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I I I I I I I I I I I I I I I I I I I DESIGN AND EVALUATION OF A MODIFIED IN SITU MESOCOSM TO STUDY DENITRIFICATION IN THE KARLSRUHE AQUIFER by Jason M. Warne Bachelor of Science, Geological Engineering, 2002 A Thesis Submitted to the Graduate Faculty of the University of North Dakota in partial fulfillment of the requirements for the degree of Master of Science Grand Forks, North Dakota August 2004

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Page 1: STUDY DENITRIFICATION IN THE KARLSRUHE …apps.library.und.edu/geology/Warne, Jason, M., MS Thesis 2004.pdfSTUDY DENITRIFICATION IN THE KARLSRUHE AQUIFER by ... 2002 A Thesis Submitted

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DESIGN AND EVALUATION OF A MODIFIED IN SITU MESOCOSM TO STUDY DENITRIFICATION IN THE KARLSRUHE AQUIFER

by

Jason M. Warne Bachelor of Science, Geological Engineering, 2002

A Thesis

Submitted to the Graduate Faculty

of the

University of North Dakota

in partial fulfillment of the requirements

for the degree of

Master of Science

Grand Forks, North Dakota August 2004

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This thesis, submitted by Jason M. Warne in partial fulfillment of the requirements for the Degree of Master of Science from the University of North Dakota, has been read by the Faculty Advisory Committee under whom the work has been done and is hereby approved.

This thesis meets the standards for appearance, conforms to the style and format requirements of the Graduate School of the University of North Dakota, and is hereby approved.

/).~. ean of the Graduate School

Date

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PERMISSION

Title Design and Evaluation of a Modified In Situ Mesocosm to Study Denitrification in the Karlsruhe Aquifer

Department Environmental Engineering

Degree Master of Science

In presenting this thesis in partial fulfillment of the requirements for a graduate degree from the University of North Dakota, I agree that permission for extensive copying for scholarly purposes may be granted by the professor who supervised my thesis work, or in his absence, by the chairperson of the department or the dean of the Graduate School. It is understood that any copying or publication or other use of this thesis or part thereof for financial gain shall not be allowed without my written permission. It is also understood that due recognition shall be given to me and to the University of North Dakota in any scholarly use which may be made of any material in my thesis.

Signature

Date

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TABLE OF CONTENTS

LIST OF FIGURES ......... ...... .............. ... . .. . ..... ... ....... .............. ............. ............ vi

LIST OF TABLES ............................................................................................. viii

ACKNOWLEDGMENTS ...... .. ........... ... . . . . . ................. .. . . . . . . .......... ..... .. ........ ..... ix

ABSTRACT...................................................................................................... X

INTRODUCTION.............................................................................................. 1

MATERIALS AND METHODS......................................................................... 9

Design and Construction of the M-ISM . ... ........... ...... .... ..... .. ...... ........... 9

Top Plate Assembly................................................................... 10

Pump Housing Assembly............................................................ 10

Submersible Pump . . . . . ...... ........... .. . .. . . .. . .................. ................... 11

Final Assembly .. .. . . .. . . . . . . . .. . .. .. . .. .. .. .. . .. .. . .. . .. . .. . . . . . . . . . . . . . . . . .. . .. . . . . . . . . .. 11

Construction Time and Costs . . . . . . . . . .. .. . . . . . .. . . . . . .. .. . . .. . . . . . .. . .. . . .. . . . .. . . 12

ISM Installation and Tracer Test Initiation .............................................. 12

RESULTS AND DISCUSSION ......................................................................... 16

Sand Point Performance ........................................................................ 16

Submersible Pump Performance............................................................ 17

In Situ Tracer Test .................................................................................. 19

Denitrification . . .. . . .. . . . .. .. . . . .. . . . . . . .. . . . . . . . . . . . . . . . . . . . . .. . . . . . . . .. .. . . .. .. . .. .. . . . . . . . 19

0-ISM ............................................................................... 23

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M-ISM ............................................................................... 24

Dilution . . . . . . . . . . . . . . . . .. .. . .. .. .. . . .. .. . . . . . . . . . . . . . . . . . . .. .. .. .. . . . . . .. . . .. . . . . . . . . . . . ... . . . 34

Leakage ........................................................................... 34

Sediment Texture ............................................................. 37

M-ISM Design .. . . . . . . . .. . . . .. .. . . . . . . .. . . . . . . .. . . . . .... .... ... . . .. . . .. . . .. . . .. .. 38

SUMMARY AND CONCLUSIONS ... ..... ................ ..... ............... .... .................... 40

APPENDICES . . . .. ........... .... . . .. ... . .... ........... ... ........... ...... ... . . ....... .............. .......... 42

A. Analytical Results .......................................................................... 43

B. Pumping Rate Data for the Mini-Typhoon™................................ 49

C. Geochemical and Textural Analysis Results ............................... 51

D. Reaction Rates .............................................................................. 54

E. Annular Space Water Analysis Results ....................................... 57

F. Sediment Size Versus Dilution ...................................................... 59

REFERENCES .................................................................................................. 62

V

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LIST OF FIGURES

Figure Page

1. 0-ISM design ...................................................................................... 3

2. 0-ISM riser pipe assembly .................................................................. 4

3. M-ISM design ...................................................................................... 6

4. Pump housing assembly on the M-ISM .............................................. 7

5. Locations of IS Ms in the denitrification network ................................ 13

6. Normalized concentrations of bromide and nitrate-N in the O-ISM ... 23

7. Normalized concentrations of bromide and nitrate-N in the M-ISM .. 24

8. Zero-order denitrification rate in the M-ISM ...................................... 26

9. First-order denitrification rate in the M-ISM ....................................... 26

10. Trends in major cation concentrations in the M-ISM ......................... 27

11. Trends in major anion concentrations in the M-ISM .......................... 27

12. Saturation indices for calcite in the M-ISM ........................................ 29

13. Saturation indices for sulfate minerals in the M-ISM ......................... 31

14. Saturation indices for siderite in the M-ISM ...................................... 32

15. Saturation indices for ferric iron minerals in the M-ISM .................... 33

16. Comparison of zero-order denitrification rates of ISMs in the network ............................................................................................. 34

17. Comparison of dilution rates of ISMs in the network ......................... 35

18. Pumping rate data for the Mini-Typhoon™ submersible pump ......... 50

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19.

20.

21.

Dilution rate versus effective grain size of ISM sediments ................ 60

Dilution rate versus sand content of ISM sediments ......................... 60

Dilution rate versus clay content of ISM sediments .......................... 61

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LIST OF TABLES

Table Page

1. Major cations and anions in the 0-ISM ..................................................... 21

2.

3.

Major cations and anions in the M-ISM ..................................................... 22

Analytical results for the 0-ISM ................................................................. 44

4. Analytical results for the M-ISM ............................................................... .46

5. Geochemical analyses of soil samples from ISM sites (T. Tesfay, personal communication, June, 2004) ..................................................................... 52

6. Textural analyses of soil samples from ISM sites (T. Tesfay, personal communication, June, 2004 ) ..................................................................... 53

7. Analysis results of water from the M-ISM annular space .......................... 58

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ACKNOWLEDGMENTS

I would like to express my thanks to my chairperson Dr. Scott Korom for

his guidance and perseverance through this study and all of my academic work

here at the University of North Dakota. I would also like to thank Dr. Harvey

Gullicks and Dr. Charles Moretti for serving as members on my committee.

Funding for this project was provided by the North Dakota Department of

Health and the North Dakota State Water Commission. Support and guidance

for this project from Bill Schuh, senior hydrologist at the North Dakota State

Water Commission (NDSWC), is appreciated. In addition, I would like to thank

Eben Spencer for his assistance in sample collection and analysis, Merlyn

Skaley (NDSWC) for his assistance in sample collection, Alan Wanek (NDSWC)

for finding the sites, and the landowners for allowing us to install and sample the

ISMs on their land.

Finally, I would like to thank my family for their support and patience

through the course of my studies here at UNO: My wife Christy and my two

boys, Eithan and Kaiden.

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ABSTRACT

To simplify the in situ mesocosm (ISM) design given in Schlag (1999), a

modified ISM was designed and built in which a 6-inch long sand point replaces

three 16-inch diameter screens. The modified design also includes an optional

submersible pump mounted on top of the ISM chamber, making it capable of

applications at depths greater than those attainable using a peristaltic pump from

the ground surface. Two ISMs, one the original design (0-ISM) and the other the

modified design (M-ISM) with an optional submersible pump, were installed in the

Karlsruhe aquifer, near Minot, ND, in late June, 2003. Tracer tests were initiated

in both ISMs to monitor denitrification rates at the two sites. The analytical

results of water samples collected from the two ISMs showed no evidence of

denitrification in the 0-ISM. However, the analytical results showed that the M­

ISM had a first-order denitrification rate constant (r2 = 0.99) of 0.0031/day with

organic carbon, ferrous iron, and sulfide as the apparent electron donors. The

submersible pump experienced a minor electrical problem, but showed promise

as a means to make the modified ISM appropriate for deep installations.

