quality innovation plan
TRANSCRIPT
• Date : 2 Jan’14
• Reporter : Vinit Chaudhary
• Deptt : Quality
Agenda Talking Point (Discussion / Decision)
Presentation Time Spend Time
Quality Innovation Plan 2014
Leaders have to Listen 70% and suggest Opinion 30%Let’s Make a Suggestion but Don’t Blame on Other OpinionTime Is Money
MeetingRule
1. 2013 Q. Result & Review of innovation activities2. 2014 Target & action Task3. 2014 Investment plan -Appendix. - Analysis of quality KPI Issue trend &
Achievement target - Appendix Action plan quality KPI wise - Detail investment plan sheet
2 Hours 30 Minutes
•FFR To be improve through innovation and best practice implementation.•All the activities done for FFR improvement to be follow regularly.•To reduce the process issues , self/Sequential Checkpoint to be monitor by Quality Inspector on line.
2013 Quality Innovation Review Process defect Rate
Process defect Rate(PPM)
Good Point
Weak Point
Review 2013
1. PCB Rejection / Functional Issue Reduce .2. Out case gap improvement.3. HVT Rejection Reduce .4. Carton Box Moisture Issue end.5. Accessory Missing issue Reduce.6. Appearance issue detection increase.7. Rotating Ring Broken Issue decrease.
1. Harness Wire Issue Increase2. Door High Leakage issue increase.3. Door Melt Issue in 20 Ltr .4. Choke cover melt rej. Increase in 20 ltr. Model.5. 30 Ltr. Chamber fan touching .motor bracket issue.6. Convection & grill model oil fume not control.7. 30 Ltr. Convection heater IR fail rej. increase.8. Lamp fuse rej. Increase .9. Suction Fan Extra Noise Issue Increase .10. Magnetron rej. Increase.
23541
Y’12
1459038%↓
Total PPM
Process PPM
Part PPM
Y’13
15114
Y’12
10831
7444
Y’12
3829
Y’13
Y’13
28%↓
48%↓
Process defect Rate2013 Target & Task of key action
Process
1) Choke Cover Melt 20L
Current Target Tool Deptt Start End
0.08 0.06 DI Material 14’01 14’03
0.04 0.03 DI Material 14’01 14’03
0.04 0.03 DI Material 14’01 14’03
0.04 0.03 DI Material 14’01 14’03
0.04 0.03 DI Material 14’01 14’03
0.04 0.03 DI Material 14’01 14’01
0.03 0.02 DI Material 14’01 14’03
1 Level 2 Level 3 level
Design
Part
2) MWO Dead
1) Door Melt 2) Door High Leakage 3) Connector Open
1) No Issue
PDR
20%↓
`13Result
`14.Target
14590ED
Total
0.74%
0.38%
0%
4) Lamp Fuse
6) Heater Sheath IR Fail
5) Micro Mode No Power Consumption
Current Target Tool Deptt Start End
0.12 0.096 Task /DI Prod 14’01 14’03
0.03 0.024 Task /DI Prod 14’01 14’03
0.02 0.016 Task /DI Prod 14’01 14’03
0.01 0.008 Task /DI Prod 14’01 14’03
0.01 0.008 Task /DI QA 14’01 14’03
11771
3) Door Paint NG
7) Suction Fan Extra Noise
4) MWO Dead 5) Chamber Fan Extra Noise
PDR Improvement Action Plan Door Melt
Door Melt
2013(R) 2014(Tgt)
20%
0.12%0.096 %
Action Plan Tool Schedule DepttResp
Latching Issue ( 0.11 0.09Cavity Embossing issue ( 0.01 0.008 )
Special Checkpoints
• Cavity Front Plate Flatness Check
• Door Gap check on latching
• Door & cavity temp. check.
• Curling Gap in 32 Ltr.
Defect Detail
MP
Test Std
Parts
1. Door & cavity gap maintain 0.4mm by Jig.2. Door & Front plate Temp. check in LQC to ensure
latching Process3. Cavity Front Plate Flatness
Verification.4. Curling Gap Inspection
starts in LQC .
1. Embossing Height Inspection start in SQA.
2. Curling Gap inspection start in SQA.
1. Door & Front plate Temp. <90˚C. 2. Curling Gap < 0.2mm
3. Front Plate Flatness < 0.5mm
14’01
14’01
14’01
C.P Singh
Vijay
C.P Singh
Prod
Prod
QA
14’02 Vijay QA
DI
14’01
14’02
Amit
Amit
SQA
SQA
14’01
14’02
14’02
Vijay QA
Vijay QA
C.P Singh QA
DI
DI
DI
DI
DI
DI
DI
DI
PDR Improvement Action Plan MWO High Leakage
MWO High Leakage
2013(R) 2014(Tgt)
20%
0.03%0.024
Action Plan Tool Schedule DepttRespMetal Frame Fin Bend ( 0.01 0.008 )Latching NG( 0.02 0.016 )
Special Checkpoints
• Grill Bar Fitment Direction in 32 Ltr.
• Door Metal Frame Fins Alignment.
• Door and Cavity Gap should be maintain and uniform .
