F249A-D*
with new stop plate GE P/N 127A6753P1
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79-3357 11-25-80. Replaced diodes in ion chamber power supplies 2C51-K605 per GE_
field engineering memo #79-03
80-3446 12-17-80 Replaced flange gasket on N2 storage tank 2Ty8-A001 with 1/8" teflon gasket
80-3493 12-18-80 Replaced asphalt drain ditch and railroad as were after damage due to water errosion
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repaired parts according to original specs
80-3839 12-4-80 Repaired loose connection in the 2B21-J002 panel which was connected to thermocouple 2B21-N004F
80-4059 12-11-80 Removed defective solenoid off PSW outlet valve 2P41-4339A and replaced with pilot solenoid off of 2P41-4339B
80-4126 11-14-80 Made adjustments on R45 on main chasis and power supply bd. of reactor building vent monitor 2D11K636B, also adjusted R3 on log ratemeter board
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80-4291 12-5-80 Stand by plant service water pump 2P41-C002 was disassembled and serviced so as to pump at rated pressure; pump and motor were reinstalled and proc. HNP-6951 performed
80-4320 11-19-80 Backfilled 2E11-N015B, flow indicator 2E.11-R603B now reads*
correctly
80-4340 11-19-80 Cleaned and lubricated HPCI turb. control valve 2E41-TCV limit" - - - - -
switch plunger with C.R26
80-4351 11-27-80 Replaced bad GM tube in ARM 2D2-P600 in the sensor and converter
80-4456 12-15-80 R e p la'c e'd one min-3 fuse in "A" RPS scram pilot valve to control rod 2C11-26-03
80-4537 11-15-80 Removed and functionally tested per Tech Specs hyraulic snubber 2E11-RHR-R86
80-4538 11-15-80 Removed and functionally tested per Tech Specs hydraulic enubber.
2B31-55B-17
80-4539 11-15-80 Removed and functionally tested per Tech Specs hydraulic snubber 2B31-55A-17
80-4540 11-13-80 Removed and functionally tested per Tech Specs hydraulic snubber 2E21-R40
80-4541 11-13-80 Removed and functionally tested per Tech Specs hydraulic snubber 2E21-R87
80-4542 11-15-80 Removed and functionally tested per Tech Specs hydraulic snubber 2E21-R107P
80-4543 11-13-80 Removed and functionally tested per Tech Specs hydraulic anubber 2E11-RHR-R15B
80-4544 11-13-80 Removed and functionally tested i per Tech Specs hydraulic snubber
2E21-R72B
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80-4546 11-13-80 Removed and functionally tested per Tech Specs hydraulic snubber 2T46-R68A
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80-4571 11-20-80 Removed and functionally tested per Tech Specs hydraulic snubber 2B31-SSA3
80-4573 11-22-80 Removed and functionally tested per Tech Specs hydraulic snubber 2B31-SSA8
80-4574 11-22-80 Removed and functionally tested per Tech Specs hydraulic snubber 2B31-SSA7
80-4575 12-6-80 Removed and functionally tested per Tech Specs hydraulic snubber 2E11-RHR-R238A
80-4576 12-6-80 Removed and functionally tested per Tech Specs hydraulic snubber 2E11-RHR-R241A
80-4577 12-6-80 Removed and functionally tested per Tech Specs hydraulic snubber 2E11-RHR-R245A
80-4578 12-6-80 Removed and functionally tested per Tech Specs hydraulic snubber 2E21-R53A
80-4579 12-6-80 Removed and functionally tested per Tech Specs hydraulic anubber 2E11-RHR-R250
80-4580 12-8-80 Removed and functionally tested per Tech Specs hydraulic snubber 2T46-SGTS-R67
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RWCU pump 2631-C0013 in order to stop leak
80-4664 12-11-80 Replaced sheared off spring pins in Unit 1 to Unit 2 fuel pool cooling crosstie valve 2641-F037
80-4666 11-27-80 Changed setpoints on recorder 2D11-R619 for Rx b1dg. vent exh. hi radiation alarm 2H11-P601
80-4702 NA Calibrated under RPT breaker' ~~
under voltage ' monitors.-
2C71-K25A-F according to DCR 80-227 ad H-27605
80-4708 12-9-80 Bore all inter bowls and suction bowls to 6.100", interpellers wear, rings fabricated to .005", cut interference pr sed on impeller to 6.084" on standby service water pump 2P41-C002
80-4710 11-23-80 Adjusted spring charging switch on PSW pump 2P41-C001D
80-4714 11-20-80 Replaced RWCU pump 2631-C001A backup ring with a TEFZEL 280 backup ring per DCR 80-408
80-4725 12-9-80 Inspected station service battery chargers 2R42-5026, 5027, 5028, 5029, 5030, 2051 while performing charger load test per HNP-2-3905
80-4790 12-17-80 Tightened and adjusted operator and limit switch on vessel outlet isolation valve EBB 2G31-F.056B
80-4845 12-11-80 Adjusted, cleaned, and lubricated | torque switch on RHR drywell
isolation valve 2E11-F040
80-4856 12-23-80 Replaced solenoid and valve of chem, waste floor drain tank recire valve 2G11-F413
80-4860 12-17-80 Readjusted limits on fuel pool |
cooling and cleanup panel 2G41-P001 valve lights
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recorder 2748-R609 blue pin calibrated
(::2 80-4864 12-16-80 Moved bug source back to proper *
position and tightened all knobs on all indicators and power supplies on control rm area rad monitor indicator 2D21-K601,
80-4859 12-11-80 Pulse preamp for Unit 2 radwaste effluent radiation monitor 2D11-N007 was strapped for 16: 1 attenuation factor
80-4901 12-16-80 Repaired connector and replaced fuse for CMCAM 2D21-R167
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80-4934 12-9-80 Removed and functionally tested per Tech Specs E-system snubber 2B31-SSA21 *
() 80-4941 NA Installed test. valves P/N-152510-100 on E-system snubbers 2B31-c006 that did not have them
80-4943 NA Adjusted micro-switches on Cable spreading rm iso valve tamper alarm 2Z43-F301E
80-4978 12-9-80 Procedure HNP-2-3167 was performed on RHR pump 2E11-C001A,B,C,D
80-4982 12-16-80 Calibrated press switch on D/G air compressor 2R43-C001C
80-5021 12-17-80 Old SBLC squib valve 2C41F004A was replaced after it had been fired per HNP-2-3703 , J.
80-5022 12-17-80 Old SBLC squib valve 2d41-F004B was preplaced by new valve P/N 1532-162-01 after it had been fired per HNP-2-3702 O
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80-5039 NA Moved pipe clamp on snubber 2B21-R112 around on pipe to line up with snubber and allow free rotation; also removed paint from shaft
80-5041 NA Moved bracket holding snubber 2R21-R116 in order to allow for free rotation,
80-5050 NA Installed new gall plug, cleaned thread on plug using tap the size of 1 4/16" 12 threads per inch-
on standby liqid centrol squib. valve 2C41-F004B
80-5066 12-16-80 Removed and functionally tested per Tech Specs hydrauic snubber 2B31-SSB6
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