X

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INTRODUCTION

Stainless steel chambers called in situ microcosms have been found to

provide a practical means by which to conduct tracer tests in shallow

groundwater studies of chemical processes. Gillham et al. (1990) used a 1.9-L in

situ microcosm to effectively isolate a portion of an aquifer from advection while

conducting a tracer test for denitrification. Gillham and his co-authors concluded

that the in situ microcosm provided a "major advantage" over previous tracer test

methods by reducing the required time and equipment, and simplifying the

interpretation of the tracer test results. Citing the success of the in situ

microcosm described by Gillham et al. (1990), Bates and Spalding (1998)

conducted a denitrification study in which a group of six 11-L in situ microcosms

were installed 4.6-m apart in an aquifer. As a result of their study, Bates and

Spalding described the in situ microcosm as a practical piece of equipment,

capable of producing consistent results that are representative of aquifer

den itrification.

While the studies by Gillham et al. ( 1990) and Bates and Spaulding ( 1998)

demonstrated that the in situ microcosm was useful, their size limited the

duration of the tracer tests and the volume of water that could be sampled.

Schlag (1999) conducted a denitrification study using two larger, 186-L chambers

which were named in situ mesocosms (ISMs). These ISMs were enlarged to

1

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accommodate a monthly sampling schedule lasting two years. The longer

testing period allowed the observation of relatively slow aquifer denitrification

reactions while larger sample volumes allowed a comprehensive water analysis

of each sample. Later, 14 additional ISMs were installed to study aquifer

denitrification processes at eight more sites in Minnesota and North Dakota.

More ISM installations have been discussed for sites in Manitoba, Montana,

North Dakota, and South Dakota.

While the original ISM design produced good results, there are aspects of

the design that could be changed to ease construction and expand its

capabilities. One disadvantage of the original ISM is that its use is restricted to

aquifers with shallow water tables because sampling must be done with a

peristaltic pump on the ground surface. A peristaltic pump, using vacuum

pressures, is unable to draw water from depths beyond approximately 25 feet

below the ground surface. Consequently, aquifers with water tables at depths

greater than about 25 feet have been excluded from ISM denitrification tracer

tests. Because denitrification is suspected to occur at these depths (Korom,

1992), the North Dakota State Water Commission (NDSWC) and the North

Dakota Department of Health (NDDH) have expressed interest in an ISM design

that would facilitate denitrification tracer tests at depths greater than 25 feet

below the ground surface.

The original ISM design (Figures 1 and 2) also uses a three-screen

assembly that spans the inside diameter of the top of the chamber. The purpose

of these screens is to allow a water sample to be drawn from the entire top of the

2

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Riser pipe and sample 1.-------- tube assembly

See Figure 2

Bumper, 5.1-cm 92.0") I.D. schedule 80 pipe

:---=-i---L--~~---=:=:::--::::; +- Top plate

~ 1.6 mesh/cm wire cloth

t--39 mesh/cm wire cloth

if---1.9-cm x 0.64-cm I expanded mesh

I I I I

),I 40.6-cm (16.0) O.D.

·---------------

Figure 1. 0-ISM design.

3

-b 0 co -E 0 I

N lO 'I""' .... (1) .0 E ca .c 0

~ (/)

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,( ~ Extended above ground surface

------- 3.8-cm (1.5") riser pipe connected to coupler welded onto top plate

------- 1.9-cm (0.75") pipe

---------0.79-cm (0.31") O.D. tubing

; 1--------- 0.79-cm (0.31") compression fitting

........ D (I) (I) -.c c.-:::J (I)

~ 0 0) (.J 0

"'O ..... ~~ ~ "fil

·- "'O

D "'O -0 (I)

:lE ==

.,.__ ______ Top half, 1.9-cm (0.75") coupler

Disk threaded and tapped for compression fitting

- 8 mesh/cm wire cloth

Bottom half, 1.9-cm (0.75") coupler

Iii --------- 1.9-cm (0. 75") threaded nipple

1.9-cm (0.75") coupler welded ..... _____ _ inside hole on top plate

Figure 2. 0-ISM riser pipe assembly.

4

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sediments in the ISM and to prevent excessive disturbance of sediments during

sampling (Schlag, 1999). While this screen assembly has given good results

(Schlag, 1999; Korom et al., in review), it is labor-intensive to construct.

This thesis presents the design, construction and use of an ISM based on

the design of the ISMs described in Schlag (1999) and Korom et al. (in review),

but with two modifications:

(1) A 6-inch long sand point was used in the modified design in place of the

three screens in the main chamber (compare Figures 1 and 3) of the

original design to simplify the construction of the ISM by reducing the

material and time required for construction.

(2) A dedicated submersible pump was added to the top of the modified ISM

main chamber (Figures 3 and 4) to allow the modified ISM to be used in

deeper applications than those attainable with a peristaltic pump.

The objective was to determine if these modifications would adversely affect

tracer test performance.

An ISM with the modifications listed above was constructed and installed

in a shallow aquifer as part of the network of ISMs described in Korom et al., (in

review). A tracer test was initiated in the ISM and water samples were collected

and analyzed. The results were compared to the analyses of water samples

from the other ISMs in the network, which were all constructed according to the

original design. The comparison suggests that the modified design produced a

higher rate of dilution of the tracer test than that of the original design; however

the relatively high dilution rate did not adversely affect the tracer test. Good

5

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------Pump housing

Cut away view of the 6.4-cm (2.5") outer riser

------ pipe containing the pump housing

,..,._ ___ _..... __ Sand point

ISM chamber 152-cm (60.0")

i+- 40.6-cm (16.0") O.D. --+1

Figure 3. M-ISM design.

6

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_...-- Coupler connecting to ~ 1.9-cm (0. 75") inner riser pipe

...,._---Top endcap including the bulkhead

------Submersible pump

ic.:::::::-----:=ii Pump Inlet

-----Pump housing

·----Bottom endcap

..,.._----Nipple connecting to sand point

Figure 4. Pump housing assembly on the M-ISM.

7

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aquifer denitrification data were produced by the modified ISM and are presented

herein. A blown fuse in the dedicated submersible pump controller caused a

minor problem. However, after replacement of the fuse, the pump continued to

perform satisfactorily for the rest of the initial tracer test and through the initiation

of a second tracer test.

8

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MATERIALS AND METHODS

To compare the time of construction, cost of materials, and performance,

two ISMs were built. The first ISM was constructed according to the original

design and construction procedures described by Schlag (1999); thus, it will be

herein referred to as the 0-ISM (see Figures 1 and 2). The second ISM differed

from the first in that the three screens in the 0-ISM were replaced with a 6-inch

sand point and a dedicated submersible pump was added to the top of the ISM

chamber (see Figures 3 and 4). Because it was modified, the second ISM will be

referred to in this paper as the M-ISM. Construction methods specific to the sand

point modification and the optional pump assembly for the M-ISM are given

below.

Design and Construction of the M-ISM

As was the case when the original ISMs were built, it was preferable to

use 316 grade stainless steel components, especially in those areas that come in

contact with aquifer sediments and water involved in the tracer test (Schlag,

1999). However, such components were not always available. The sand point

purchased for the M-ISM for example, was constructed of both 304 and 316

stainless steel. When 316 grade stainless steel components were not available,

304 grade stainless steel components were used. All welding was done with a

TIG (tungsten inert gas) welder and final welds were continuous.

9

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Top Plate Assembly

The top plate for the M-ISM began with a round, 0.64-cm (0.25") thick

stainless steel plate that was 40.6-cm (16.0") in diameter. A 5.7-cm (2.25") hole

was drilled in its center to allow a 5.1-cm (2.0") coupler to be inserted through the

plate and welded flush with the plate bottom. To create a place for the sand

point to connect to the top plate, a donut-shaped piece of 0.64-cm (0.25") thick

stainless steel plate with a 3.2-cm {1.25") hole drilled in its center was welded

inside and flush with the bottom of the 5.1-cm (2.0") coupler. To complete the

top plate assembly, the sand point was inserted into and flush with the top of the

donut hole and welded in place. The completed top plate assembly was then

positioned on top of the ISM chamber with the sand point pointed down inside

the chamber and welded in place.

Pump Housing Assembly

The pump housing was constructed of a 25.4-cm (10.0") long piece of 3.8-

cm (1.5") diameter schedule 10 pipe that was threaded on both ends. An end

cap for the bottom of the housing was constructed by welding a round 0.64-cm

(0.25") thick plate with a 1.9-cm (0.75") hole drilled in its center to the end of a

3.8-cm {1.5") coupler. One end of a 15.2-cm (6.0") long piece of 1.9-cm (0.75")

diameter schedule 10 pipe was welded to this plate and threaded on the other

end to serve as a nipple to connect to the sand point.

To keep water from rising above the pump cavity in the 1.9-cm (0.75")

inner riser pipe, a bulkhead was constructed by welding a round piece of 0.64-cm

(0.25") thick steel plate between two halves of a 3.8-cm (1.5") coupler. Holes

10

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were drilled in the bulkhead to allow power cords and the sample tube to connect

to the pump in the pump housing. A 10.2-cm (4.0") long piece of 3.8-cm (1.5")

diameter schedule 10 pipe, threaded on both ends, connected to the bulkhead

coupler. For the top of the pump housing a second end cap was constructed

with a 1.9-cm (0.75") coupler welded on the end to connect to the 1.9-cm (0.75")

inner riser pipe.