Defect Detail
MP
Test Std
Parts
1. Door & cavity gap maintain 0.4mm by Jig.
2. Door Metal Frame Fin Uniformity inspection .
3. Fool Proof Jig for avoid Grill Bar Reverse Fix.
1. Door Metal Frame Fin Alignment.
1. 100% Grill Bar Inspection in LQC.2. Cavity Front Plate and Door Gap Uniformity.
14’01
14’01
C.P Singh
C.P Singh
Prod
Prod
14’02
DI
14’01 Amit SQA
14’02
14’01
Vijay QA
C.P Singh Prod
C.P Singh Prod
DI
DI
DI
DI
DI
PDR Improvement Action Plan Connector Open/Loose
Connector Open/Loose
2013(R) 2014 (Tgt )
20%
0.02%0.016%
Action Plan Tool Schedule DepttRespT.T Motor Connector OpenMain Supply Connector Open
Special Checkpoints
• Connector Should be Press Properly.
• No stress allowed on wires.
Defect Detail
MP
Test Std
Parts
1. Training to Wiring Operators regular bases.
2. Two person for Connector verification.
3. Connector Operator Cross Verification .
4. Operator Skill Verification check sheet .
5. Connector verification check sheet in OQA.
1. TPA Added at Main Supply Connector.
1. 100% connector verification as per below mention process. Pull connector to hold wire Press Connector Inside move to other connector
14’01 C.P Singh
Vijay
Prod
QA
DI
DI 14’01 Mr. Kamaljeet
DI 14’01Vijay QA
Vinit QA
DI
DI
DI
DI
Vijay QA
14’01~14’03 C.P Singh Prod
Material
14’01~14’03
14’01~14’03
14’01~14’03
PDR Improvement Action Plan MWO Dead
MWO Dead
2013(R) 2014 (Tgt )
20%
0.01%0.008%
Action Plan Tool Schedule DepttRespMicro Switch Not Press ( 0.009 0.007 )Fuse Defected ( 0.001 0 )
Special Checkpoints
• Latch Board screw should not be free .
• Micro Switch To Be press completely .
Defect Detail
MP
Test Std
Parts
1. Latching Operators to be fix
2. Holder Locker Screw tight after latching with Electrical gun.
3. 100% Door open/close test in LQC.
4. Fuse 100% electrical inspection in input.
1. Door Latch Should not be warp .
2. Micro Switch Assembled at Supplier end.
1. Latch Board Screw Torque to be > 15 kgf-cm2 2. Micro Switch Should be press completely after Door open/Close operation.3. No deformation allowed in Holder Locker After ELT.
14’01
14’01
C.P Singh
Vijay
Prod
QA
DI
DI 14’01 Mr. Kamaljeet
DI 14’01 Vijay QA
DI
DI
DI
14’01 Vijay QA
14’01 C.P Singh Prod
MaterialDI 14’01
DI
DI
14’01
14’01
Vijay QA
Rakesh QA
PDR Improvement Action Plan Convection fan touching noise
Convection fan touching noise
2013(R) 2014(Tgt)
20%
0.01%0.008%
Action Plan Tool Schedule DepttResp
Fan Bubbling / Alignment NGBoss eccentric .0.01% 0.008%
Special Check Point
• Motor bracket hole CD should be match with Motor CD
• No burr Allowed at Motor Bracket Hole.
• Fan Flatness Should be OK .
• No Ring Washer Required Under Boss .
Defect Detail
MP
Test Std
Parts
1. 100% fan flatness inspection in input.
2. Jig introduced to do centric fitment of motor bracket.
3. Fan Fixing Method Change to stop fan bubbling.
1. Motor Bracket New Tool Provided to ADITYA Auto.2. Motor bracket hole ID reduced to reduce the Play between motor bracket and chamber.
1. Sound Amplifier System Introduce in FQC to Detect Minor Sounds also.
14’01 C.P Singh ProdDI
13’08DI
14’02DI
C.P Singh
C.P Singh
Prod
Prod
13’11DIADITYA Auto Tooling
13’10DI Karan Garg
R&D
14’03DI Vinit QA
PDR Improvement Action Plan Door Paint NG and Scratch
Door Paint NG and Scratch
2013(R) 2014(Tgt)
20%
0.04%0.03%
Action Plan Tool Schedule DepttResp Packing issues0.04% 0.03%
Special Check Point
1. Only one door should be in single block of box .
2. Transportation from E-Vision to E-Durables through Folk lifter instead of Hand lifter.
3. Trolleys made for painted panel .
Defect Detail
MP
Test Std
Parts
1. Packing improved like import door. 2. Only one door placing in one block of box.3. Transportation from E-Vision to E-durables through folk lifter instead of hand lifter.4. 100% door checking in input for scratch and paint NG.
1. Packing improved to avoid transportation issues.2. SQA inspection enhance S2/1.5 G1/0.64
1. 100% door checking in input.
2. Sampling in SQA , G1/0.64
13’11 E-Vision ProdDI
14’01 E-Vision ProdDI
14’01 E-Vision LogisticDI
13’11 C.P Singh ProdDI
13’11 E-Vision ProdDI
14’01 Vinit QADI
13’11 C.P Singh ProdDI
14’01 Vinit QADI
PDR Improvement Action Plan Choke Cover Melt
Choke Cover Melt
2013(R) 2014(Tgt)
20%
0.08%0.06%
Action Plan Tool Schedule DepttRespMetal Frame Fin Bend0.08% 0.06%Grill Bar Reverse Fix .
New Model Check point
• 100% inspection of door for metal Frame Fin Bend.
Defect Detail
MP
Test Std
Parts
1. Choke Cover Temperature Inspection in LQC for start 30 MWO .2. In repairing MWO For Choke Cover Melt , Operator will verify the Fins alignment .
1. Import Door SQA Inspection Start.2. Supplier Counteraction taken
1. Metal Frame Fin Alignment Inspection.
14’01 C.P Singh ProdDI
14’01 C.P Singh ProdDI
14’01 Vinit QADI
13’12 Vinit QADI
14’01 Vinit QADI
PDR Improvement Action Plan Lamp Fuse
Lamp Fuse
2013(R) 2014(Tgt)
20%
0.04%0.03
Action Plan Tool Schedule DepttResp
Part Defected0.04% 0.03%
Special Check point
• . 100% Lamp checking with Tesla jig for crack and Vacuum.
• 100% Lamp visually checking for filament loose and crack issue.
• 100% Lamp electrical testing on jig.
• Lamp Transportation via Separate vehicle to improve handling.
Defect Detail
MP
Test Std
Parts
1. Electrical Testing standard revised . Before : 1 Min on 1 Min Cool PackAfter : 1 Min on 5 Min Cool Pack2. Lamp Handling improved.
1. 100% Lamp checking with Tesla jig for crack and Vacuum.2. 100% Lamp visual inspection and Electrical testing started.
1. Lamp Packing improved for reduce crack issue.
DI 14’01 Vinit QA
DI 14’01 Ashu Store
PDR Improvement Action Plan Micro Mode No Power Consumption
Micro Mode No Power Consumption
2013(R) 2014(Tgt)
20%
0.04%0.03
Action Plan Tool Schedule DepttRespMGT 0.018 % 0.014%PCB 0.009 % 0.007 %Diode 0.003 % 0.002 %
Special Check point
• 100% PCB functional Inspection in input.
• Diode Protector Fuse Installed .
• ICTS Testing
• ELT Testing.
• MGT should not be damage .
• MGT Connector should be properly fixed.
• Diode Protector Fuse Rating.
Defect Detail
MP
Test Std
Parts
1. MGT Fixing stage shift after MWO balancing stage to avoid Jerking.2. Electrical gun using at MGT Fixing .3. 100% PCB Functional inspection in Input
1. Magnetron Specification enhance 2M214 2M2462. Diode Protector Fuse implemented .
1. HVT ICTS test , One from Each E.T.D.2. Monthly Reliability of HVT and PCB .
13’11 C.P Singh ProdDI
13’07 C.P Singh ProdDI
13’07 C.P Singh ProdDI
13’10 Mr. Sanjay QADI
13’10 Mr. Sanjay QADI
13’05 Vinit QADI
13’01 Vinit QADI
MGT Defected ( Micro Mode No Power Consumption )
Issue.
Breakthrough Add Life Cycle test to check Part reliability.
Test Condition:-Sample: 08
Test Duration: 830Hrs.
System Change
Result 2014
Anode Temp OKVoltage Cycle Test OKLife Cycle OKELT OK
Validation
MGT (0.018% 0.014%)
Contribution in Micro Mode No Power Consumption : 40%
2013 Failure Status :
Total Defects :27
Production : 147486
Rejection PPM : 183
Cause :Running part has no design margin available i.e operating at 100% Efficiency.
Due to less margin part give reliability Issue and fail itself
Main Issue:-
1.Magnet Crack
2.Anode Cap burn
2013 2014
21
183
HVD Defected ( Micro Mode No Power Consumption )
Issue.
Breakthrough
ON / OFF Limit Test to check the part Sustainability.
Test Condition:-Main AC increase and Micro Mode ON/OFF (Comparison)
System Change
Result 2014
ON / OFF Test OKELT OKLife Test OKSpike Test OK
Validation
HVD Assembly 0.003% 0.002 %
Contribution in Micro Mode No Power Consumption : 10 %
2013 Failure Status :
Total Defects :1
Production : 147486
Rejection PPM : 6
Issue
Protector Short
HV Protector change to HV fuse To reduce its failure at higher Voltages
HV Fuse
2013 2014
06
PDR Improvement Action Plan PCB Failure
PCB Failure
2013(R) 2014(Tgt)
20%
0.009%0.007
Action Plan Tool Schedule DepttResp
Part Defected0.009% 0.007%
New Model Check point
• 100% Controller checking in SQA/Input with the help of jig.
• Wristband should be available at all stages of wiring.
• All defects sharing with LGETA .
Defect Detail
MP
Test Std
Parts
1. 100% Controller using on line after verification of SQA.2. On line wristband tester introduce to avoid ESD failure.3. Wristband provide to All PCB wiring operator.
1. Share the defect with the works, and pay attention to the delivery process: a: IMD, SMT, handing insert, EMS movement b: ICT 、 FCT inspection C: Repair unit
2. Relay, VFD a: Defect collection, and send back to manufacture for analysis and improvement b:defect rate control:
1. Monthly Reliability of PCB .
13’07 Prakash QADI
13’06 Chetna ProdDI
14’02 Chetna ProdDI
13’12 Mr. Rajendra
DI Material
13’12 Mr. Rajendra
DI Material
13’01 VinitDI QA
PDR Improvement Action Plan MWO Dead
MWO Dead
2013(R) 2014 (Tgt )
20%
0.04%0.03%
Action Plan Tool Schedule DepttRespPCB ( 0.013% 0.010% )Harness ( 0.012 % 0.009%)Holder Locker( 0.004 % 0.003%)Diode ( 0.002% 0.001%)
Special Checkpoints
• Wire Harness Main Connector Should not be open.