Submersible Pump

The pump used in the M-ISM was a Proactive Industries Mini-Typhoon™

submersible groundwater pump. It is a centripetal force pump with a 2.54-cm

(1.0") inlet and a 0.95-cm (0.375") I.D. discharge outlet. It is powered by direct

current supplied through a variable speed controller that connects to a 12-volt

automotive or marine battery. The controller allows the user to turn the power off

and on using a toggle switch and to vary the speed of the pump with a rheostat

dial. The pump was placed into the pump housing and its power cords and

output tube were threaded through the bulkhead. A silicone sealant was applied

to the holes in the bulkhead where the power cords and sample tube passed

through.

Final Assembly

The diameter of the pump housing required the use of a 6.4-cm (2.5")

diameter schedule 80 riser pipe. A 5.1-cm (2.0") nipple and a 6.4-cm (2.5") to

5.1-cm (2.0") reducing coupler were attached to the 5.1-cm (2.0") coupler on the

top plate. The 6.4-cm (2.5") riser pipe was then attached to the reducing coupler

in the field before installation of the M-ISM.

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All threaded connections that were to remain permanently connected were

assembled using Teflon™ thread sealing tape and medium strength (blue) liquid

thread locker. This included all threaded connections except the nipple which

connected the pump housing to the sand point in the top plate; this connection

was assembled with Teflon™ thread sealing tape only, to allow the pump

housing to be removed for pump maintenance if necessary.

Construction Time and Costs

Construction time for the M-ISM, not including the optional pump housing

assembly, was less than that of the 0-ISM because the sand point required no

preassembly before being attached to the top plate. The three screens of the 0-

ISM required approximately 5 hours of construction time to cut the screen

material to size, assemble the screens, and drill holes into the top plate of the 0-

ISM so the screens could be bolted on. The optional pump housing used on the

M-ISM required approximately 8 hours of construction time.

In general the cost of the material used to build the 0-ISM and the M-ISM

was approximately the same because the cost of the sand point used in the M­

ISM approximated the cost of the material used to make the three screens used

in the 0-ISM. The material for the optional dedicated pump and the associated

pump housing is an added cost of approximately $200, if used as on the M-ISM.

ISM Installation and Tracer Test Initiation

The M-ISM and 0-ISM were installed in the Karlsruhe aquifer near

Karlsruhe, ND (see Figure 5) in late June, 2003. The Karlsruhe aquifer is a 51.8

km2 (20 mi2) surficial outwash plain consisting of sand and lenticular beds of

12

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-------------------

~

w

·---. "'""'~'"'' __ _____,

'Mot Karlsruh~ • H Larimore

(2 sites) amar* * * Robinson

'Bismarck

nd Forks

·"·

:

'8,emidji

* .Akeley Perham-W

..,... Perham-M ·Fergus Fall,s

'St Cloud i

-! J

i'Duluth

r I

'Min?eapolis •.,

I 'Marshall

I l* Luve~: _____________ _

Figure 5. Locations of ISMs in the denitrification network.

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I I I I I I I I I I I I I I I I I I I

sandy gravel. It has an average thickness of 7.6 m (25 ft) (Randich, 1981 ). The

township and range coordinates for the 0-ISM site are 153-77-8DDA. The 0-

ISM was installed at a depth of approximately 21 feet below the ground surface.

The water table at this site was approximately 13 feet below the ground surface.

The sediments at the 0-ISM site were observed to be relatively course,

consisting of gravel with sand and a few larger cobbles mixed throughout. The

sediment was red in color indicating an iron rich environment.

The township and range coordinates for the M-ISM site are 154-77-

33DDD. Due to budget constraints and the high cost of excavation, the M-ISM

was not tested in a deep installation. Instead the M-ISM was installed at a depth

of 16 feet below the ground surface. The water table at the site was

approximately 6 feet below the ground surface and the sediments were observed

to consist of clean, medium grained sand. As the excavation neared the water

table the color of the sediment changed from a slightly red color to a grayish

color indicating a reducing environment.

In early August, 2003, we returned to purge the ISMs and to initiate tracer

tests for denitrification. The ISMs were purged by pumping out approximately

three pore volumes (185 L) of groundwater and wasting it down gradient of the

ISM. This was done to ensure that only native groundwater occupied the pore

space in the ISM chamber because water from another well was used during the

installation of the ISMs. During the purging process the submersible pump on

the M-ISM was run at different settings on the rheostat dial to determine its

pumping capabilities. The rheostat dial settings range from O to 5. It was

14

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determined that the minimum setting that would produce water was

approximately 2.5. At the maximum setting (5), the pump produced water at 3.3

Umin. To prevent the possible formation of preferential flow paths, the majority

of the purging was done at a setting of 3.5 on the rheostat dial, which

corresponded to a pumping rate of approximately 1.8 Umin.

To initiate the tracer test, approximately 80 L of groundwater water were

pumped from the ISM into a reservoir and amended with sodium nitrate (NaN03)

and sodium bromide (NaBr). The bromide was added to serve as a conservative

tracer to estimate dilution of the amended water with native groundwater in the

ISMs (Schlag, 1999; Korom et al., in review). This solution was then stirred

about every 15 minutes while it was siphoned back into the ISMs.

After amendment, the ISMs were rested for approximately one month.

After this time an ISM groundwater sampling routine was started in which

samples were collected about every two months starting at the end of August,

2003 and ending in June, 2004. Full descriptions of ISM installation, tracer test

initiation, and sampling procedures as well as sample analysis procedures are

given in Schlag (1999) and Korom et al. (in review).

15

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RES UL TS AND DISCUSSION

Sand Point Performance

One concern regarding the sand point was that the relatively small surface

area of the screens might become clogged with fine sediment, thus restricting or

stopping the flow of water during pumping events. A test of the maximum

pumping rate after the last sampling event on May 24, 2004 gave a value of 2.5

Umin. This corresponds to a 24% (0.8 Umin) decline in maximum pumping rate

from the rate determined during the purging process (3.3 Umin) at the beginning

of the study. However, it was later determined that this decline in pumping rate

was due to the two different power sources used for the two pumping rate tests.

As a result, it was concluded that any clogging of the sand point screens was

minimal, if existent at all.

Unfiltered samples from the M-ISM had low turbidity (see analytical results

in Appendix A) and contained no sand sized sediment, indicating that the

screens in the sand point were filtering adequately. The installation and testing

of an ISM with a sand point at a finer grained site, such as those studied in the

Elk Valley aquifer by Schlag (1999) and others, may prove more diagnostic of the

filtering capabilities of the sand point.

16

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Submersible Pump Performance

The submersible pump on the M-ISM functioned without incident for about

the first five months of the tracer test. During purging and amendment

procedures it was found that at the maximum controller setting (5), the

submersible pump produced water at a rate of 3.3 Umin. A graph of pumping

rate data advertised by ProActive Industries {Appendix B) indicates that the

average maximum pumping rate of the Mini-Typhoon TM at 16 feet of lift is

approximately 7.5 Umin. Therefore the maximum pumping rate of the

submersible pump in the M-ISM is 56% lower than the advertised maximum rate.

This is likely due to head loss caused by a restriction of flow through the small

screen surface area of the sand point, suction lift from the sand point to the pump

inlet, and friction losses in the discharge tubing. The table of pumping rate data

in Appendix B indicates that the Mini-Typhoon™ has a maximum lift of 43 feet.

However, because of head loss, the effective maximum lift of the pump in the M­

ISM is significantly less than 43 feet. Consequently, the maximum depth of

installation for the M-ISM using the Mini-Typhoon TM model pump is significantly

less than 43 feet below the ground surface. However, the maximum installation

depth could be increased by using a more powerful pump and using discharge

tubing that has the same inside diameter as the pump outlet to reduce head loss.

Despite the apparent head loss, the submersible pump produced water at

a maximum rate that was seven times faster than our peristaltic pump at the

depth of the M-ISM {16 feet). To prevent the formation of preferential 'flow

channels within the M-ISM it was purged at a lower rate of 1.8 Umin. This was

17

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over 3.5 times faster than the pumping rate of our peristaltic pump which has a

maximum pumping rate of about 0.5 Umin at 16 feet (the depth of the M-ISM).

The ability to purge at the higher rate with the submersible pump saved nearly 5

hours of time versus purging with the slower peristaltic pump.

The first two sampling events (8-25-2003 and 10-20-2003) were also done

using the submersible pump. The samples were taken at the minimum setting on

the pump controller that would produce water (about 2.5) to minimize the

chances of cavitation and reduce pump heating, which could potentially de-gas

the water sample. When a 0.45 micron inline filter was added to the sample

tube, the pump speed had to be increased by moving the controller dial to

approximately 2.8 to allow water to be pushed through the filter.