• Micro Switch Lock Should Not Be Broken.
• PCB Inspection Marking Should be Available.
Defect Detail
MP
Test Std
Parts
1. 100% PCB inspection start in SQA/Input.
2. Latch Board Screw re-tight by electrical gun after latching.
3. 100% Marking on latch board switch lock in 32 ltr.
4. 100% Harness Main Connector open/loose inspection .
1. PCB Fuse and Diode Quality improved.
2. Micro Switch Assembled at Supplier end.
3. Latch Board material change soft to hard.
4. Diode Protector Fuse Implemented
5. TPA Added in main connector harness.
1. Latch Board Screw Torque to be > 15 kgf-cm2.
13’07
14’01
Prakash ProdDI
DI 13’11 R&D
DI
DI
DI
14’01
14’01 C.P Singh Prod
Material
DI 13’12
DI 14’01 Vijay QA
DI 14’02
DI 13’10
DI 13’11
Mr. Rajendra
Mr. Karan R&D
Mr. Nishant
Mr. Sanjay QA
MaterialMr. Rajendra
C.P Singh Prod
C.P Singh Prod
PCB Failure Issue
Issue.
BreakthroughPower ON/OFF test for New PCB Design
Test Condition:-AC input up to 500V and ON/OFFUnit (Comparison Test)
System Change
Result 2014
Spike Test OKVoltage Cycle OKON / OFF Test OK
Validation
PCB (0.013% 0.010%)
Contribution in Micro Mode No Power Consumption : 10 %
2013 Failure Status :
Total Defects :20
Production : 147486
Rejection PPM : 135
Main Issue:-
1.No Power
2.Cleaning
No Power Improvement
1. Fuse change to PTC
20L / 32L
Cleaning Issue:
Conformal Coating Applied
(20L / 21L / 28L / 32L)
2. Bridge Diode change to Discrete
(Vrrm Specs change 600 to 1000V)
20L / 32L
Issue Cause / Analysis Schedule Issue
Door switch Drop (soft lock)
Logic Tree Analysis Improvement Door switch Adjust (soft lock)Model : 32 Ltr convection
Sof
t loc
k is
sue
POM is soft and self lubricating material
it leads to improper switch operation in field
Conclusion
While repeated forcefully Opening and closing the door , switch fixing area becomes weak
Due to repeated pressing the switch fixing area further reduces in strength
Currently using latch board with POM material
NEED to develop latch board with hard material such as PBT as per Korea guide lines
Developed new latch boardWith PBT material as per global guide line.PBT is hard and brittle compared to POM so no chance of soft lock
POM Latch Board
Analysis
Harness TPA Addition
Reason :
Part :
- Harness connector in not TPA type
- Harness same blue color wire on two terminals
may cause connection error
- PCB Main (Power) Connector wire loose/open.
• No Display
• Intermittent Display
PCB Dead/Not working :
NG
Loose/Broken
Process :- Harness lot , sample basis checking in SQA
(visual inspection)
Action Plan:
Part :
- Add TPA in harness all models
-Make different wire colors in
harness to avoid connection
error
(With TPA)
TPA: Terminal Position Assurance
Process :
- Harness lot - To check 100% loose
connection at SQA
Issue Cause/Analysis Schedule
PDR Improvement Action Plan Suction Fan Extra Noise
Suction Fan Extra Noise
2013(R) 2014(Tgt)
20%
0.03%0.02%
Action Plan Tool Schedule DepttResp
Suction Fan0.02% 0.015%Suction Guide 0.01% 0.008%
Special Check point
• 100% Fan Alignment.
• Jig to be use at Fan Fixing and Motor Fixing Stage.
Defect Detail
MP
Test Std
Parts
1. Suction Fan Alignment Checking in input. 2. Suction Fan to be Fix by Jig to avoid mishandling.3. Suction Guide to be place on Jig before fixing the Motor to avoid bending.4. Sound Amplifier implemented in FQC to detect minor sounds.
1. Suction Fan Packing improved . Normal box to pizzon box.
2. Suction Guide Rib Strength increased to avoid bending.Fan Center Location Shift
1. 100%Suction Fan Flatness
14’01 C.P Singh ProdDI
14’01 Chetna ProdDI
14’02 Chetna ProdDI
13’12 Mr. Rajendra
DI Material
13’12 Mr. KaranDI R&D
14’01 C.P SinghDI Prod
14’03 Vinit QADI
Issue Cause / Analysis ScheduleSuction Guide Noise Issue
Cause and Inspection and Root cause
a)Noise from suction guide.
Inspection
■ Improvement Countermeasure
• Model / Tool : All• Country : India.• Issue occur : Field Claim
Phenomena : Noise from MWO
1.Noise from Suction Fan
Set Analysis
100% Check on prod line-Noise Chamber■ Analysis
a) Fan blade touching to suction guide.b) Filter assy vibration noise.c) Fan motor vibration.
Noise-chamber-ED
a) Fan blade touching to suction guide. Fan centre location shifted.
b) Filter assy vibration noise. Emboss added for filter assy support
c) Fan motor vibration. All emboss with same height.
2013 Quality Innovation Review SQA PRR
SQA PRR (PPM)
LRN
13160
1631613053
`12.Result
`13.Target
`13.Result
Good Point
Weak Point
Review 2012
Major issue status(YTD)
1. Roti Bar & Handle Quality Improved from vendor end2. Shelf High & Low Quality Improved From Vendor end3. 32L Latch Board Quality Improved 4. 32L Glass Tray Quality Improved5. 32L Model Controller Electrical Issues Decrease.6. Carton Box Moisture Issue decrease.7. Micro switch assembled at supplier end , lock broken
issue decrease.8. Heater Sheath removed ( Rejection was high )9. Cavity Rejection decrease . 10. Magnetron Quality Improved.
1. Heater Sheath HV/IR fail Increase2. Lamp rejection Increased3. 20 L grill Model Controller PCB rejection Increase4. Key Membrane defect increase.5. EPS Quality Issue increase.6. Glass tray crack line issue increase.7. Door Choke Cover Out issue increase.8. Controller Knob Free Issue increase.
19.34%
SQA Improvement Action Plan
Action Plan Tool Schedule DepttResp
Sheet Metal
Molding
Packing separator use each part protection for rubbing each other
Inspection Strenghtening before & after Assly
Mold Preventive maintenance schedule revised from 30 15days for flash issue.
DI Jan’14 Material
New Tool making for back cover.
8742
33%
`14 Tgt
13160
`13 (Result)
PDI Process Strengthening – Inspector Job RotationSQA Inspection Strengthening – Sample selection criteria revision
Time Check Process Strengthen For paint process
DI Sandeep
Handing improvement At Supplier End DI Mr. Kamaljeet Material
SQA
Packing Issue
Color Carton Box to be change in Khaki box to reduce moisture over issues.
DI Mat/SQA/R&D
1 Level 2 Level 3 level
Back Cover , - 18% - Black line & yellow mark
Steam Shelf- 11%
-Black Mark & Burr &Handle Welding Broken
Shelf High & low- 5%
- Welding Mark & Polishing NG
Door Assembly - 8%
Choke Cover Cut (During Removing
Flash) ,Flash in Choke cover Sealant out & paint
NG, Paint NG
,Scratch, Choke cover out
Carton box– 12%
Moisture Issue
Packing Table 32L- 3%
Less Height from one side
Mold Preventive maintenance schedule maintain at supplier end for EPS Mat/
SQA/R&D
DI
DI
DI
DI
Jan’14
Jan’14
Jan’14
Jan’14
Mr. Kamaljeet
Jan’14 MaterialMr.
Kamaljeet
Jan’14 SQAVinit
Jan’14 SQAVinit
Mr. Kamaljeet
Mr. Kamaljeet
Outgoing Quality Assurance2014 Target & Task of key action
Appearance
1) Paint Over DFT2) Glass Tray Strucking3) Door Paint Peel Off 4) MWO Dirty5) Wrong Screw Use6) Grease Missing 7) Screw Free8) Rotisserie Bar thickness Over9) Door Melt10) Door Glass Broken
Current Target Tool Deptt Start End19% 0 DI QA 14’01 14’0310% 0 DI QA 14’01 14’0310% 0 DI QA 14’01 14’035% 0 DI PROD 14’01 14’035% 0 DI PROD 14’01 14’035% 0 DI PROD 14’01 14’035% 0 DI PROD 14’01 14’035% 0 DI QA 14’01 14’035% 0 DI PROD 14’01 14’035% 0 DI QA 14’01 14’03
1 Level 2 Level 3 level
Design
Functional1) Lamp Fuse 2) Suction Fan Extra Noise3) Chamber Fan Extra Noise4) Back Cover Extra Noise
1) No Issue
OQA
20%↓
`13Result
`14.Target
2.5%
2.0%
28%
72%
0%
Current Target Tool Deptt Start End10% 0 DI Material 14’01 14’0310% 0 DI QA 14’01 14’035% 0 DI QA 14’01 14’035% 0 DI QA 14’01 14’03
2013 Quality Innovation Review OQA
OQA (PPM)
28082087
`13 Tgt `13 Result
3709
`12 Ach
E-Durables
43%↓
Good Point
Weak Point
Review 2013
1. Ring melt not found in ELT2. Extra screw in machine & screw loose not in OQA
ELT3. Power cord rej. Control.4. Screw Free Issue reduced.5. Part 3F Improved.6. Connector Open/Loose issue detection enhance.7. Part Failure ( MGT & T.T Motor reduce )8.
1. TT Motor not Work 2. Over DFT in Cavity & Outcase found in OQA & ELT3. Lamp fuse in ELT4. M/C Dead (capacitor & Diode Defective)5. MWO Extra Noise Issue Increase .
OQA Improvement Action Plan
Action Plan Tool Schedule DepttResp
1711
20%
`14 Tgt
2087
`13 (Result)
Reason: Lamp DefectedAction Plan: 1) Lamp Handling improved.2) Electrical Testing Started3) Lamp Packing Improved.