At the third sampling event (11-19-2003) the submersible pump did not

function. Attempts to turn it on and to adjust its speed with the controller yielded

no response from the pump. Though the pump did not function, its flow-through

design allowed the water samples to be taken using a peristaltic pump from the

surface. Therefore, the next three sampling events (12-22-2003, 2-18-2004, and

3-23-2004) were conducted using a peristaltic pump. After the March sampling

event (3-23-2004), it was determined that the cause of the submersible pump

malfunction was a blown fuse in the pump controller. The fuse was replaced and

the pump worked normally again. Therefore, the samples taken on 5-24-2004

were taken using the submersible pump. In addition, the pump continued to work

normally through the initiation of a second tracer test in the M-ISM in June, 2004.

18

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Although it would have been preferable to use the submersible pump for

every sampling event, the malfunction allowed for comparison of water quality

analytical results between water samples taken from the M-ISM with a peristaltic

pump and the submersible pump. There were no apparent trend deviations in

water quality associated with the use of the peristaltic pump versus the

submersible pump. Thus, the objective to determine if the modifications made to

the M-ISM would affect tracer test performance is met with respect to the

submersible pump.

In Situ Tracer Test

Denitrification

The four requirements for denitrification are: (1) the availability of N oxides

as terminal electron acceptors, (2) the presence of denitrifying bacteria, (3) the

availability of suitable electron donors, and (4) anaerobic or reducing conditions

(Korom, 1992). Because we are amending the ISMs with sodium nitrate, we

know that the first requirement is met. The presence of denitrifying bacteria is

assumed in this study. The availability of electron donors was determined by the

geochemical analyses of soil samples from the sites in research conducted by T.

Tesfay (personal communication, June, 2004). Preliminary results of the

geochemical analyses for all of the sites in the ISM network are shown in

Appendix C. The analysis shows that the 0-ISM sediments contain 0.252%

sulfide, 0.245% ferrous iron (amorphous), and 0.051 % organic carbon by weight.

The M-ISM sediments are shown to contain 0.194% sulfide, 0.094% ferrous iron

19

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(amorphous), and 0.017% organic carbon. The availability of these electron

donors to biogeochemical reactions is unknown.

The fourth and final requirement for denitrification, reducing conditions,

was determined based on a combination of observations and analyses. During

the installation of the M-ISM there was a noticeable change in the color of the

sediments from reddish colored to grayish colored near the water table

(approximately 6 feet below the ground surface), indicating reducing conditions.

Also, the presence of reduced (ferrous) iron in the geochemical analysis of T.

Tesfay (personal communication, June, 2004) indicates that the conditions were

reducing at the depth of the M-ISM (approximately 16 feet below ground

surface). Reducing conditions indicated by changes in sediment color were less

apparent during the installation of the 0-ISM; however, the geochemical analysis

of T. Tesfay (personal communication, June, 2004) shows an abundance of

reduced iron.

Having established that the conditions at the two sites had potential for

denitrification, it had to be determined if denitrification did indeed occur, and if so,

what electron donors took part in the denitrification reactions. The method used

in Schlag (1999) and Korom et al. (in review) was to observe trends in the

concentrations of analytes given in the water sample analysis results and match

those trends to the reactants and products of known denitrification reactions. In

this way, it was possible for them to estimate what reactions were occurring. The

trends and corresponding reactions were then used as evidence for or against

the occurrence of denitrification and the electron donors involved. The trends of

20

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I I

Table 1. Major cations and anions in the 0-ISM.

I Sampling Na+ Mg2+ K+ Ca2+ Diss. Mn Diss. Fe Date mmol/L mmol/L mmol/L mmol/L ~mol/L ~mol/L

I 08/25/03 15.1 1.82 0.263 1.51 7.94 < 0.179

10/20/03 14.6 1.90 0.276 1.55 11.1 0.358

I 12/22/03 13.1 1.71 0.253 1.46 8.48 0.197

I 03/23/04 13.2 1.77 0.266 1.52 10.2 0.233

06/01/04 12.4 1.74 0.258 1.49 10.2 0.251

I Sampling Br" NQ3--N SQ42- IC QC

I Date mmol/L mmol/L mmol/L mmol/L mmol/L

08/25/03 0.561 5.33 0.451 2.79 0.603

I 10/20/03 0.507 4.82 0.482 2.63 0.560

I 12/22/03 0.466 4.33 0.479 2.92 0.326

03/23/04 0.338 3.29 0.476 3.03 0.077

I 06/01/04 0.369 3.29 0.577 2.80 0.556

I Diss. Mn is presumed to be dissolved Mn2+

Diss. Fe is presumed to be dissolved Fe2+

IC = dissolved inorganic carbon

I QC = dissolved organic carbon

I I I I I 21

I

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I I

Table 2. Major cations and anions in the M-ISM.

I Sampling Na+ Mg2+ K+ Ca2+ Diss. Mn Diss. Fe Date mmol/L mmol/L mmol/L mmol/L ~mol/L ~mol/L

I 08/25/03 8.48 1.70 0.14 2.62 15.1 0.179

I 10/20/03 7.66 1.56 0.15 2.40 15.6 < 0.179

11/19/03 6.83 1.44 0.15 2.20 13.9 0.358

I 12/22/03 5.96 1.33 0.14 2.05 13.2 < 0.179

02/18/04 5.83 1.42 0.15 2.17 13.9 0.233

I 03/23/04 5.48 1.39 0.15 2.12 13.5 < 0.179

05/24/04 4.87 1.38 0.14 2.10 13.4 0.304

I I Sampling 8( N03--N so/· IC oc

Date mmol/L mmol/L mmol/L mmol/L mmol/L

I 08/25/03 0.637 6.30 1.19 1.51 0.19

10/20/03 0.602 5.25 1.22 1.51 0.07

I 11/19/03 0.482 3.63 1.29 1.50 0.26

12/22/03 0.457 3.08 1.23 1.52 0.13

I 02/18/04 0.413 2.43 1.20 1.53 0.02

03/23/04 0.299 1.45 1.25 1.61 0.07

I 05/24/04 0.283 1.24 1.26 1.49 0.20

I Diss. Mn is presumed to be dissolved Mn2+

Diss. Fe is presumed to be dissolved Fe2+

I IC = dissolved inorganic carbon

OC = dissolved organic carbon

I I I 22

I

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the analytes for the water samples taken from the 0-ISM and M-ISM are

described below. Reactions representing these trends are presented and used

as evidence for or against the occurrence of denitrification and the associated

electron donors at the 0-ISM and M-ISM sites.

0-/SM

Over the course of the study, five sets of water samples were taken from

the 0-ISM. Table 1 shows a summary of the analytical results for major cations

and anions in the 0-ISM from the comprehensive analyses given in Appendix A.

The results show that the B( concentration in the 0-ISM decreased from 0.561

mmol/L (44.8 mg/L) to 0.345 mmol/L (27.6 mg/L) in 211 days. Table 1 also

shows that the N03--N concentration in the 0-ISM decreased from 5.33 mmol/L

{74.6 mg/L) to 3.33 mmol/L {46.7 mg/L) in 211 days. Within analytical error{±

3% ), the decrease in the normalized B( concentration was identical to the

• Bromide - -o- - Nitrate-N

§ 1.2 ------

~ ~ j ~:: ~ ~ ~---=-==-=~" i . . t::! 0.4 f-«s E 0.2 ._ 0 z 0.0

0 100 200

Days

300

Figure 6. Normalized concentrations of bromide and nitrate-N in the 0-ISM.

23

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decrease in the normalized N03--N concentration in the 0-ISM, as shown in

Figure 6. Consequently, there does not appear to be any decrease in N03--N

concentration beyond that explained by dilution as measured by the bromide

tracer. Therefore, I conclude that there was no denitrification detected in the 0-

ISM.

M-/SM

Seven sets of water samples were taken from the M-ISM during the 273

days of the study. A summary of the analytical results given in Appendix A for

major cations and anions in the M-ISM is shown in Table 2. The results show

that the B( concentration in the M-ISM decreased from 0.637 mmol/L (50.9

mg/L) to 0.283 mmol/L (22.6 mg/L) in 273 days. Table 2 also shows that the

N03 -N concentration in the M-ISM decreased from 6.30 mmol/L (88.3 mg/L) to

1.24 mmol/L (17.4 mg/L) 273 days. A graph of the normalized concentrations of

-+- Bromide -o- Nitrate-N C:

1.2 0 15 ... 1.0 ... C: (I)

0.8 0 C: 0

0.6 0 "O (I) 0.4

.I::! ai 0.2 E ... 0.0 0 z

0 50 100 150 200 250 300

Days

Figure 7. Normalized concentrations of bromide and nitrate-Nin the M-ISM.

24

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Br" and N03--N in the M-ISM (Figure 7) shows that there is a decrease in N03--N

concentration beyond that explained by dilution of the bromide tracer.

The actual loss of N03--N, beyond that explained by dilution, was 1.56

mmol/L (21.8 mg/L). Calculating an average denitrification rate from this value

gives 5.71 µmol/L/day (0.080 mg/L/day). Figure 8 shows the amount of N03 -N

lost per sampling event which has been corrected for dilution using the Br" tracer.