1 Level 2 Level 3 level
Reason: Fan Blade Alignment NG Action Plan: 1)100% Suction fan Alignment inspection2)Jig introduce for fan fixing.3)Noise Detection enhance
Reason: Back Cover Cocking Open Action Plan: 1)SQA JIR Revised .2)Noise Detection Enhance
Reason: Chamber Fan Bush touchingAction Plan: 1)Motor Bracket Hole ID Reduce.2)Jig Introduced for centric fitment of fan3)Fan Fixing Method Revised4)100% fan flatness inspection 5) Noise Detection enhance
1) Lamp Fuse
2) Suction Fan Extra Noise
3) Chamber Fan Extra Noise
4) Back Cover Extra Noise
14’01 QADI Vinit
14’01QA/ProdDI
14’01 QADIVinit/C.P Singh
14’01 QADI Vinit
Vinit/C.P Singh
OQA Improvement Action Plan
Action Plan Tool Schedule DepttResp
1711
20%
`14 Tgt
2087
`13 (Result)
1 Level 2 Level 3 level
1) Paint Over DFT
Reason : Reworked cavity /OutcaseAction Plan: 1)Properly sanding cavity/ Outcase before repaint and marked rework cavity100% cavity inspected for over DFT.
2) Glass Tray Strucking
Reason: Cavity Embossing Height LessAction Plan: 1) SQA JIR Revised.2) Category wise Embossing Height Controlled .3) LQC Work instruction revised.
3) Door Paint Peel Off
Reason: Door Paint Not DryAction Plan: 1)Oven Temperature To be interlock with Conveyor.2) Sample Size Increase in SQA . 5 Nos 20 Nos
4) MWO Dirty
Reason: Dirty Hand GlovesAction Plan: 1)Time Check For Hand Gloves 2)Cleaning Cloth Change After Every 2 Hours.
14’01 QADI Vinit
14’01 QADI Tirath
14’01 QADI E-Vision
14’01 ProdDI C.P Singh
OQA Improvement Action Plan
Action Plan Tool Schedule DepttResp
1711
20%
`14 Tgt
2087
`13 (Result)
1 Level 2 Level 3 level
5) Wrong Screw Use
Reason : Reworked cavity /OutcaseAction Plan: 1)Properly sanding cavity/ Outcase before repaint and marked rework cavity100% cavity inspected for over DFT.
14’01 QADI Vinit
6) Grease Missing
Reason : Skip by operator.Action Plan: 1)W.I Revised at Door Fixing Stage.2) Latching Operator will verify the same.
7) Screw FreeReason : Pneumatic High Torque.Action Plan: 1) FRL used at Outcase fixing stage
8) Rotisserie Bar Thickness Over
Reason : Thickness Error from supplier end.Action Plan: 1) 100% roti bar thickness inspection in input.2) In New Models Multi Roti Bar removed.
9) Door Melt
Reason : Cavity Front Plate Flatness Issue.Action Plan: 1) 100% Cavity Flatness Inspection in Input.2) Cavity JIR Revised.
10) Door Glass BrokenReason : Door Glass DefectedAction Plan: 1) Glass Reliability test Done At LG end .
14’01 QADI Vinit
14’01 QADI Vinit
14’01 QADI Vinit
14’01 QADI Vinit
14’01 QADI Vinit
2013 Quality Innovation Review OQA
FFR (%)
6.45
`13 Tgt `13 Result
7.43
`12 Ach
E-Durables-1.28%↓ Good Point
Weak Point
Review 2012
1. PCB Rejection / Functional Issue Reduce .2. Out case gap improvement.3. HVT Rejection Reduce .4. Carton Box Moisture Issue end.5. Accessory Missing issue Reduce.6. Appearance issue detection increase.7. Rotating Ring Broken Issue decrease.8. Lamp Failure decrease.
1. Harness Wire Issue Increase2. Door High Leakage issue increase.3. Door Melt Issue in 20 Ltr .4. Choke cover melt rej. Increase in 20 ltr. Model.5. 30 Ltr. Chamber fan touching .motor bracket issue.6. Convection & grill model oil fume not control.7. 30 Ltr. Convection heater IR fail rej. increase.8. Lamp fuse rej. Increase .9. Suction Fan Extra Noise Issue Increase .10. Magnetron rej. Increase.
7.53
FFR Improvement Action Plan
Action Plan Tool Schedule DepttResp
5.60 %
25%
`14 Tgt
7.53%
`13 (Result)
1 Level 2 Level 3 level
1) Magnetron Failure Issue
2) PCB Failure Increase
3) Diode Failure Increase
4) MWO Damage Issue
5) Non Part Issues
6) Latch switch Adjustment Issue .
7) Convection Fan Extra Noise
8) Suction Fan Extra Noise 9) Glass Tray Movement Free
10) Connector Open
D.I
D.I
D.I
D.I
D.I
D.I
D.I
D.I
D.I
D.I
13’09 – 13’12
13’09 – 13’12
13’09 – 13’12
13’09 – 13’12
13’09 – 13’12
13’09 – 13’12
13’09 – 13’12
13’09 – 13’12
13’07– 13’09
13’09– 13’12
R&D
EMS/R&D
R&D
EMS / R&D
EMS
EMS/R&D
EMS/R&D
EMS/R&D
R&D/Material
EMS/R&D
Mr. Dinesh
Mr. Dinesh
Mr. Dinesh
Mr. Karan
Vinit / C.P Singh
Mr. Karan
Mr. Karan
Mr. Karan
Mr. Karan
VinitMr. Dinesh
Part FFR - MGT
Issue.
Breakthrough Add Life Cycle test to check Part reliability.
Test Condition:-Sample: 08
Test Duration: 830Hrs.
System Change
Result
Anode Temp OKVoltage Cycle Test OKLife Cycle OKELT OK
Validation
Lvl 3 : Highest level in Divison, Lvl 2 : IL first, Lvl 1 : New standardized concept product
MGT (1.66%)
FFR Contribution 19%Cause :Running part has no design margin available i.e operating at 100% Efficiency.
Due to less margin part give reliability Issue and fail itself
Plan 1 2 3 4 5 6 7 8 9 10 11 12
Y'12R 1.65 1.69 1.66 1.68 1.69 1.75 1.89 2.15 2.71 2.60 2.17 1.76Y'13T 1.70 1.55 1.41 1.32 1.23 1.13 1.07 1.00 1.00 0.93 0.77 0.70Y'13R 1.59 1.46 1.40 1.33 1.25 1.20 1.32 1.41 1.66 1.78%Imp 4% 13% 16% 21% 26% 31% 30% 34% 39% 32%
Main Issue:-
1.Magnet Crack
2.Anode Cap burn
30%
Part FFR - PCB
Issue.
BreakthroughPower ON/OFF test for New PCB Design
Test Condition:-AC input up to 500V and ON/OFFUnit (Comparison Test)
System Change
Result
Spike Test OKVoltage Cycle OKON / OFF Test OK
Validation
Lvl 3 : Highest level in Divison, Lvl 2 : IL first, Lvl 1 : New standardized concept product
Plan 1 2 3 4 5 6 7 8 9 10 11 12
Y'12R 0.69 0.67 0.61 0.57 0.53 0.49 0.51 0.59 0.76 0.83 0.77 0.68
Y'13T 0.68 0.65 0.61 0.6 0.58 0.55 0.54 0.53 0.54 0.55 0.52 0.49
Y'13R 0.63 0.58 0.53 0.51 0.47 0.47 0.56 0.63 0.77 0.85
%Imp 9% 14% 12% 12% 12% 3% -11% -7% -2% -2%
PCB (0.78%)
Contribution 9%
Main Issue:-
1.No Power
2.Cleaning
No Power Improvement
1. Fuse change to PTC
20L / 21L / 28L / 32L
Cleaning Issue:
Conformal Coating Applied
(20L / 21L / 28L / 32L)
2. Bridge Diode change to Discrete
(Vrrm Specs change 600 to 1000V)
20L / 21L / 28L / 32L
20%
Part FFR - HVD
Issue.
Breakthrough
ON / OFF Limit Test to check the part Sustainability.
Test Condition:-Main AC increase and Micro Mode ON/OFF (Comparison)
System Change
Result
ON / OFF Test OKELT OKLife Test OKSpike Test OK
Validation
Lvl 3 : Highest level in Divison, Lvl 2 : IL first, Lvl 1 : New standardized concept product
HVD Assembly 0.38%
FFR Contr. 4%
Plan 1 2 3 4 5 6 7 8 9 10 11 12
Y'12R 0.22 0.22 0.22 0.21 0.19 0.18 0.17 0.18 0.20 0.21 0.19 0.20Y'13T 0.23 0.25 0.26 0.27 0.27 0.27 0.26 0.25 0.25 0.26 0.23 0.21Y'13R 0.23 0.26 0.29 0.30 0.32 0.33 0.34 0.34 0.38 0.42%Imp -7% -16% -33% -45% -66% -82% -98% -91% -88% ####
Issue
Protector Short
HV Protector change to HV fuse To reduce its failure at higher Voltages
HV Fuse
15%
Part FFR - Door
Issue Breakthrough- Drop height increase 60 100 cm.
- Ball impact test included to check glass strength.
System Change
Result
Transportation Test OKLQC Door Melt Improve
Validation
Lvl 3 : Highest level in Divison, Lvl 2 : IL first, Lvl 1 : New standardized concept product
FFR 0.26%
Contri: 3%
Monthly Trend (New FFR)
Cause : Door handle hit on front side
because of less margin. Hinge dimension not maintained
as per spec.
Main Issue:-
1. Door Glass Broken
2. Choke Cover Melt
Improvement : New integrated packing design with increased depth and height . New hinge tool (progressive ) developed
Before After
Apply Date: New Packing: 32L Jan’13 28L Feb’13 21L Oct’13 New Hinge Tool : 28L ->May’13 21L ->Jun’13
10%
Non Part
Issue.
Breakthrough System Change
Result
Validation
Lvl 3 : Highest level in Divison, Lvl 2 : IL first, Lvl 1 : New standardized concept product
Non Part 3.63%
FFR Contribution 46%
•TPA Added in Harness
•All Dealer Call will go in Non FFR code
•100% Checking on line for loose connection.
•QRG added for installation issues.
•Suction Guide centering done
•Vinyl Bag change to Lami Bag to improve scratch issues
•Conformal coating applied on PCB to •Improve PCB related issue.