The slope of the regression gives an average denitrification rate of 5.28

µmol/L/day (0.07 4 mg/L/day), which agrees closely with the calculated value.

However r2 = 0.70 for this regression. For comparison, Figure 9 shows the N03-

N loss per sampling event, corrected for dilution, as a first-order reaction [as

given by Haggerty et al. (1998), Equation 1 O]. The r2 = 0.99 for this regression,

indicating that the apparent denitrification follows first-order kinetics, and is

dependent on N03--N concentration. The slope of the regression in Figure 9

shows a first-order denitrification rate constant of 0.0031/day. Explanations of

zero-order and first-order reactions are given in Appendix D.

The major cations analyzed in the water samples taken from the M-ISM

(Table 2) include Na+, Mg2+, K+, Mn2+, and Ca2+. The changes in their

normalized concentrations throughout the study are shown in Figure 10. All of

these cations exhibit temporal trends which are attributed to dilution,

precipitation, and cation exchange. Dilution and precipitation and their possible

roles in denitrification in the M-ISM will be discussed later in this paper. Reduced

25

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:::::i' 30 -C)

E 25 -"O 20 Q)

q:: ·c:

15 ..... C Q)

10 0 z

I 5 a z 0

0

50 100

150

Days

• •

y=0.074x+6.38

R2 = 0.70

200 250 300

Figure 8. Zero-order denitrification rate in the M-ISM.

'C'

0.2

0

o -0.2 () 1:3 -0.4 ~ C -0.6

....J

-0.8

-1 0 50 100 150

Days

y= -0.0031x + 0.0082

R2 =0.99

200 250

Figure 9. First-order denitrification rate in the M-ISM.

26

300

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-+- Na --Mg -.- K 4E- Ca -o- Mn

C: 1.2 .Q -~ 1.1 -C: 1.0 (I)

u C: 0.9 0

(.) 0.8 i

.!:::! 0.7 · "ffi E 0.6 ... 0 0.5 z

0 50 100 150 200 250

Days

Figure 10. Trends in major cation concentrations in the M-ISM.

-+- DIC --S04 -.- N03-N 4E- Br

C: 1.2 B (ti

1.0 ... -C: (I)

0.8 u C: 0

0.6 (.)

i 0.4 .!:::! "ffi 0.2 E ... 0 0.0 z

0 50 100 150 200 250

Days

Figure 11. Trends in major anion concentrations in the M-ISM.

27

300

300

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iron (Fe2+) is not included in Figure 10 because its concentration remained

relatively low(~ 0.360 µmol/L) throughout the study. However, this consistently

low concentration is an important indicator of denitrification and is also discussed

later in this paper.

The major anions from Table 2 include IC (assumed to be as HC03-),

so/-, N03-, and Bf and their normalized concentrations in the M-ISM throughout

the study are shown in Figure 11. As shown, the DIC concentration remained

relatively steady over the course of the study, the S04 2- concentration showed a

slightly increasing trend, and the Bf and N03--N concentrations show a

decreasing trend until the end of the study.

If the decrease in N03-N beyond that explained by dilution is due to

denitrification, there should be evidence of one or more contributing electron

donors present in the trend analysis. The three most likely electron donors are:

. 2+ 2+ organic carbon (OC), sulfide, and metals such as Fe and Mn (Korom, 1992).

Nitrate may be denitrified heterotrophically by QC according to the

following reaction given in Korom et al. (in review)

(1)

which results in the production of CO2, or inorganic carbon (IC). The dominant

form of IC at pH values ranging from 6.5 to 8.3 is HC03- (Drever, 1997). Lab

values of pH taken for each sample set indicate that the pH of the samples from

the M-ISM ranged from 7.35 to 7.58. Therefore, the IC produced by reaction (1)

will be considered to be in the form of HC03-. The IC in the M-ISM showed no

observable trend. However, it is possible that the IC being produced by reaction 28

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{1) is being precipitated out so that an increased concentration in the water is not

seen.

A water quality modeling program known as PHREEQC (Parkhurst and

Appelo, 1999) was used to determine the saturation index {SI) of associated

minerals in the M-ISM where

SI = log (ion activitiy product/ equilibrium constant)

An SI < 0 for a given mineral indicates that the water is undersaturated with

(2)

respect to the mineral and dissolution is possible. An SI > 0 for a given mineral

indicates that the water is supersaturated with respect to that mineral and

precipitation is possible.

The SI for a mineral containing inorganic carbon is shown in Figure 12 for

the duration of the study. The figure shows that the carbonate mineral calcite, if

present, would be supersaturated in the M-ISM and would thus be capable of

precipitating out of solution. Therefore, it is possible that organic carbon

-a- Calcite {CaC03)

0.5 X (I) 0.4 "'O .E C: 0.3 0

':+:I 0.2 ~

::::, -ro 0.1 Cl)

0.0 0 50 100 150 200

Days

Figure 12. Saturation indices for calcite in the M-ISM.

29

250 300

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contributed more to denitrification than can be shown by the observed increase in

IC in the M-ISM. Figure 1 O shows that Ca2+ and Mg2+ concentrations in the M­

ISM decreased at virtually the same rate throughout the study. This suggests

that additional IC produced by reaction ( 1) may have precipitated out as a

magnesian calcite (CaC03) as reported by Schlag (1999) and Korom et al. (in

review). Table 2 shows a decrease in concentration of 0.52 mmol/L for Ca2+ and

0.32 mmol/L for Mg2+. This equates to 0.84 mmol/L of IC, which by reaction (1 ),

could account for approximately 67% of the N03--N denitrified. However, based

on the lower rate of Na+ disappearance compared to B( dilution, it is also

possible that the decrease in the concentrations of Ca2+ and Mg2+ is partially due

to cation exchange with Na+_ Therefore, the amount of nitrate denitrified by OC

is s 67%.

Nitrate may also be denitrified by autotrophic processes in which bacteria

use inorganic material for energy (Korom, 1992). An autotrophic reaction in

which nitrate is denitrified by sulfide and ferrous iron in the form of pyrite (FeS2) is

given in Schlag (1999)

2 FeS2 + 6 N03- + 2 H20 = 3 N2 + 2 FeOOH + 4 so/· + 2 H+ (3)

Denitrification by reaction (3) would result in an increase in so/· concentration in

the M-ISM as long as sulfate minerals were not precipitating out. The Sis for

sulfate containing minerals (Figure 13) indicate that the water in the M-ISM would

be undersaturated with respect to gypsum (CaS04), but supersaturated with

respect to barite (BaS04). The concentration of barium (Ba2+) in the M-ISM

decreased by 0.626 µmol/L which would result in an insignificant 0.626 µmol/L

30

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I I I I I I I I I I I I I I I I I I I

-11- Barite (BaS04) -.1:- Gypsum (CaS04)

2 X

• • Q) • • ··-=-=--- • "'O 1 C

C 0 0 :;::::i

e! ::::,

+-' -1 ctl : (/) t * • * • • •

-2

0 50 100 150 200 250 300

Days

Figure 13. Saturation indices for sulfate minerals in the M-ISM.

reduction in so/- by barite precipitation; any other so/- produced by reaction

(3) would be expected to stay in solution. Table 2 shows that the concentration

of so/- in the M-ISM increased by 0.07 mmol/L which by reaction (2) accounts

for approximately 7% of the N03--N denitrified. The Fe2+ in pyrite (FeS2)

contributes 1/15 of the denitrification caused by pyrite in reaction (3) (Korom et

al., in review) and would therefore be responsible for another 0.47% of the nitrate

denitrified.

The remaining likely electron donors are the metals Fe2+ and Mn2

+. The

Mn2+ concentration displayed a decreasing trend, which is consistent with

participation in denitrification reactions. However, the total Mn2+ decrease was

only 1. 70 µmol/L (0.096 mg/L), which would account for virtually no denitrification

of nitrate (Korom et al., in review).

31

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I I I I I I I I I I I I I I I I I I I

--- Side rite (FeC03)

0.0 X Q)

"O -0.5 C:

C: 0 -1.0 :;::::;

~ ::::, ..... -1.5 · m en

-2.0 0 50 100 150 200 250 300

Days

Figure 14. Saturation indices for siderite in the M-ISM.

Fe2+ concentrations were near or below detection limits for the duration of

the tracer test (see Table 2). Because soil samples 'from the site were found to

contain Fe2+ (0.094% amorphous), Fe2

+ concentrations in the M-ISM water could

be expected to be higher than was observed, suggesting precipitation or

participation in denitrification. Sis for the Fe2+ mineral siderite (Figure 14) show

that the water in the M-ISM was undersaturated with respect to siderite (FeCQ3)

for the entire tracer test, indicating that any Fe2+ going into solution would likely

remain there. Therefore, it is likely that the consistently low Fe2+ concentration in

the M-ISM water is explained by its participation in denitrification as suggested by

Korom (1992). Denitrification by Fe2+ can occur by the following equation given

in Schlag (1999)

which results in the production of the ferric iron mineral geothite (FeOOH). 32

(4)

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I I I I I I I I I I I I I I I I I I I

8 X (l) "O 6 ·- --

C:

C: 0 4 ~

~ :, - 2 -ro en

0 0

-.tr- Fe(OH)3 -11-Geothite (FeOOH)

-

I

50 100

I

150

Days

200 250

t

-300

Figure 15. Saturation indices for ferric iron minerals in the M-ISM.

Sis for Fe3+ containing minerals (Figure 15) show that the M-ISM was

supersaturated with respect to iron hydroxide [Fe(OH)J] and highly

supersaturated with respect to geothite {FeOOH) throughout the study. This

supports denitrification by Fe2+ according to reaction (4) and may explain the

remaining N03--N denitrified in the M-ISM.

A comparison of the zero-order rate of denitrification in the M-ISM with the

zero-order denitrification rates of other ISMs in the network is shown in Figure

16. It shows that the tracer test in the M-ISM produced a relatively high rate of

denitrification; only the denitrification rate at the Larimore site is greater.

Concomitantly, the geochemical analyses. given in Appendix C, show that the M­

ISM sediments contain a relatively high amount of total electron donors. This

suggests that the relatively high rate of denitrification observed in the M-ISM may

be due in part to the availability of electron donors at the site.

33

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I I I I I I I I I I I I I I I I I I I

.$ 0.2 co 0::: -C: >. 0.15 0 co

+:I 32 0.1 B~

I+: 0)

:S E 0.05 ·--C: (I) 0 Cl

ISM Site

Figure 16. Comparison of zero-order denitrification rates of ISMs in the network.

Dilution

The average rates of dilution are high in the 0-ISM and M-ISM compared

to the average rate of dilution of the other research ISMs in the network. The

average rate of bromide dilution for all research ISMs in the network is about

0.04 mg/L/day. Figure 17 shows the bromide dilution rate of the 0-ISM, the M­

ISM and the average bromide dilution rate of all other research ISMs in the

network. It shows that the sample-to-sample bromide dilution rate in the 0-ISM

is higher than the average bromide dilution rate, but remained inside the 95%

confidence interval of the average bromide dilution rate for all other research

ISMs in the network. Figure 17 also shows that the bromide dilution rate in the

M-ISM is well above the average bromide dilution rate for research ISMs.

Leakage

The M-ISM dilution rate is most closely matched by the Larimore 1 ISM,

which is the R-ISM and tracer test described in the Schlag (1999) denitrification

34

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-------------------

(,.) OI

1.6

1.4

1.2 C: .Q 1 -~ .... C: Q) 0.8 () C: 0

CJ 0.6 ,._

co -0 Q)

0.4 .!:::! 1i:i E

0.2 ... 0 z

0

-0.2

-0.4

0

----Akeley ----- Larimore 4 -+- Perham-W -Average

100 200

-.-Hamar Luverne

-e-0-ISM - 95% confidence

---------

300 400

Days

Larimore 2 Perham-M

--11- Larimore 1

500 600

Figure 17. Comparison of dilution rates of ISMs in the network.

----er- Larimore 3 - Robinson -.-M-ISM

R2 = 0.40

700 800 900

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I I I I I I I I I I I I I I I I I I I

study. Schlag {1999} states that the reason for the high rate of dilution in the R­

ISM during his tracer test was a leak that was discovered in one of the pipe

connections. To determine if the M-ISM was leaking, the 1.9-cm {0.75") inner

riser pipe was checked for tightness during the last sampling event {5-24-2004}.

The pipe was only able to be tightened less than % turn, and was not a likely

source for a leak.

Next, the annular space between the inner 1.9-cm {0.75") riser pipe and

the outer 6.4-cm {2.5"} riser pipe was checked for water. It was found be filled

with approximately 6 feet of water. To determine the origin of the water, filtered

samples were taken at both the top and the bottom of the water column in the

riser pipe. These samples were analyzed for both Br" and N03--N content. The

results of the analysis {Appendix E} show that the Bf and N03--N concentrations

were significantly less than 5 mg/L, indicating that the water did not come from

within the M-ISM. The top of the riser pipes were protected from infiltration by

rainwater by a 4 inch PVC protective casing. Therefore, the most likely source of

this water is groundwater entering the outer 6.4-cm {2.5") riser pipe through the

connection at the coupler on the top of the ISM chamber.

It is unlikely that the water in the annular space contaminated any of the

amended water in the M-ISM because all the connections in the 1.9-cm {0.75")

inner riser pipe were sealed with Teflon TM thread sealing tape. In addition, the

water pressure within the 1.9-cm {0.75") inner riser pipe and pump housing would

be equal to the water pressure in the annular space. Thus, there would be no

pressure gradient to cause water to enter the M-ISM chamber if a pathway

36

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I I I I I I I I I I I I I I I I I I I

existed. Because the water in the annular space was determined to be

groundwater and it is unlikely that it entered the M-ISM chamber, it was

concluded that a leak was not the cause of the high dilution rate in the M-ISM.

Sediment Texture

Because dilution is relatively high in both the 0-ISM and the M-ISM, it was

hypothesized that the dilution rate may be affected by the grain size distribution

of the sediments in which they are installed. The results of the textural analysis

of sediments from each ISM site conducted by T. Tesfay (personal

communication, June, 2004) (Appendix C) show that the sediments at the 0-ISM

site and the M-ISM site are relatively course. At the 0-ISM site, 98.2% of the

sediment by weight is sand sized or greater, with 24.8% gravel. At the M-ISM

site 97. 7% of the sediment by weight is sand sized or greater, with 8.8% gravel.

To investigate the relationship between the dilution rates of bromide in

IS Ms and the grain size of the aquifer sediments, the average dilution rates of

each research ISM in the network were plotted against the effective grain size,

percent sand, and percent clay of the sediments at their respective sites. A

graph of the average rates of dilution versus the effective grain size (d10) of

aquifer sediments for all ISMs in the network (Appendix F) shows little apparent

relationship between the effective grain size of aquifer sediments and the rate of

dilution of bromide. Likewise, a graph of the average rates of bromide dilution

versus the percent sand content of aquifer sediments for all ISMs in the network

(Appendix F) also shows little apparent relationship between the sand content of

aquifer sediments at these sites and the dilution rate of bromide the ISMs.

37

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I I I I I I I I I I I I I I I I I I I

Finally, a graph of the average bromide dilution rate versus percent clay

content of aquifer sediments for all ISMs in the network (Appendix F) shows a

weak relationship (r2 = 0.19) between the clay content of the sediment and the

average rate of dilution; specifically the higher the clay content, the lower the

bromide dilution rate. Though this relationship is weak, it does agree with the

high dilution rates at the 0-ISM and M-ISM sites, as the clay contents in the

sediments at these sites are among the lowest in the ISM network. However, the

clay contents at the 0-ISM and M-ISM sites are not significantly lower than the

clay contents at other ISM sites with much lower bromide dilution rates. This

suggests that sediment size is not a significant factor in the rate of dilution.

M-ISM Design

The most significant difference in design between the M-ISM and all other

ISMs in the network is the replacement of the three screens in the upper part of

the chamber with a sand point. This design difference seems to be the most

likely reason for the increase in dilution rate in the M-ISM. To investigate this

possibility, a review of the two designs is helpful.

The three screens in the top part of the original ISM chamber are

designed to allow water to be sampled from the entire diameter of the ISM

(Schlag, 1999). Ideally, during the injection of the amended water at the initiation

of the tracer test, these three screens would also allow the amended water to

spread across the inside diameter at the top of the chamber, promoting plug flow.

This spreading behavior could be aided by the existence of a layer of clay and silt

sized sediments under the screens, which may be deposited at the bottom of the

38

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I I I I I I I I I I I I I I I I I I I

excavation during the installation of the ISM. Ideally, this plug of amended water

would continuously fill the ISM chamber, forcing the unamended water out the

open chamber bottom. In reality, however, there is mixing of the amended and

native groundwater in the original ISM chamber during amendment.

Because the sand point in the modified ISM does not span the diameter of

the chamber, it may not allow the incoming amended water to form plug flow,

therefore letting more unamended water stay in the chamber to dilute the

amended water. In addition, the sand point may be long enough to penetrate

through the fine layer of sediment thought to be deposited during the excavation

of the hole for the ISM, and may be located in the sand of the aquifer. This sand

would likely have a greater hydraulic conductivity than the finer sediments at the

top of the chamber and would promote greater mechanical dispersion during the

amendment process, resulting in more mixing of the amended and unamended

waters. Furthermore, the continued high rate of dilution after amendment may be

the result of the formation of preferential flow paths. More testing is needed to

confirm that the modified design is responsible for the high rate of dilution and

what the specific causes are.

39

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I I I I I I I I I I I I I I I I I I I

SUMMARY AND CONCLUSIONS

This study presented an ISM based on the original ISM design given in

Schlag (1999) and Korom et al. (in review), but with two modifications:

(1) A 6-inch sand point was used in the modified design in place of the three

screens in the main chamber of the original design to simplify the

construction of the ISM by reducing the material and time required for

construction.

(2) A dedicated submersible pump was added to the top of the modified ISM

main chamber to allow the modified ISM to be used in deeper applications

than those attainable with a peristaltic pump.

The objective was to determine if these modifications would adversely affect

tracer test performance.

The use of the sand point in the new design of the M-ISM saved

approximately 5 hours of construction time compared to the 0-ISM which used

the three-screen assembly of the original design. The cost difference between

the two designs was negligible.

Although the M-ISM was not tested in a deep application due to

installation costs, the submersible pump performed well at 16 feet below the

ground surface. The only malfunction experienced throughout the study

occurred when a blown fuse in the pump controller caused the pump not to

40

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I I I I I I I I I I I I I I I I I I I

function. Once discovered, this problem was easily repaired and the pump

performed satisfactorily for the remainder of the tracer test, and through the

initiation of a second tracer test A test of the maximum pumping rate of the M­

ISM showed that there was significant head loss through the sand point and

tubing of the M-ISM. Although the performance of the submersible pump was

lower than expected, it did allow the successful collection of groundwater

samples from the M-ISM. With proper testing and sizing, a dedicated

submersible pump will allow an ISM to be used at depths greater than 25 feet

The analytical results from the M-ISM show that the denitrification and

dilution rates in the M-ISM were relatively high compared to the other research

ISMs in the network. The analytical results suggest that organic carbon and

ferrous iron were the most prolific electron donors at the M-ISM site, while sulfide

was a minor electron donor. The relatively high rate of dilution in the M-ISM may

be attributed to the geometry of the sand point However, the high rate of dilution

did not affect the results of the tracer test and good denitrification data were

collected.

In conclusion, the modified ISM design with the optional dedicated

submersible pump successfully performed its intended duties. The installation of

an ISM of the modified design in a deep installation is needed to test its true

capabilities. The limiting factor in performing these deeper tests is likely to be the

cost of installing the ISM.

41

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I I I I I I I I I I APPENDICES

I I I I I I I I I

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I I I I APPENDIX A

I Analytical Results

I I I I I I I I I I I I I 43

I

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-------------------Table 3. Analytical results for the 0-ISM.

Na Mg K Ca Mn Fe NH3-N Lab Field m~l'L mg/L mg/L mg/L mg/L m9/L m9/L eH eH

Date 08/25/03 346 44.3 10.3 60.5 0.439 < 0.010 < 0.010 7.59 7.39 10/20/03 336 46.2 10.8 62.0 0.609 0.020 < 0.010 7.63 8.31 12/22/03 301 41.5 9.90 58.6 0.466 0.011 < 0.010 7.62 7.65 03/23/04 304 43.0 10.4 61.0 0.563 0.013 < 0.010 7.73 7.75 06/01/04 284 42.3 10.1 59.6 0.558 0.014 < 0.010 7.86 7.42

NDDH WQL NDDH WQL NDDH WQL F Cl Cl HC03 C03 S04 S04 N03-N02-N N03-N

m9/L mg/L m9/L mg/L mg/L m9/L mg/L mg/L mg/L Date

08/25/03 0.089 12.9 832 < 1 58.0 43.3 78.0 74.6 ~ 10/20/03 0.092 12.4 12.1 847 < 1 48.9 46.3 61.9 67.5 ~

12/22/03 0.103 13.2 12.0 878 < 1 47.5 46.0 64.2 60.6 03/23/04 0.105 13.0 10.1 891 < 1 49.8 45.7 45.9 46.1 06/01/04 0.084 12.4 874 <1 50.5 55.4 39.2 46.1

Br Be B Al Cr Ni Cu Zn As mg/L mg/L mg/L mg/L mg/L mj;JIL mg/L mg/L mg/L

Date 08/25/03 44.8 < 1.00 366 < 50 9.07 16.4 3.12 34.3 1.2 10/20/03 40.5 < 1.00 317 < 50 8.45 21.9 3.53 38.2 1.4 12/22/03 37.2 < 1.00 346 <50 < 1.00 6.53 5.41 6.00 1.2 03/23/04 27.0 < 1.00 345 <50 33.5 5.19 4.90 2.23 1.6 06/01/04 29.5 < 1.00 337 < 50 5.35 5.56 5.00 3.51 1.2

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-------------------Table 3 cont.

Se Ag Cd Sb Ba Tl Pb Total P OH mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L

Date 08/25/03 < 1.0 < 1.00 < 1.00 < 1.00 193 < 1.00 < 1.00 < 0.004 < 1 10/20/03 < 1.0 1.23 < 1.00 < 1.00 195 < 1.00 < 1.00 < 0.004 <1 12/22/03 < 1.0 < 1.00 1.41 < 1.00 175 < 1.00 < 1.00 < 0.004 < 1 03/23/04 < 1.0 < 1.00 < 1.00 < 1.00 211 < 1.00 < 1.00 0.045 < 1 06/01/04 < 1.0 < 1.00 < 1.00 < 1.00 197 < 1.00 < 1.00 0.032 < 1

T.Alk. Lab Field T. Hard. Si02 CaC03 Conduct. Conduct. CaC03 T. Hard. Turbidity %Na mg/L mg/L mmhos/cm mmhos/cm mg/L gr/gal NTU % SAR

Date 08/25/03 21.7 682 1960 334 19 1.70 68.4 8.24

.,::.. 10/20/03 21.7 694 1890 1702 345 20 < 1.00 67.0 7.86 (.11

12/22/03 20.2 720 1830 1744 317 19 1.20 66.4 7.35 03/23/04 21.4 730 1770 329 19 < 1.00 65.8 7.28 06/01/04 20.3 716 1720 1614 323 19 < 1.00 64.7 6.87

Dissolved Inorganic Organic Total Solids Carbon Carbon Carbon mg/L mg/L mg/L mg/L

Date 08/25/03 1290 170.0 18.1 188.1 10/20/03 1210 160.4 16.8 177.2 12/22/03 1190 177.9 9.8 187.7 03/23/04 1130 184.7 2.3 187.0 06/01/04 1070 170.9 16.7 187.7

Blank= not analyzed

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-------------------Table 4. Anal}1ical results for the M-ISM.

Na Mg K Ca Mn Fe NH3-N Lab Field mg/L mg/L mg/L mg/L mg/L mg/L mg/L eH eH

Date 08/25/03 195 41.2 5.4 105 0.832 0.010 0.118 7.50 7.56 10/20/03 176 37.9 5.9 96.3 0.855 < 0.010 7.58 7.95 11/19/03 157 34.9 6.0 88.0 0.765 0.020 0.113 7.50 6.12 12/22/03 137 32.3 5.4 82.0 0.723 < 0.010 < 0.010 7.53 7.70 02/18/04 134 34.4 5.8 87.0 0.765 0.013 < 0.010 7.47 7.74 03/23/04 126 33.8 5.7 85.1 0.743 < 0.010 0.018 7.67 7.71 05/24/04 112 33.5 5.6 84.3 0.736 0.017 < 0.010 7.35 7.62

.J:,. NDDH NDDH WQL NDDH WQL O'.)

F Cl HC03 C03 S04 S04 N03-N02-N N03-N Br mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L

Date 08/25/03 0.095 5.25 463 < 1 114 109 86.4 88.3 50.9 10/20/03 0.108 4.76 466 < 1 117 110 73.5 48.1 11/19/03 0.119 4.90 456 < 1 124 119 51.5 45.0 34.3 12/22/03 0.118 5.04 464 < 1 118 118 44.2 43.1 36.5 02/18/04 0.108 4.69 477 <1 115 134 29.4 34.0 33.0 03/23/04 0.115 4.87 471 < 1 120 140 24.0 20.3 23.9 05/24/04 0.091 4.37 471 < 1 121 139 17.1 17.4 22.6

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-------------------Table 4 cont.

Be B Al Cr Ni Cu Zn As Se mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L

Date 08/25/03 < 1.00 81 < 50 2.94 6.35 1.76 4.55 < 1.0 < 1.0 10/20/03 < 1.00 < 50 < 50 4.15 4.05 < 1.00 1.75 < 1.0 < 1.0 11/19/03 < 1.00 75 < 50 5.33 4.78 4.48 < 1.00 < 1.0 < 1.0 12/22/03 < 1.00 87 < 50 1.04 3.08 2.38 7.10 < 1.0 < 1.0 02/18/04 < 1.00 88 < 50 5.80 2.75 2.23 3.01 1.4 < 1.0 03/23/04 < 1.00 88 < 50 17.9 2.83 1.67 < 1.00 < 1.0 < 1.0 05/24/04 < 1.00 64 < 50 < 1.00 4.98 1.90 1.06 < 1.0 < 1.0

~ Ag Cd Sb Ba Tl Pb Total P OH Si02

""" mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L mg/L Date

08/25/03 < 1.00 < 1.00 < 1.00 394 < 1.00 < 1.00 < 0.004 < 1 21.8 10/20/03 < 1.00 < 1.00 < 1.00 359 < 1.00 < 1.00 < 1 17.8 11/19/03 < 1.00 1.02 < 1.00 348 < 1.00 < 1.00 0.015 < 1 15.7 12/22/03 < 1.00 1.42 < 1.00 279 < 1.00 < 1.00 < 0.004 < 1 14.4 02/18/04 < 1.00 1.17 < 1.00 363 < 1.00 < 1.00 < 0.004 < 1 15.0 03/23/04 < 1.00 1.02 < 1.00 308 < 1.00 < 1.00 < 0.004 < 1 14.6 05/24/04 < 1.00 < 1.00 < 1.00 307 < 1.00 < 1.00 < 0.004 < 1 14.0

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-------------------Table 4 cont.

T.Alk. Lab Field T. Hard. Dissolved CaC03 Conduct. Conduct. CaC03 T. Hard. Turbidity %Na Solids

mg/L mmhos/cm mmhos/cm mg/L gr/gal NTU % SAR mg/L Date

08/25/03 379 1600 432 25 3.40 49.0 4.08 696 10/20/03 382 1490 1424 397 23 4.91 48.5 3.84 669 11/19/03 374 1370 1294 364 21 2.19 47.8 3.58 871 12/22/03 380 1270 1231 338 20 2.20 46.2 3.24 807 02/18/04 391 1180 1090 359 21 < 1.00 44.2 3.07 749 03/23/04 386 1140 352 21 < 1.00 43.2 2.92 716 05/24/04 386 1090 349 20 < 1.00 40.5 2.61 671

~ (XI

Inorganic Organic Total Carbon Carbon Carbon mg/L mg/L mg/L

Date 08/25/03 92.2 5.6 97.8 10/20/03 92.3 2.0 94.3 11/19/03 91.6 7.7 99.3 12/22/03 93.0 3.8 96.8 02/18/04 93.2 0.5 93.7 03/23/04 98.3 2.2 100.5 05/24/04 90.7 6.0 96.7

Blank = not analyzed

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I I I I APPENDIX B

I Pumping Rate Data for the Mini-Typhoon™

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-------------------

c.n 0

- 10. C:

:5 8 -JB 6 ro 0::: C) 4 C: C. E 2 :s a..

0

0 10

y = -0.0026x2 - 0.0989x + 9.795

R2 = 0.98

20 30 40 50

Lift (ft)

Figure 18. Pumping rate data for the Mini-Typhoon TM submersible pump.

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I I I I APPENDIXC

I Geochemical and Textural Analysis Results

I I I I I I I I I I I I I 51

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Table 5. Geochemical analyses of soil samples from ISM sites (T. Tesfay, personal communication, June, 2004).

Studl site Depth (ft) % Fe2+ (amp) % S(-1) %TOC

Akeley 15, 17 0.099 0.007 0.024

Perham-M 13, 15 0.142 0.147 0.011

Perham-W 14 0.037 0.018 0.023

Luverne 21.5 - 22.5 0.004 0.023 0.018

Hamar 18 0.004 0.011 0.041

Robinson 23.5 0.077 0.024 0.077

Larimore 16.5 0.142 0.054 0.404

Karlsruhe-0 21.5 - 22.5 0.245 0.252 0.194

Karlsruhe-M 16 - 18 0.094 0.194 0.017

amp= amorphous (non-crystaline) TOC = Total Organic Carbon These results are preliminary

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Table 6. Textural analyses of soil samples from ISM sites (T. Tesfay, personal communication, June, 2004 ).

Stud:t site Depth {ft} % Gravel %Sand %Silt % Cla:t

Akeley 15, 17 0.36 63.33 24.09 12.22

Perham-M 13, 15 0.04 96.36 0.00 4.44

Perham-W 14 8.24 88.18 0.00 4.44

Luverne 21.5-22.5 38.62 51.27 2.33 7.78

Hamar 18 1.71 89.04 4.80 4.44

Robinson 23.5 6.99 84.32 2.01 6.69

Larimore 16.5 0.00 72.96 16.56 10.48

Karlsruhe-0 21.5 - 22.5 24.76 73.42 0.00 4.44

Karlsruhe-M 16 -18 8.82 88.89 0.00 3.33

% = percent by weight These results are preliminary

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I I I I APPENDIX D

I Reaction Rates

I I I I I I I I I I I I I 54

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Zero-Order Reaction Rate

A zero-order reaction is one where the rate of the reaction is independent

of the concentration of the reactant or product so that the concentration of the

reactant decreases linearly with time. This is shown mathematically by Reynolds

and Richards (1996) as

dC =-k dt

Integrating and rearranging equation (5) gives

C=C0-kt

(5)

(6)

where Co is the initial concentration of the reactant (mg/L), k is the reaction rate

constant (mg/Uday), and C is the concentration of the reactant (mg/L) at time t

(days). Equation (6) plots as a straight line on arithmetic graph paper with k as

the slope of the line.

First-Order Reaction Rate

A first-order reaction is one where the rate of reaction is proportional to the

concentration of one reactant so that the concentration of that reactant

decreases non-linearly with time. A first-order reaction rate equation given in

Reynolds and Richards (1996) is

dC =-kC dt

(7)

Integrating and rearranging equation (7) gives

Inc= In Co kt (8)

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where C0 , k, t, and Care defined as above. Equation (8) plots as a straight line

on logarithmic graph paper with k as the slope of the line.

An equation to find a first-order reaction rate constant, corrected for

dilution using a tracer, is given in Haggerty et al. (1998) as

1n(cd J = -kt c,,

where Cd is the normalized concentration of the reactant, Ctr is the normalized

concentration of the tracer, and k and tare defined as above. Rearranging

equation (9) gives

(9)

ln(Cd )- ln(C,,.) = -kt (10)

and rearranging equation (10) gives

ln(Cd) = ln(C,,. )-kt (11)

Similar to equation (8), equation (11) plots as a straight line on logarithmic graph

paper with k as the slope of the line.

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I I I I APPENDIX E

I Annular Space Water Analysis Results

I I I I I I I I I I I I I 57

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Table 7. Analysis results of water from the M-ISM annular space.

Sampling 8( N03--N so4· Date Location {mg/L} (mg/L} (mg/L}

06/04/04 Top << 5 << 5 41.5

06/04/04 Bottom << 5 << 5 56.3

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I I I I APPENDIX F

I Sediment Size Versus Dilution

I I I I I I I I I I I I I 59

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0.12 ~---····--···················~ -···········--- ··········--·-,

0.1 .m co 0::: -§ ia' 0.08 l ~32 I • ~ §, 0.04 .. •. ____ ....:...----:-:.-----

~ 0.02 -- · ••

~ ~ 0.06 t=l R2 = 0.07

• • 0 ..... ~····- --- .. 1 ....... --··---.......,

0 1 2 3

Effective Grain Size, d10, (mm)

Figure 19. Dilution rate versus effective grain size of ISM sediments.

0.12 ~----··············-----------··············--··-······~

0.1

.m 0 co --;:; .08 0::: co C 32 0 =::::! 0.06

:;:::; C>

£5 S 0.04

0.02

• R2 = 0.03 • _______--;

• • • • 0 -t----····--~-----············~------,

0 50 100

Percent Sand

150

Figure 20. Dilution rate versus sand content of ISM sediments.

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0.12 ~--------·-············ ------------,

0.1 jg co - 0.08 0:: 32 § 'a, 0.06

:;:i E 6 - 0.04

0.02

0 -+------~--····----·······r············--~----,

0 5 10 15

Percent Clay

Figure 21. Dilution rate versus clay content of ISM sediments.

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REFERENCES

Bates, H.K., and R. F. Spalding, Aquifer denitrification as interpreted from in situ microcosm experiments, Journal of Environmental Quality, 27, 174-182, 1998.

Drever, .. I.I., The geochemistry of natural waters, 436 pp., Prentice-Hall, Upper Saddle River, 1997.

Gillham, R.W., M.J.L. Robin, and C.J. Ptacek, A device for in situ determination of geochemical transport parameters, Ground Water, 28(5), 666-672, 1990.

Haggerty, R., M.H. Schroth, and J.D. lstok, Simplified method of "push-pull'' test data analysis for determining in situ reaction rate coefficients, Ground Water, 36(2), 314-324, 1998.

Korom, S.F., Natural denitrification in the saturated zone: A review, Water Resources Research, 28(6), 1657-1667, 1992.

Korom, S.F., A.J. Schlag, W.M. Schuh, and A. Kammer Schlag, In situ mesocosms: Denitrification in the Elk Valley aquifer, in review with Groundwater Monitoring and Remediation.

Parkhurst, D.L., and C.A.J. Appelo. 1999. User's guide to PHREEQC (version 2) - a computer program for speciation, batch reaction, one-dimensional transport, and inverse geochemical calculations. U.S. Geological Survey Water Resources Investigations Report, 99-4259, Denver, Colorado.

Randich, P.G. Ground-water resources of McHenry County, North Dakota. North Dakota Geological Survey Bulletin, B-74, part Ill, 32 p., 3 pl., 1981.

Reynolds, T.D. and P.A. Richards, Unit operations and processes in environmental engineering, 798 pp., PWS, Boston, 1996.

Schlag, A.J. 1999. In-situ measurement of denitrification in the Elk Valley aquifer. M.S. thesis, Department of Geology and Geological Engineering, University of North Dakota, Grand Forks, North Dakota.

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