•Std. demo guide for service engineers to improve demo quality.
•HV Protector change to HV Fuse
•Lamp packing improved
• Electrical gun used for latch board tightening instead of manual
• Continuous Feedback to production line for non part issues.
• Add Inspection on critical stages
6M FRR showing improvement trend
10%
Main Issue:-
1. Part Adj– Harness/Fuse/Door switch
2. Cleaning– Cavity/Glass Tray
3. Electrical – House wiring/Socket
4. Explanation– Functional/Recipe related
Issue Cause / Analysis Schedule Issue
Non Part - Door switch Adjust (soft lock)
Logic Tree Analysis Improvement Door switch Adjust (soft lock)Model : 32 Ltrconvection
Sof
t loc
k is
sue
POM is soft and self lubricating material
it leads to improper switch operation in field
Conclusion
While repeated forcefully Opening and closing the door , switch fixing area becomes weak
Due to repeated pressing the switch fixing area further reduces in strength
Currently using latch board with POM material
NEED to develop latch board with hard material such as PBT as per Korea guide lines
Developed new latch boardWith PBT material as per global guide line.PBT is hard and brittle compared to POM so no chance of soft lock
StatusFPA completed4M completed
POM Latch Board
Costing MP
11th May 14th May
Schedule:
Analysis
Trial
Issue Cause / Analysis Schedule Issue
Non Part -Guide Chamber Noise Issue
Logic Tree Improvement Bush touch noise in convection chamber
Noi
se Motor shaft misalignment
Conclusion
Motor bracket warpage
Analysis
Fan Blade warpage
Bush touching in guide chamber
Motor bracket draw height NG
1.Motor bracket hole more than outer chamber
2.Hole size mismatch give rise to play in the
assembly .
Tool modification done for motor bracket hole 5 mm -- > 4.2
4.2 mm
Before After
5 mm
Tool modified : 9th Apr’13
Stock Available : 1000
Implementation: 15th Apr’13
Guide Chamber Assembly
5 mm
M 4
Bush
Motor Shaft
Chamber Wall
Bush Touch with inner chamber
Outer chamber wall
12+0.2 mm
4.5 mm
Issue Cause / Analysis ScheduleNon Part – Suction Guide Noise Issue
Cause and Inspection and Root cause
a)Noise from suction guide.
Inspection
■ Improvement Countermeasure
• Model / Tool : All• Country : India.• Issue occur : Field Claim
Phenomena : Noise from MWO
1.Noise from Suction Fan
Set Analysis
100% Check on prod line-Noise Chamber■ Analysis
a) Fan blade touching to suction guide.b) Filter assy vibration noise.c) Fan motor vibration.
Noise-chamber-EDNoise-chamber-amber
a) Fan blade touching to suction guide. Fan centre location shifted.
b) Filter assy vibration noise. Emboss added for filter assy support
c) Fan motor vibration. All emboss with same height.
Defect Phenomenon
Non Part : Glass Tray Fitment Issue
Cause/Analysis Issue Cause/Analysis Schedule
ScheduleGlass tray fitment issue in 20L
models1. Turntable assy not supported at the centre unlike
other categories.2. Depth of glass tray rib is less for roller rotation.
Before AfterSamplereceive
10/6
ProductTest
17/6
PO
18/6 25/8
Apply
Rib
PO
22/7 25/7
ETD
Revised Schedule
July Opening - 10000In transit - 1344July ETD - 3000 – 7th Jul - 17160– 23rd Jul Aug ETD - 8064 – 11th Aug 39586
Apply
25/8
15/911/8
PCB- Harness TPA Addition
Reason :
Part :
- Harness connector in not TPA type
- Harness same blue color wire on two terminals
may cause connection error
- PCB Main (Power) Connector wire loose/open.
• DOA/
• No Display
• Intermittent Display
• Wiring Adj.
PCB Dead/Not working :
NG
Loose/Broken
Process :- Harness lot , sample basis checking in IQC
(visual inspection)
Action Plan:
Part :
- Add TPA in harness all models
-Make different wire colors in
harness to avoid connection
error
(With TPA)
TPA: Terminal Position Assurance
Process :
- Harness lot - To check 100% loose
connection at IQC
Issue Cause/Analysis Schedule
Return
Issue.
Breakthrough System Change
Result
Validation
Lvl 3 : Highest level in Divison, Lvl 2 : IL first, Lvl 1 : New standardized concept product
Return FFR 0.24%
Contribution 2.7%
Monthly Trend (New FFR)
1. Packing Improvement for dent
2. Lami bag added for scratch
3. TPA addition in harness
4. Policy change for return DR GR
Drop height increase
60 100 cm.
6M FFR also showing improvementMain Issue:-
1. DOA– PCB/MGT
2. Dent/Scratch
3. Customer Dissatisfaction
10%
Issue Cause / Analysis Improvement/Schedule
Improvement Idea : 1) New integrated packing design with 50 mm
Height increased 2) Increased drop test height 0.6m 1m
Implementation: Issue : Outcase Dent Analysis :
Outcase Case Dent during transit.
Before After
Simulation : - Transportation test done with integrated
packing and increased ht 0.61m - No dent on outcase observed. Packing Upper :-
Height increase by 50mm
Return: Packing Improvement- Out Case Dent
Model wise apply date: