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  • 8/15/2019 Production Operations (16pages)

    1/1662 MARCH 1999 •

    Most oil wells producing from the

    Glauconite YY pool of the Lake Newell fieldin southern Alberta, Canada, have very

    high flow capacities. Wellbore operations

    are complicated by the slant-well configu-

    rations, with surface angles of 45° increas-

    ing up to 75° bottomhole and horizontaldisplacements in excess of 6,600 ft. After

    discovery of the Countess upper MannvilleYY pool in 1989, a marine three-dimen-

    sional-seismic program, shot in 1991,showed that the reservoir extended 1.25

    miles underneath the manmade Lake

    Newell. The reservoir was developed with

    14 producers and one injector. Eleven of 

    the 15 wells were slant drilled from a padlocation where drilling begins at an angle of 

    up to 45° at surface (Fig. 1). The original

    oil in place was estimated to be 15 mil-

    lion bbl, with ultimate recovery estimated

    at 8.8 million bbl. Primary production

    began in January 1990, and water injectionwas implemented in July 1993.

    Because of the reservoir’s high permeabil-

    ity, most wells in the reservoir have high

    productivity indices. Any pressure drop

    within the system has a significant impacton productivity. All wells flowed initially,

    but shortly after the initiation of water

    injection, water cuts increased and artificial

    lift was installed. Gas lift was selected

    because of the availability of compressioncapacity, infrequent workovers, low operat-

    ing costs, exceptional well inflow capabili-

    ty, lack of wellbore restrictions for produc-

    tion logging and pressure surveys, and lowrisk of a potential oil spill in an environ-mentally sensitive area.

    OPTIMIZATION OPPORTUNITY 

    To evaluate waterflood performance, thereservoir was divided into three areas on the

    basis of structure and net oil pay. Pressure

    was maintained in Areas 1 and 2, but

    increasing water cuts of 70 to 90% resulted

    in steeply declining oil-production rates.The reserves-life indices (remaining reserves

    divided by current production rate) of thesetwo areas were in excess of 15 years com-

    pared with the desired 4 to 7 years. Cement-squeeze operations were performed on the

    wells without success. A review of the pro-

    ducing wells in Areas 1 and 2 indicated that

    gas-lift optimization was necessary to

    increase drawdown and oil production andto improve the oil-recovery rate. The Area 3

    reserves-life index was estimated at less than

    2 years. Therefore, optimization efforts were

    focused on wells in Areas 1 and 2.

    A study of the pressure drops in the sur-face system determined that increasing the

    size of pipeline at the pad site would

    reduce pressure drops and increase pro-

    duction. However, the most effective meas-

    ure would be to improve the downhole

    artificial-lift system. The system review

    also determined that adequate capacity

    existed at the testing and battery facilities

    to handle increased well production from

    wellbore optimization.

    OPTIMIZATION ATTEMPTS

    A flowing-pressure-gradient survey was

    performed on the most prolific well in thefield in September 1996. Subsequent tub-

    ing-flow-performance analysis could not

    match actual data with theoretical calcula-tions, indicating that the production-string

    design and gas-lift performance were

    not optimized.

    Theoretically, for an efficient gas-lift

    installation with 2.875-in. tubing, fluid pro-duction should have increased from 717 to

    1,500 B/D of liquid (BLPD). This increase

    could be accomplished by replacing several

    gas-lift valves with valves that had differentoperating pressures. A coiled-tubing-de-

    ployed system replaced the three existing

    valves successfully in November 1996. The

    well was placed back on production with a

    minimal increase in fluid production to 850

    PRODUCTION ENHANCEMENT OF

    PROLIFIC, EXTENDED-REACHGAS-LIFT OIL WELLS

    This article is a synopsis of paper SPE

    48935, “Significant Production En-

     hancement of Extended-Reach, Prolific

    Gas-Lift Oil Wells—Case History of 

    Systematic Problem Resolution,” by

    D. Hahn, SPE, D. Yu, SPE, M. Tiss, SPE,

    R. Dunn, SPE, and D. Murphy,

    PanCanadian Resources, prepared for

    the 1998 SPE Annual Technical Con-

    ference and Exhibition, New Orleans, 27–30 September.

    P R O D U C T I O N O P E R A T I O N S

    Fig. 1—Slant-well schematic: true vertical depth (TVD) is 3,380 ft, and measured depth(MD) is 7,200 ft.

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    P R O D U C T I O N O P E R A T I O N S

    • MARCH 1999 63

    BLPD. A subsequent flowing-pressure-gra-

    dient survey in January 1997 still showed

    excessive pressure drop in the tubulars.

    For the next 6 months, significant effortwas expended to obtain a reasonable expla-

    nation for the differences between actual

    and calculated tubing performance. Advice

    was solicited from an international experton gas lift who also was unable to model

    the actual performance with various nodal

    analysis packages. Therefore, it was deter-

    mined that some other unexplained phe-

    nomenon was contributing to the problem.The following production-impairment

    mechanisms were considered.

    • Production/injection measurement

    equipment.

    • Hole in the tubing near surface.• Nonrepresentative flowing-pressure

    gradient caused by production interference

    from flow past the gauges.• Phase separation and stratification of 

    fluids (water, oil, and gas) in the tubing.All the metering was verified and

    deemed to be providing accurate data. A

    hole in the tubing near the surface was

    ruled out because the flowing-pressure gra-dient indicated a definite gradient shift at

    the gas-injection point. Wireline gauge

    rings were run to confirm that no tubular

    restrictions existed. Review of the flowing-

    pressure-gradient results, with and withoutpressure gauges in the tubing (i.e., lubrica-

    tor and sump), demonstrated that the

    gauges were not interfering with produc-

    tion; therefore, the gradients were deemed

    to be accurate.Recent research and experiments on hor-

    izontal- and deviated-well flow characteris-

    tics indicate that phase separation in tubu-

    lars can be an issue because higher-specific-gravity fluids will move at slower velocities

    or even reverse the flow along the bottom

    of the tubular. Because these slant wells are

    a special application of an extended-reach

    deviated well, it was postulated that theeffective flowing diameter of the tubing was

    possibly smaller because of possible reverseflow of the heavier liquid phase on the low

    side of the tubing. This effect would

    increase pressure drops along the tubing.The tubing was replaced with 3.5-in. tubing

    to obtain at least 1,450 BLPD; however,

    only 1,130 BLPD was achieved, indicating

    that the problem was probably of a different

    nature and still not understood.

    EMULSIONS AND DEMULSIFIERS

     While trying to reconcile the underachiev-

    ing gas-lift performance, discussions held

    with the property team determined that theCountess YY crude oil tends to form tight

    emulsions in the surface progressing-cavity

    transfer pumps. The tight emulsions result

    in significant pressure drops in the surfaceflowlines. The pressure-drop/emulsion

    problem was being addressed through the

    continuous injection of demulsifier

    upstream of the transfer pump.

    The design of a typical gas-lift mandrelintroduces the lift gas into the tubing flow

    stream countercurrent to the liquid stream.

    This action can create significant turbu-

    lence in this area and cause significant

    shearing/agitation of the liquid phases.These turbulent conditions could be the

    catalyst that promotes severe emulsification

    of the fluids.

    Tests of emulsion samples taken at thewellhead revealed that they were very vis-

    cous and stable. The viscous emulsified

    flow regime created excessive pressure

    drops within the wellbore that impededproduction. Surrounding wells are alsoprone to emulsions.

    Several weeks after the August 1997

    installation of larger tubing, a demulsifier

    was introduced into the injection-gas

    stream. After 2 days, the well respondedwith a very strong production surge. The

    estimated rate was in excess of 2,830 BLPD.

    The production spike would last for 2 to 3

    hours then revert to its normal rate for 6 to

    7 hours. This cycle repeated itself two tothree times every day. During these high-

    rate surges, the surface piping at the well-

    head vibrated vigorously and operational

    problems were encountered with the sepa-ration and gas-processing equipment. The

    demulsifier was a two-component blend of 

    active ingredients in hydrocarbon carriers.

    The dry lift gas probably absorbed the

    hydrocarbon carrier, causing the resultingthicker demulsifier active ingredient to

    remain at the top of the annulus fluid.

    Project economics dictated the installa-

    tion of a chemical capillary string. The ded-

    icated chemical-injection string allowsintroduction of chemicals where produced

    fluids enter the tubing string, letting activa-tion take place before the fluids reach the

    more turbulent region of lift-gas injection.

    RESULTS

    The initial chemical-injection rate of 5.3

    gal/D was reduced to 4 gal/D after several

    days. The production stabilized at 3,000BLPD. High wellhead pressures were caused

    by surface piping restrictions that were recti-

    fied in May 1998. A flowing-gradient survey

    was run after the tubulars were upgradedand demulsifier was being injected through

    the capillary string. The gradient surveydemonstrated excellent agreement between

    measured pressures and pressures calculated

    with the Hagedorn-Brown correlation.

    Because the tight produced emulsions inthe tubulars impaired gas-lift performance,

    a second well was upgraded in a similar

    manner. Production increased from 380 to

    1,775 BLPD, an incremental increase of 560

    BOPD. The current rate is in close agree-ment with the theoretical predictions.

    Subsequent to the introduction of this

    chemical, no evidence of paraffin deposi-

    tion within the tubulars has been seen.Dewaxing-related operating costs have

    been reduced, and flow efficiencies

    improved, probably because of increased

    flowing temperatures. Also, with the

    downhole injection of demulsifier, the useof the chemical for surface treatment at

    the testing/transfer facility has been

    reduced significantly.

    Since July 1997, the oil-production ratesfrom the Countess YY pool increased 1,475B/D, from 1,825 to 3,300 B/D (even higher

    than the previous peak rate of 3,000 B/D in

    early 1994 shortly after the waterflood was

    initiated). The perseverance in resolvingthe technical issues surrounding the poor

    gas-lift performance of these wells has

    improved cash flow and profitability of this

    pool significantly.

    SYSTEMATIC PROBLEM-

    RESOLUTION CYCLE

    The resolution of inadequate well-produc-tion performance occurred after several

    iterations that followed a modified

    Shewhart cycle. The four steps of this cycle

    can be summarized as follows.

    1. Plan: diagnose the problem, collectdata, determine changes, and develop an

    action plan.

    2. Do: execute the action plan to carry

    out change.

    3. Check: observe the results.4. Act: analyze the results. What was

    learned? Do side effects or benefits still

    exist? Was the plan successful? Repeat

    cycle if unsatisfactory.During the entire process of arriving at

    the most satisfactory solution for the issue

    of obtaining production rates near the the-

    oretical predictions, the multidisciplinary

    team followed the systematic pattern forcontinuous improvement. This cycle was

    repeated at least four times before the best

    solution emerged.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the

     synopsis has been taken has not been peer reviewed.

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    64 MARCH 1999 •

    Meters for measuring multiphase flow are

    unique tools that allow measurement of 

    produced fluids (oil, water, and gas) with-

    out separation into individual phases. Twodistinct and fundamental approaches to

    multiphase-flow measurement exist. The

    first includes no fluid separation, and the

    second uses partial (hybrid) measurement.

    No single multiphase-flow-measurement-system design or technology resolves all

    multiphase-flow-measurement issues sat-isfactorily. Each approach has benefits as

    well as shortcomings. Even with these lim-itations, worldwide use has increased.

    Approximately 50 multiphase-flow

    meters were in service in 1995; this num-

    ber increased to approximately 150 in

    1997. Subsea application was the majorreason for the original growth of the tech-

    nology and is expected to be the dominant

    driver in the future.

    Most commercial multiphase-flow-meas-

    urement systems have no level- or pressure-control equipment to maintain but do

    include process-variable transmitters,

    which generally are off the shelf with stan-

    dard calibration procedures. However, mostsystems require some form of electrical

    power and, in some cases, a controlled

    environment (such as a control room) for a

    flow computer. Because new electronic sys-

    tems have been problematical wheninstalled in the field, Conoco was com-

    pelled to test at the field level.

    MPFM 1900VI DEVELOPMENT

    The field-level performance-evaluation test

    begun in late 1997 was the final step of adevelopment program started in 1992. A joint-industry-project (JIP) agreement

    between Conoco Inc., Norske Conoco A/S,

    and Fluenta A/S was reached in 1991 on a

    program that spanned 2 years and consist-

    ed of four development activities. The workresulted in Fluenta’s MPFM 1900VI multi-

    phase-flow meter.

    Previous testing of water-cut meters at

    Conoco’s Grand Isle shore base in 1988indicated that “live” fluids (at bubblepoint)

    affected the accuracy performance of many

    instruments, causing them not to meet themanufacturers’ accuracy specifications.

    This bubblepoint-fluid condition occurswhen pressure drops below the last separa-

    tion pressure, which occurs as fluid flows

    through pipes and fittings.

    Conoco’s multiphase-flow test and vali-

    dation flow loop outside Lafayette,Louisiana, was commissioned in March

    1993. Its original objective was to validate

    meter performance with produced fluids by

    use of multiphase (liquid/liquid, liquid/gas,and liquid/liquid/gas), clamp-on ultrasonic,

    water-cut, and any other technology with

    potential operational and economic

    improvements.

    Testing of Fluenta’s MPFM 900V, theforerunner of the MPFM 1900VI, began in

    April 1993. The project was to end by

     January 1994 with the tests of the MPFM

    1900VI. Because of unplanned events,

    however, the flow-loop-test phase did notend until February 1997. The JIP test pro-

    gram was planned to be completed after the

    conclusion of field-level testing in the U.S.

    Gulf of Mexico.

    USE OF MULTIPHASE-FLOW-

    MEASUREMENT TECHNOLOGY 

    The economic incentive to use multiphase-flow technology is derived from the initial

    savings of weight and space on convention-

    al platforms, providing instantaneous flow-

    rate information, reduced maintenance,and more efficient detection of problems

    associated with declining production. In a

    subsea application, multiphase-flow tech-

    nology becomes an enabling technology,

    allowing measurements in an environmentwhere separators are unproved.

    A business case was developed for thisfinal field test that assumed that average

    daily production volumes from the plat-

    form would be increased by 1 to 2%. It was

    further assumed that this increase in pro-duction would come about because the

    meter would allow production adjustments

    with faster feedback from measurements,

    decreasing the apparent decline rate; pro-

    duction tests could be performed moreoften and for shorter periods of time; and

    response to unplanned production-rate

    changes could be faster.

    METER DEVELOPMENT

    The meter measures oil, gas, and water flowrates without physical separation of the well

    stream. The nonintrusive, real-time, full-

    bore instrument requires no bypass line and

    no invasive mixing device. The meter deter-

    mines fluid slip automatically and calcu-lates volume flow rates at actual and cus-

    tomer-supplied standard conditions. Fluid

    slip is the relative velocity between liquid

    and gas phases in a multiphase system

    where gas tends to flow faster than liquid.The measurement system includes a

    capacitance sensor, an inductive sensor, a

    gamma densitometer, a venturi meter, and a

    system computer. The capacitance sensor isused to measure the permittivity of the

    mixture and the gas velocity in oil-continu-

    ous multiphase-flow situations. If the flow

    becomes water continuous, the system flow

    computer automatically selects the induc-tive-sensor signals to calculate the conduc-

    tivity and gas velocity of the mixture. The

    gamma densitometer is used to measure the

    density of the flow stream. The flow com-

    puter performs the analysis on the data andthe data are brought safely to the computer

    by cables through safety barriers.

    Principle of Operation. Measurement of 

    the flow is divided into two parts, fluid frac-

    tions and velocities. Oil, water, and gas flow

    rates are calculated on the basis of the mea-sured fractions and velocities. The permit-

    tivity and density are different for each of 

    the three components of an oil/gas/water

    mixture. If these permittivities and densitiesare known and the total permittivity and

    density of the mixture are measured accu-rately, the fractions of each of the three com-

    METERING MULTIPHASE FLOW

    IN THE GULF OF MEXICO

    This article is a synopsis of paper SPE

    49118, “Application of the First

     Multiphase-Flow Meter in the Gulf of 

     Mexico,” by Edward G. Stokes, SPE,

    Conoco Inc.; Dennis T. Perry, PetroTraces

    Inc.;  Marshall H. Mitchell, Conoco Inc.;

    and Martin Halvorsen, Fluenta A/S, pre-

     pared for the 1998 Annual Technical

    Conference and Exhibition, New Orleans, 27–30 September.

    P R O D U C T I O N O P E R A T I O N S

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    66 MARCH 1999 •

    P R O D U C T I O N O P E R A T I O N S

    ponents can be determined. For water-con-

    tinuous mixtures, the inductive sensor is

    used to calculate the fractions. The principle

    is basically the same, except that conductiv-ity (not permittivity) is being measured.

    Studies have shown that generating

    gas/liquid flowing conditions without slip

    is virtually impossible. Even if no-slip con-ditions could be generated artificially, slip

    would reoccur a very short distance down-

    stream of the mixing device (typically 5 to

    10 diameters). The strategy for this system

    was to find and develop mathematical mod-els that give dependable velocity measure-

    ments under all slip conditions.

    This system determines the velocities of 

    the large and small gas bubbles and the liq-

    uid. The capacitance and inductive sensorscontain a number of electrode configura-

    tions that are used to measure the velocities

    of the large gas bubbles through crosscorre-lation. The velocity of the small gas bubbles

    and the liquid is found from the differentialpressure across the venturi meter. When

    the two velocity components are deter-

    mined, they are combined with information

    from the fraction measurements to calcu-late the individual flow rates of oil, gas,

    and water.

    FIELD TESTING

    Initial plans called for testing of all wells for

    24 hours at a set gas-lift rate to establish a

    base condition. This test would be followedby another 24-hour test at the same operat-

    ing conditions of choke size, pressure, and

    gas-lift rate to evaluate repeatability. After

    the first two series of long-duration tests,

    test duration was determined by field-oper-ations personnel. Adjustments also were

    made to observe, in real time, each well’s

    response to conditional changes (i.e.,

    choke diameter, gas-lift rate, or process-

    system settings).

    Meter Installation. The meter system was

    installed with upward vertical flow.

    Physical installation included a drip pan tocontain spills, block valves to allow work tobe done on the meter without depressuring

    the whole platform, and manual sample

    ports at the meter inlet. The multiphase-

    flow computer was installed in the opera-

    tor’s doghouse on the well-bay deck.

    Safety Issue (Gamma Densitometer).

    The gamma densitometer used at the test

    site was rented from ICI Tracerco and used

    cesium-137 as the gamma-emitting isotope.

    The source-energy rating is 24 mCi, which

    requires special handling and operatingprocedures and personnel training.

    FIELD OB SERVATIONS

    Separator-Discharge Sampling. The sep-

    arator-sediment/-water sampler was not

    used because a representative sample couldnot be taken during the dump cycle.

    Because of the nature of on/off fluid flow, a

    dump cycle would start with mostly water

    and end with mostly oil. Although thedump rate was reasonably consistent, sam-

    pling the dump cycle yielded nonrepeat-

    able results. Instead, liquid samples were

    taken manually at the inlet to the multi-

    phase-flow meter.

    Fluid Cloud-Point Problem. One well

    was found to flow at close to its cloud

    point. After several series of tests where

    various wells were flowed through the

    metering system, the indicated water cutfor all wells became consistently lower

    than the manual water-cut samples.Inspection and cleaning of the meter cor-

    rected the problem and returned the meter

    performance. The capacitance unit had aparaffin deposit covering the liner surface,

    which had to be cleaned to enable prop-

    er operation.

    Safety. To use a gamma densitometer in the

    field, a licensing procedure had to be devel-

    oped that included the following.

    1. Permission from regulatory agencies

    to proceed with the usage.

    2. Removal from previous location.3. Transportation to field.

    4. Installation and leak check.

    5. Field training and maintenance.

    6. Contingency planning and documen-

    tation of Items 1 through 5.7. Roll-up plan for removal of radioactive

    source after use.

    Observations. Multiphase-flow metersproved to be more robust than anticipated,with no mechanical failures during the test

    period. It was very difficult to acquire all

    the required data consistently and accurate-

    ly over different shifts and rotating person-nel. However, less than 10% of the data waseliminated for poor quality. The only main-

    tenance problems were with software early

    in the program and paraffin buildup when

    testing close to the fluid cloud point.

    The field performance of the meteringsystem appeared to be similar to the flow-

    loop performance. Measurement repeata-

    bility was demonstrated, except for the

    consistent accumulation of paraffin found

    throughout the test period for one well.The piping and electrical installations were

    simple and straightforward, making thesystem easy to move at low cost.

    Testing indicated that the duration of the

    well test does not affect the relative perfor-mance of the meter compared with the sep-

    arator. Projected 24-hour production rates

    from the separator and multiphase-flow-

    meter system were affected in some wells

    by the length of the well test. Many wells do

    not flow at the average daily rate constant-ly; instead, they appear to cycle.

    At some point in each well, the multi-

    phase-flow meter was subjected to instan-

    taneous flow conditions below the meter’sspecified liquid-rate minimum. This was

    caused by surging, where a liquid slug is

    followed by an extremely high gas fraction

    with very low liquid rates. This sluggingoccurred at regular intervals. The meter

    was useful in establishing optimum gas-lift

    rates through the relatively instantaneous

    nature of its data calculation and display.

    Issues for Future Use. Future use of any

    new-technology multiphase-flow-measure-

    ment equipment depends on the following.

    • The absolute accuracy of multiphase-

    flow-measurement systems must improve

    to a maximum of ±5% at all conditions of 

    flow for gas, oil, and water.

    • How the conflict that arises (becausethe method of determining a separator’s

    hydraulic efficiency in the field often is not

    specified) when comparing typical perfor-

    mance between a separator and a new-tech-

    nology multiphase-flow meter is resolved .• How multiphase-flow-measurement

    accuracy is proved after repair, recalibra-

    tion, or system change (i.e., level or pres-

    sure).

    • How one determines whether a meas-urement-system performance change might

    have occurred during use (such as the wax-

    buildup problem experienced during the

    field test).• The U.S. Minerals Management Service

    (MMS) custody-transfer requirements are

    2% for sales of gas and 0.25% for sales of 

    liquids. Currently, multiphase-flow-meas-

    urement technology cannot meet thesestringent requirements. The question is

    whether multiphase-flow technology can

    be improved sufficiently to close this gap

    and be approved for fiscal measurement by

    the MMS.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the

     synopsis has been taken has not been peer reviewed.

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    • MARCH 1999 67

    The main objectives of production logging

    are to diagnose well-production problems

    (such as inflow rates and entries of unwant-

    ed fluids), supply information for reservoirmodeling, and provide data to optimize the

    productivity of future and existing wells.

    Determining the inflow profile of oil can

    help plan a drilling strategy, formulate

    cleanup methods for current and futurewells, determine drainage patterns, and

    allocate production to sidetracks. Deter-mining the water-entry locations and posi-

    tion of the water cone can provide a betterunderstanding of the reservoir water-trans-

    port mechanisms and supply data for

    potential workovers. Ultimately, use of the

    results should improve the productivity

    and long-term recovery from the field.Most of this discussion refers to

    oil/water systems, with occasional refer-

    ences to gas/liquid systems. Many of the

    oil-/water-system results are applicable to

    gas/liquid systems. In a horizontal well,whether it is a barefoot completion or com-

    pleted with a cemented casing or slotted

    liner, oil/water flow tends to be segregated

    by gravitational forces.Along different sections of the wellbore,

    the heavy- and light-fluid phases segregate

    according to the following regimes: strati-

    fied with a flat interface; stratified with a

    wavy interface; stratified with a bubblyinterface; light phase slugging over the

    heavy phase; or one phase existing purely as

    bubbles in the other phase. Except for very

    heavy oils, stratified flow is normal when

    the holdup is significant (>20%) for both oil

    and water and can occur for liquid flowrates ranging from 0 to more than 12,000

    B/D. Whatever the density contrast betweenthe heavy and light phase, stratified flow is

    more likely for flow in sections of wellbore

    with deviations greater than 90° (i.e., down-

    hill flow). Stratified flow with a bubbly

    interface can occur with low water holdupsand is more likely as deviation decreases

    below 90°. Slugging of the light phase can

    occur at deviations of less than 90° and is

    more common in gas/liquid flow. Flow

    where one fluid phase is mixed as bubblesin the continuous phase tends to occur

    more often if the heavy and light phases

    have similar densities or if one fluid phase

    enters through a jet into the wellbore.Problems encountered in measuring

    holdup and velocities in multiphase flow in

    horizontal wells include the following.

    • Sumps and traps change the cross-sec-

    tional area open to flow.• Segregated flow where different fluids

    have different velocities can greatly compli-

    cate spinner readings.

    • Slight slope deviations from horizontal

    can cause significant changes in holdupand fluid velocities.

    • Deviations of much less than 90° can

    cause backflow and circulation.

    • Sensors that relate the density of a col-

    umn of fluid to the difference in pressuremeasured at the top and bottom of the col-

    umn cannot work in horizontal wellbores.

    • A nuclear fluid-density meter is unde-

    sirable because it is environmentally haz-ardous and provides inaccurate measure-

    ments (particularly in heavy-oil/water sys-

    tems of the Northwest shelf of Australia).

    • Slotted liners create complications foraccurate calculation of the total flow ratebecause of the uncertainty introduced by

    the annulus between the liner and the

    open hole (e.g., annular flow, changing

    hole diameter, or variable eccentering of 

    the liner).• The spinner behaves insensitively at

    low flow rates, which typically occur

    toward the toe of the well where the inflow

    contributions are often of strong interest.Because of segregated flow, interpretation

    techniques for vertical wells often are not

    applicable to horizontal wells. Moreover,existing correlations for horizontal and

    deviated oil/water flow do not deal with the

    effects of slight deviations. Therefore, a newtool string consisting of traditional and

    recently developed sensors has been tested.

    The possible existence of gas traps and

    water sumps causes another general diffi-

    culty when trying to understand flowbehavior in horizontal wells. Given the

    observed production of these fluids at the

    surface, it would be dangerous to construe

    the downhole flow regime of water and gas.For example, when only oil is produced atthe surface, it generally would be incorrect

    to assume that single-phase oil flow

    exists downhole.

    INTEGRATED PRODUCTION-

    LOGGING TOOL

    The tool string shown in Fig. 1 is astripped-down version of one designed to

    deal with three-phase flow and is generally

    adequate for flow that is mainly oil/water.

    The tool string contains multiple sensors

    that measure the same quantity. For exam-ple, the locations of water inflow into a

    mainly oil-filled wellbore could be inferred

    from an interpretation of data from the

    spinner plus the fluid holdups measured

    by Schlumberger’s Reservoir SaturationTool (RST) and FlowView Plus tool

    (FVPT) or from the flow image and bubble

    counts from the FVPT. All data from all

    sources must be considered when perform-

    ing the interpretation.

    CONVEYANCE

    The example wells were logged with the aid

    of a tractor run above the tool string. It wasused to push the string toward the toe of the well. The logging was done while the

    tool string was pulled out of the wellbore

    by wireline.

    EXAMPLES

    Three wells were logged in the Wandoofield, 37 miles offshore Australia on the

    Northwest shelf. The field contains a thin

    oil column (72 ft) sandwiched between a

    small overlying gas cap and a strong aquifer.The oil gravity is 19°API, with a reservoir

    viscosity greater than 15 cp. Reservoir per-meability ranges from 500 to 10,000 md.

    NEW PRODUCTION-LOGGING

    TECHNOLOGY FOR HORIZONTAL WELLS

    This article is a synopsis of paper SPE

     50178, “Application of New-Generation

    Technology to Horizontal-Well Produc-

    tion Logging—Examples From the

    North West Shelf of Australia,” by  A.

    Carnegie, SPE, Schlumberger, and N.

    Roberts, SPE, and I. Clyne,  Mobil E&P

     Australia Pty. Ltd., originally presented

    at the 1998 SPE Asia Pacific Oil & Gas

    Conference and Exhibition, Perth, Australia, 12–14 October.

    P R O D U C T I O N O P E R A T I O N S

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    P R O D U C T I O N O P E R A T I O N S

    The field was developed with horizontalwells, 15 oil producers and one gas injector.

    The average length of openhole section forthe oil producers is 3,281 ft.

    Understanding of water influx into the

    horizontal wells is crucial to the long-termrecovery from the field. Early breakthrough

    of water was expected because of the thin

    oil column, unfavorable mobility ratio, and

    strong bottomwater drive. Results from a

    previous production-logging campaignindicated that water influx occurred at the

    heel of the well, the location of maximum

    drawdown. Recent production logs suggest

    that this assumption was applicable onlyfor wells intersecting sands of uniform per-

    meability or for wells with higher-perme-

    ability sands at the heel.

    Example 1.  Well WB1a intersects higher-permeability sands at the toe of the well.

    These sands are thought to have incurred

    large fluid losses during drilling operations,

    which may have damaged the formation.

    Test objectives were to determine the flow

    contribution of the sidetrack, the wellinflow profile, and water-entry locations.

    The tool string consisted of a directional

    full-bore spinner; an FVPT; and sensors for

    pressure, temperature, and acceleration. AnRST analysis was unnecessary because thedownhole flow regime was known to be

    essentially two phase (oil and water). The

    holdup in an oil/water flow regime can be

    determined by the FVPT reliably.

    The shut-in log data show a strong cor-relation between parameters: the FVPT

    bubble counts and water-holdup-analysis

    results and the low sections of the well tra-

     jectory. The spinner indicated that cross-flow was insignificant or nonexistent.

    Data from the FVPT corroborate the spin-

    ner with respect to water at low points inthe wellbore. But only the spinner can be

    used to suggest the existence of gas pock-

    ets at high sections of the wellbore. Water

    sumps and gas traps typically are found inshut-in wells with little or no crossflow.During the flowing pass, the full-bore

    directional spinner indicated that inflow

    to the wellbore was relatively uniform,

    probably indicating that the sidetrack was

    not contributing significantly.The holdup analysis shows that, during

    flowing conditions, the sumps had been

    dispersed and smeared except for one at

    5,676 ft, where the flow from the toe wasprobably too low to affect it. The bubble-

    map log track, which was blank for the

    shut-in pass, shows an abundance of bub-

    bles under flowing conditions. These bub-

    bles are probably water because they usual-ly occur on the lower side of the liner.

    Example 2. The next well logged was

     Well WB4a, which intersects higher-per-

    meability sands at the toe of the well.

    These sands constitute 9% of the total

    openhole section of the well. The initial

    logging passes were shut-in spinner-cali-bration passes. When the surface flow

    rates were stable at 3,490 BOPD and 7,265

    BWPD, logging was performed.

    Near the toe of the well, the fluids werestratified vertically (water underneath,hydrocarbon on top) and the bubble count

    was low (compared with the heel). Moving

    up the hole, the temperature, bubble count,

    and water holdup increased dramatically

    and the flow became more mixed. The bub-bles between 6,300 and 6,102 ft were likely

    water because the water holdup increased

    dramatically (from 6,300 to 6,234 ft). This

    influx location coincides with the pointwhere the well intersects the higher-perme-

    ability sands at the toe of the well.

    In the segment of wellbore between6,102 to 3,281 ft, the water holdup

    decreased. The flow became bubbly, and

    the bubbles probably were oil because most

    occurred on the high side of the liner. Water and hydrocarbon also became pro-gressively more mixed (i.e., dispersed).

    From 6,102 to 3,281 ft, all the influx was

    oil. On the basis of the spinner response,

    the oil productivity was uniform.

    Example 3. The third horizontal well sur-

    veyed was Well WB9, which wasgeosteered under an existing producer and

    intercepted a water cone at 4,921 ft. The

    tool string consisted of an FVPT and an

    RST. The FVPT provided the wellbore

    water-/hydrocarbon-holdup data. Thesedata were necessary to interpret the forma-

    tion measurements made by the RST. The

    RST was used to determine the oil, water,

    and gas saturations in the formation and to

    provide wellbore holdup data. The resultsindicated that the residual-oil saturation in

    the zone from 4,970 to 5,102 ft was

    approximately 27%, compared with 19%

    from core analysis.The data from the RST tool, acquired

    while in dual-burst pulsed-neutron mode,

    clearly show character that is not an artifact

    of the wellbore conditions and, therefore,

    should be a formation response. Thisresponse implies that the RST may be used

    for time-lapse monitoring. The wellbore

    holdup determination from the RST agrees

    well with that from the FVPT. These results

    are being used by Mobil for reservoir mod-eling and for time-lapse monitoring.

    Fig. 1—Tool string used for the Australian Northwest shelf examples (conveyed by tractor—not shown).

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the

     synopsis has been taken has not been peer reviewed.

    Combinable

    production-logging toolto obtainpressure andtemperature.

    The RST used to

    determine waterflow; three-phaseholdup; formationoil, water, and gassaturations; andgamma ray count.

    Full-bore directionalspinner used todetermine totalflow rate.FVPT

    Flowview tool Flowview tool

    Combined tools positioned at a 45° offset and usedto determine holdup, flow image, bubble map, andbubble velocity.

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    70 MARCH 1999 •

     Water management is important in the pro-

    duction of hydrocarbons, especially when

    water volumes steadily increase as fields

    age. Novel approaches that can reduce thewater volume downhole may supplement

    the traditional approach to oil/water separa-

    tion at the surface. Taking produced water

    out of the well stream downhole increases

    production-tubing and process-facilitycapacity for oil and gas. Downhole oil/water

    separation (DOWS) can reduce the need toupgrade water-treating facilities.

    Downhole separation offers an alterna-tive to debottleneck constrained water-han-

    dling facilities with potentially positive side

    effects, such as more favorable conditions

    for separating oil from water, increased pro-

    ductivity as a result of better wellhydraulics, reduced discharges of oily

    water, and maintenance of reservoir pres-

    sure. Reducing water at the source also

    diminishes the need for water treatment

    and for prevention of corrosion, scale, andhydrates. When wells are already pumped

    or when produced water is already reinject-

    ed, downhole separation will be beneficial,

    particularly in wells where water shutoff has proved ineffective.

    New concepts for DOWS have been

    developed under a joint-industry project

    run by the Centre for Engineering Research

    (Canada). The technical feasibility of com-pleting wells with hydrocyclones and

    downhole pumps to achieve in-well pro-

    duction, separation, and reinjection was

    demonstrated. The first successful installa-

    tion outside North America became opera-

    tional in Germany in 1997.

    CANDIDATE WELLS

    Candidate wells have a relatively low pro-

    duction rate (95%). Wells with a risk of sand pro-

    duction or emulsification must be avoided.

    The Eldingen field, east of Hannover,Germany, has produced from a shaly sand-

    stone reservoir since the 1950’s and meets

    the screening criteria. Well Eldingen-58

    produces light oil from three consolidated-

    sandstone intervals that are in pressurecommunication. The reservoir pressure is

    approximately 72 bar at a 1460-m perfora-tion depth. Production has been lifted by a

    beam pump at 80 m3 /d with 97 to 98%

    water cut. In preparation of the DOWSinstallation, a packer was set to isolate the

    top zone from the two lower zones. The top

    zone was to be the producing interval and

    the lower zones the injection interval.

    EQUIPMENT DESIGN

    The downhole separator was designed in

    consultation with the equipment supplier

    on the basis of reservoir and well data. TheDOWS for Well Eldingen-58 includes one

    hydrocyclone and two electrical-sub-

    mersible pumps (ESP’s). Fig. 1 depicts the

    downhole equipment and flow paths.

    The high-water-cut oil flows from theproduction perforations upward to the top

    of the motor shroud. The bottom of theshroud is coupled to the pump housing by

    a fluid-tight seal, forcing all fluids over the

    top of the shroud and downward along themotor into the pump. From the pump

    intake, all fluids are pumped downward by

    the total-flow pump (an upside-down ESP

    with a thrust bearing at the top and dis-charge at the bottom) into the hydrocy-

    clone where the bulk of the water is sepa-

    rated from the oil. The underflow of the

    hydrocyclone produces water clean enough

    for injection into the disposal zone. Theoverflow, oil with the remainder of the

    water, flows through bypass tubes into the

    concentrate pump for production to the

    surface. These three 20-m-long, 0.9525-

    cm-diameter tubes that bypass the lowerpump and motor are sized so that erosion

    and pressure drop are minimal.

    A common motor drives both pumps.

    This motor has protectors at top and bot-

    tom, unlike a normal ESP. The motor ispowered from the variable-speed drive at

    the surface through a flat cable, which is

    strapped to the tubing with metal bands

    and cross-coupling protectors. With a vari-

    able-speed drive and an adjustable surfacechoke, the system can cover the expected

    variability in injectivity and productivity.

    The pump design depends on the flows

    and pressures required to lift the oil-richstream compared with those needed to

    reinject the water. The push-through sys-

    tem used in Well Eldingen-58 is most effi-

    cient for dealing with the low reservoir

    pressure in Eldingen. This concept alsoavoids any breakout of gas in the hydrocy-

    clone. If the reservoir pressure is sufficient-

    ly high, a concentrate pump is not needed.

    Alternatively, the well stream may be sepa-rated before being pumped; this so-called

    DOWNHOLE SEPARATOR PRODUCES

    LESS WATER AND MORE OIL

    This article is a synopsis of paper SPE

     50617, “Downhole Separator Produces

    Less Water and More Oil,” by P.H.J.

    Verbeek and R.G. Smeenk  , Shell Intl. E&P,

    and D. Jacobs, BEB Erdgas und Erdöl,

    originally presented at the 1998 SPE

    European Petroleum Conference, TheHague, The Netherlands, 20–22 October.

    P R O D U C T I O N O P E R A T I O N S

    Fig. 1—Downhole equipment lineup of  well completion and flow paths forEldingen-58.

    Tubing to surface

    Concentrate pump

    Motor upper protector

    Motor lower protector

    Pump intake

    Total-flow pump

    Bypass tubes

    Hydrocyclone

    Injection pressure sub

    Separation packer andlocator seal assembly

    Injectionzone

    Productionzone

    Motorshroud

    Motor

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    P R O D U C T I O N O P E R A T I O N S

    pull-through concept can be applied pro-

    vided the bubblepoint pressure is high

    enough to prevent gas breakout in the

    hydrocyclone. In some crude oils, the latterconcept would avoid emulsions and poor

    injection-water quality as observed in earli-

    er DOWS trials with heavy oil.

    Solids carried by the separated water arethe biggest concern for sustained injectivi-

    ty. However, the consolidated reservoir in

    Eldingen has little sand production. For

    efficient oil/water separation, the split

    between overflow and underflow of thehydrocyclone can be controlled by chokes.

    The oil-in-water content in the underflow

    of the hydrocyclone should be 100 to

    300 ppm. To ensure this water quality into

    the disposal zone, a rule of thumb forDOWS is to keep the surface water cut

    slightly higher than 50%. The separation

    efficiency depends largely on characteristicsof the oil/water mixture, in particular oil

    droplet size. Knowledge of the droplet-sizedistribution in oil-in-water emulsions

    downhole could enable better separation.

    FIELD PERFORMANCE

    Recompleting the well has increased net oil

    production by 300%, while net water pro-

    duction to surface has decreased by 64%. In

    the first year of operation, reinjection of 

    water, separated downhole, did not damage

    matrix permeability; however, a water-cutincrease was observed in the project area.

    TECHNOLOGY OUTLOOK 

     Well re-entry has not been required for cor-rective action on downhole equipment. Thewater is injected under matrix-flow condi-

    tions, and no sign of permeability damage

    has been observed. Adjacent wells have

    experienced an increase in fluid level and

    water cut. These trends result primarilyfrom the influence of DOWS because these

    wells produce from the lower zones into

    which Well Eldingen-58 is injecting.

    Despite favorable performance, the eco-nomics of DOWS is still relatively poor.

    Assuming U.S. $15/bbl and a production-rate

    increase of 30 B/D, payback time is approxi-mately 1 year. Important factors include oil

    price, process-facility capacity, and an increasein tubing oil-flow capacity. Phasing well con-

    versions in accord with increasing water rates

    also would limit exposure of large up-front

    investments. The concept, developed origi-

    nally for debottlenecking production facili-ties, is being upgraded with a more efficient

    downhole separator aimed at reducing the

    infrastructure and facilities for offshore fields.

    CONCLUSIONS

    • Industry still needs to prove that down-

    hole separation is a reliable, cost-effective

    means to increase oil production from

    capacity-constrained facilities, potentiallylengthening the life of oil fields.

    • The downhole-separation concept, devel-

    oped originally for debottlenecking onshore

    facilities, has the potential to reduce the infra-

    structure and facilities of offshore oil fields.• Evidence exists that water, separated

    downhole, can be injected under matrix-

    flow conditions, which may lead to signifi-

    cant power savings in water-injection sys-

    tems if sustained.• Water-cut development in the Eldingen

    field indicates that DOWS should be

    applied in reservoir configurations withflow barriers between producing and injec-

    tion intervals.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the

     synopsis has been taken has not been

     peer reviewed.

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    72 MARCH 1999 •

    Fig. 1 shows a subsea-satellite field on theNorwegian continental shelf, 200 km

    northwest of Bergen, connected through a

    9-in. production line to a concrete gravity-

    based production platform. Production,

    which started in 1994, is from four pro-duction templates, and water injection, for

    pressure support, is through two injection

    templates. Oil production currently is

    25 000 m3 /d. Recoverable reserves are esti-

    mated to be 55×106 m3 of oil from Brentgroup sandstone.

    Squeeze chemicals can be injected intothe wells through a 21 / 2-in. methanol line

    from the platform, 16 km from the farthest

    production template. The individual wellsare completed differently, but most are ver-

    tical or highly deviated, with 51 / 2-in. tub-

    ing. Placement of chemicals is difficult

    without the use of coiled tubing and an

    intervention vessel, which is expensive.The most attractive solution is to bullhead

    the treatment through the methanol line

    and into the wells.

    THE NEED

     When a scale-inhibitor squeeze treatment

    with a traditional water-based product is

    needed, several operational constraints

    must be considered. These constraints,

    caused by the long distance between theplatform and the templates and the large

    volume of fluid that has to be pumped and

    backproduced, include the following.

    • High friction and low pump rates will

    be experienced because of the high reser-voir pressure and long distance.

    • Poor placement can result because of 

    the low injection rates through the 21 / 2-in.

    methanol line into 51 / 2-in. tubing.• Each production template is connected

    to four producers. Because a separate test

    line does not exist, the other wells at thetemplate must be shut in after a squeeze

    treatment to enable the squeezed well to

    produce through the 9-in. production line.

    If use of an oil-soluble scale inhibitor

    (OSSI) is possible, the squeezed well can bebackproduced without shutting in the

    other wells at the same template. Also,

    fewer relative permeability effects for dry

    wells means that a squeeze treatment canbe performed before water breakthrough

    without risking deferred production

    because of a prolonged cleanup period. Anextended squeeze life may be possible

    because the OSSI can be placed deeper intothe formation without causing water block,

    as often observed with water-based prod-

    ucts. Better placement, with a higher

    squeeze rate into the formation, may be

    possible because of a lack of pressure dropcaused by changes in saturation.

    OSSI

    OSSI’s are better described as oil-miscible

    scale inhibitors. They were developed ini-

    tially for gas-lift applications and some-times applied as combined scale/corrosion

    inhibitors. Early OSSI’s often contained

    multiple components and mutual solvents

    to hold the package together. In special

    applications, undesirable side effects (suchas behaving as a surfactant) limited the

    flexibility of component selection. New

    OSSI’s do not contain a mutual solvent and

    will dissolve in most hydrocarbons at infi-

    nite ratios.

    HYDROCARBON CARRIER 

    As part of the test program, the authors

    examined different carrier fluids (hydrocar-bon for the pill) that might be available inthe field (e.g., diesel, kerosene, crude,

    paraffin, and xylene). While xylene is theleast likely candidate, its inclusion provides

    direct comparison with the others because

    it often is regarded as the best hydrocarbon

    solvent and is used in many oil-treating

    chemicals. The choice of carrier fluiddepends on costs, handling, availability,

    and its effect on the OSSI. The last point is

    critical because the hydrolysis and parti-

    tioning kinetics of the OSSI, when it finallycomes into contact with the in-situ water

    phase, control the success of the squeeze

    treatment in the field. Also, the selectedhydrocarbon carrier must demonstrate full

    compatibility with the OSSI at differentoperating temperatures (i.e., platform,

    seabed, and downhole).

    In the tests, 10% OSSI solutions were

    made up in crude, kerosene, diesel, paraf-

    fin, and xylene. The solutions were mixed5:1 with formation water to prepare test

    samples. The samples were shaken briefly

    and left in an oven overnight at 80°C. The

    aqueous and the oil layers from each sam-ple were separated and analyzed.

    None of the solvent carriers appeared to

    have a major influence on the mass-transfer

    process of the OSSI. On contact with water,

    most of the OSSI molecules transferredfrom the oil phase into the aqueous phase

    through a combined hydrolysis and parti-

    tioning process. The level of transfer was

    extremely high, with little (

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    74 MARCH 1999 •

    P R O D U C T I O N O P E R A T I O N S

    mild scaling-regime change from CO3 to

    SO4 scale when seawater breaks through.

    After transferring into the water phase, the

    OSSI molecules must demonstrate ade-quate inhibition efficiency. Performance

    tests were carried out by use of a conven-

    tional tube-blocking-test apparatus to

    determine the minimum inhibition con-centration (MIC).

    Precolumn Test. A second tube-blocking-

    test procedure uses a precolumn sandpack

    inserted into one of the water flowlines

    placed upstream of the test coil. The col-umn simulated a squeeze treatment in the

    sandpack before the test. The arrangement

    is suitable for screening and ranking differ-

    ent scale inhibitors for squeeze treatment

    before the more expensive and time-con-suming core tests. If the effluent samples

    can be preserved and stabilized, such anarrangement can provide simultaneous,

    inexpensive comparisons of inhibition effi-cacy and retention characteristics of the

    scale-inhibitor chemicals.

    This apparatus possibly can be expanded

    so that a reservoir-conditioned-core con-

    tainer is coupled with a standard tube-blocking-test apparatus. By monitoring the

    pressure drop, the level of scale-inhibitor

    residuals, and the scaling ions in the efflu-

    ents, a more representative MIC level and

    squeeze life might be determined forfield applications.

    Once the OSSI molecules hydrolyzed

    and partitioned in the connate water, they

    migrated toward the sand surface, wherethe adsorption process took place. Their

    return is not affected by the passage of 

    hydrocarbon but follows a desorption pro-

    file similar to that of a water-based

    scale inhibitor.Poorer performance with the water-based

    scale inhibitor seems contradictory at first.

    However, after reviewing other data gener-

    ated during this study, it became clearer and

    is explained by the unique mechanism of 

    “enhanced partitioning.” When injecting awater-based scale inhibitor, the best out-

    come is complete replacement of the con-

    nate water by the injected squeeze pill. The

    maximum concentration gradient that candrive the adsorption process is equal to the

    pill concentration. However, for the OSSI,

    the maximum concentration that can be

    attained by the connate water is governedby the mass-transfer process between the

    oil and water phases.

    During the course of this study, it was

    observed that the equilibrium concentra-

    tion in the aqueous phase can be signifi-cantly higher than that in the original OSSI

    solution. This may explain the fact that,

    while the same activity of scale inhibitor

    was present in both cases, the desorption

    profile of the OSSI seemed to be better

    because of the much higher concentrationgradient that drove the adsorption process

    in the first place. Hence, the time required

    to scale up the test coil was longer.

    Reservoir-Conditioned-Core Tests. The

    results from the precolumn tube-blocking

    tests cannot predict accurately what will

    happen in the field. As part of the product-

    development program, a reservoir-condi-tioned-core test is essential to determine

    whether the OSSI can offer a reasonable

    squeeze life when deployed in the field.

    Also, any potential damage to the forma-tion that might be caused by the OSSI

    chemical must be assessed.

    To examine the retention characteristicsof the OSSI, the effluents from both the

    adsorption and desorption stages were ana-lyzed. None of the samples showed any

    detectable level of scale inhibitor. The

    results from a separate analysis also con-

    firmed that less than 1% of the injected

    OSSI remained in these samples. It appearsthat all the OSSI injected had been

    adsorbed and that very few of these

    adsorbed molecules had been released dur-

    ing the kerosene flush. A likely explanation

    for such a unique phenomenon is that thehydrolysis and partitioning of the OSSI

    were highly efficient within the porous

    media. With only 2.7 pore volumes (PV) of 

    OSSI injected, all injected scale inhibitorhad been retained. The desorption profile

    with formation brine is more like that of 

    traditional scale inhibition. After peaking at

    approximately 44 000 ppm, the scale

    inhibitor returned to approximately 100ppm after 50 PV and finally down to 1 ppm

    after 600 PV of brine injection.

    For the injectivity and formation-dam-

    age study, the differential pressure across

    the core was monitored during the injec-

    tion of the spearhead, main pill, and theinitial backflow of kerosene and formation

    brine. A small pressure rise was registered

    when the spearhead and desorption brine

    were injected. In both cases, the injectionfluid was immiscible with the in-situ fluid.

    A small, gradual rise in the differential

    pressure occurred toward the end of the

    OSSI injection, which coincided with thebreakthrough of a minute quantity of 

    water. The authors believe this likely was

    caused by the end effect and redistribution

    of the water phase. If an interaction

    between the OSSI chemical and the corematerial occurred, which might have

    caused formation damage, a sharp increase

    in the injection pressure or a cessation of 

    flow after the locked-in period would

    be expected.

    Effect of W ater Saturation. For a mainly

    water-wet formation, the connate-water

    saturation in the reservoir can vary between5 and 25%, even if the field is not yet pro-ducing water. In formations where immo-

    bile-water pockets exist, the localized satu-

    ration can be even higher. One of the final

    tests carried out was to combine the OSSIpill (10% solution in kerosene) with forma-

    tion water in various ratios. Nine samples,

    with OSSI/water ratios ranging from 1:9 to

    9:1, were prepared. Apart from one sample

    with a 1:9 OSSI/water ratio showing minorturbidity, all other samples remained fully

    compatible. Mass transfer of OSSI mole-

    cules was observed in all cases. For thehigh-water-cut sample (90%), the observed

    minor incompatibility can be overcome inthe field by use of a properly sized hydro-

    carbon spearhead.

    CONCLUSIONS

    OSSI molecules hydrolyze and partition

    readily on contact with an aqueous phase.Once partitioned, the hydrolyzed OSSI

    molecules exhibit inhibition efficiency and

    retention characteristics similar to those of 

    generic water-based products. The mass-

    transfer process of the OSSI molecules fromthe oil phase to the water phase appears to

    be irreversible. Depending on the phase sat-

    uration, enhanced partitioning can be

    achieved. A larger hydrocarbon spearhead

    should be considered for wells with a 10 to25% water cut. The combination of an OSSI

    squeeze pill and a suitable hydrocarbon

    overflush will minimize many flowback

    problems associated with relative perme-ability and water block. Also, the cleanup

    period will be much shorter, leading to

    quick restoration of oil production to its

    presqueeze rate. This restoration of produc-

    tion rate is particularly beneficial to dry ornearly dry wells and to reservoirs with poor

    lift energy. For offshore environments, an

    OSSI squeeze minimizes water handling

    and subsequent discharge to the sea, there-

    by reducing the commonly observed oil-in-water problem after a conventional water-

    based squeeze treatment.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the

     synopsis has been taken has not been peer reviewed.

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    • MARCH 1999 75

    Uncontrolled growth of sulfate-reducing

    bacteria (SRB) in oilfield systems can create

    safety, environmental, and operational

    problems (such as microbiologically influ-enced corrosion, solids production, and

    biogenic H2S generation). Anthraquinone,

    a nontoxic biodegradable substance,

    uncouples the electron-transfer process in

    SRB required for the bacteria’s respirationwith sulfate. When this metabolic pathway

    is blocked, SRB are incapable of reducingsulfate to H2S; therefore, the reaction of H2S

    with soluble iron also is blocked.

    Anthraquinone is essentially insoluble inwater; however, the chemically reduced

    form (anthrahydroquinone) is soluble in a

    caustic solution. Anthraquinone, as treat-

    ments are referred to in this paper, was

    injected as a 10-wt% solution of the solubleanthrahydroquinone disodium salt in caus-

    tic. Injection of this solution into a flowing

    water stream forms submicron-sized parti-

    cles of the inhibitor. The small particles

    coat the interior surfaces of pipelines ininjection systems and subsequently become

    incorporated into the biofilm. Once the

    particles are incorporated into the biofilm,

    they partition into the cell membrane of thebacterial cells and inhibit sulfate reduction.

    These relatively insoluble, nonreactive par-

    ticles are believed to provide a “time-

    released” treatment within the biofilm and

    a continual source of sulfide inhibitor.Periodic treatments are required to replace

    anthraquinone that has been biodegraded

    or dissolved in flowing untreated water.

    Anthraquinone is not biocidal. Bacteria

    other than SRB also may be harmful in oil-field water systems and should be con-

    trolled with conventional biocides.

    Consequently, anthraquinone treatments

    are designed to be used as a supplement in

    these applications to extend the life of tra-ditional biocide treatments.

    FIELD DESCRIPTION

    The facility is composed of two separate

    systems, A and B. Both systems receive

    water from the same source. System A is a

    single injection plant pumping approxi-mately 29,000 B/D of produced water to 28

    injection wells. System B has three injectionplants that pump a total of approximately

    28,000 B/D of filtered produced water to 51

    injection wells. Water lines that were out of service dur-

    ing the field trial were inspected visually for

    solids deposition and found to be fouled

    heavily with accumulated solids. The pre-sumption was that this condition was repre-

    sentative of the lines treated during the trial.

    LABORATORY STUDIES

    Measurable sulfide production from the

    untreated field-initiated bottle tests began 4days after the wellhead-water samples were

    taken, while samples treated with the

    anthrahydroquinone solution were inhibit-

    ed for at least 12 more days. Laboratory-ini-

    tiated bottle tests used a synthetic mediumwith the cultured SRB. This test was

    designed to evaluate the effect of Fe2+ on

    the inhibition because Fe2+ forms a weak

    equimolar complex with anthrahydro-

    quinone. The Fe2+ content in the field pro-

    duced water was approximately 100 kmol,while the anthrahydroquinone concentra-

    tion injected during the field trial was

    approximately 500 kmol. The laboratorystudy was run with approximately equimo-lar Fe2+ and anthrahydroquinone(500 kmol and 440 kmol, respectively) and

    with excess Fe2+ (500 kmol) at the same

    440-kmol anthrahydroquinone level. The

    results indicate that the iron had negligible

    impact on the inhibition effect of theanthrahydroquinone, although high iron

    levels did affect the ultimate sulfide

    level obtained.

    Results from two sets of dynamicbiofilm-inhibition studies show significant

    inhibition of sulfide production for about 3days. After sulfide production increased,

    subsequent repeat treatments (500 ppm of 

    the anthrahydroquinone solution for 2 or 4

    hours) directly into the biofilm columnrestored inhibition for at least 1 day.

    During the second test, two treatments

    were applied before inhibition ceased, but

    these treatments did not appear to extend

    the inhibition period beyond that observedfor the first test. The initial treatment of the

    influent SRB flow allows the anthrahydro-

    quinone solution to contact the SRB inti-mately for approximately 1 minute before

    entering the biofilm column. This delayallows molecules of anthrahydroquinone

    to partition into the SRB cell membrane

    and inhibit sulfate respiration after an ini-

    tial lag period. The inhibition duration forthis laboratory system with a synthetic

    medium apparently is limited to approxi-

    mately 3 days. Subsequent treatments of 

    the developing biofilm are not as effective

    as the initial treatment because of thehydrodynamics of the laboratory system.

    The drop in pH of the treatment solution

    as it is injected into the medium causes the

    formation of rather large particles of 

    anthrahydroquinone that cannot penetratethe biofilm well because of the low shear

    stress at the wall of the biofilm column. In

    the field situation, where pipeline Reynolds

    numbers and shear stresses are high, how-

    ever, the anthrahydroquinone particlesthat form as the pH drops are colloidal and

    are transported easily to the biofilm on the

    pipe wall by shear dispersion. Additionally,

    small particles are necessary to obtain highlevels of sulfide inhibition.

    FIELD TRIAL

    A California facility was chosen for ananthraquinone-treatment program because

    of the very active SRB population and

    resulting production of iron sulfide solids.

    The active SRB population in the producedwaters of this facility required daily treat-

    ments with acrolein. The field trial was

    conducted during the summer of 1997 to

    determine whether cotreatment with

    anthraquinone could extend the intervalbetween acrolein treatments.

    H2S concentrations for Systems A and Bwere monitored daily. In System A, the pro-

    CHEMICAL MITIGATION OF SULFIDE

    IN WATER-INJECTION SYSTEMS

    This article is a synopsis of paper SPE

     50741, “A New Chemical Approach To

     Mitigate Sulfide Production in Oilfield

    Water-Injection Systems,” by  M.D.

     Johnson, M.L. Harless, and  A.L.

    Dickinson, Baker Petrolite, and E.D.

    Burger, SPE, EB Technologies, original-

     ly presented at the 1999 SPE

    International Symposium on OilfieldC  hemistry, Houston, 16–19 February.

    P R O D U C T I O N O P E R A T I O N S

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    P R O D U C T I O N O P E R A T I O N S

    duced water flowing to Injection Well A-2

    soured the most rapidly during each treat-

    ment cycle because of the relatively long

    residence time in the 31 / 2-in., 1,900-ftpipeline from the header to the well. Most

    other injectors had smaller-diameter flow-

    lines or shorter lengths from the headers.

     Well A-3 was the only other System A wellto experience a significant increase in H2Sin the injection water during each cycle. In

    System B, no injection water soured during

    the first treatment cycle, although the

    diatomaceous-earth-filter outlet water had

    high H2S on 16 July because of exceptionalfouling. The problem was resolved by back-

    washing the filter. Only the water trans-

    ported to the most remote System B well, B-

    1, soured significantly during the second

    and third cycles.In System B, H2S concentrations

    increased most rapidly during the thirdcycle, possibly because the ambient temper-

    ature increased almost 18°F (to 104°F dur-

    ing the daytime) throughout that cycle.Because most pipelines are not buried, flow-

    ing-water temperature also increased, prob-

    ably contributing to higher SRB activity.

    This high activity may account for the

    shorter period before H2S began to increase.During generation of baseline (control)

    data, produced water collected from System

    A Injection Well A-3 had a significant

    increase in H2S after 1 day. Produced water

    collected from System A Injection Wells A-1 and A-2 had increased concentrations of 

    H2S after 2 days. Produced water collected

    from all System B injection wells had

    increased concentrations of H2S 1 to 2 days

    after the start of the control period. Theseresults confirmed that daily acrolein treat-

    ments were required to maintain stable H2S

    levels in both injection systems.

    TOTAL SUSPENDED SOLIDS (TSS)

    No correlation between TSS and theacrolein/anthraquinone treatments was

    noted during the field trial or control peri-

    od. Random fluctuations in TSS were notedin produced waters collected from each of the injection wells monitored. Downstream

    TSS levels correlated closely with the TSS

    levels entering the systems. TSS levels were

    elevated slightly only during the third treat-

    ment cycle in System B, corresponding tothe increased H2S levels observed duringthat cycle. Also, both H2S and TSS levels

    were higher than those of the initial two

    treatment cycles during the System B con-

    trol period. Again, increased SRB activity

    cause by elevated water temperatures dur-

    ing the third treatment cycle and absence of acrolein/anthraquinone treatments during

    the control period are probable causes of 

    these increased H2S and TSS levels.

    SRB MEASUREMENTS

    Results from SRB serial dilutions for System

    A indicate that the population remained rel-

    atively stable throughout the trial and con-

    trol periods for the sample sites monitored.The SRB levels in the System B influentwater varied more than those in System A,

    although, overall, they were slightly lower

    than those entering System A. This variabil-

    ity most likely was caused by growth of SRBin the filter cake of the diatomaceous-earth

    filter coupled with backwashing frequency.

    Except for two wellhead water samples, the

    SRB levels were between 101 and 103

    cells/mL throughout the treatment and con-trol periods.

     ANTHRAQUINONE RESIDUALS Water samples were collected at various

    locations in each system during the treat-

    ment periods to determine system use of the chemical and to confirm that the chem-

    ical traveled through the system. These data

    indicate that the anthraquinone concentra-

    tion decreased rapidly immediately down-

    stream of the injection location, then slow-ly decreased as the pipe branched to remote

    wells. Deposition of the anthraquinone in

    the biofilm was confirmed by the decrease

    in concentration within the pipeline seg-

    ments. Monitored parameters following thetreatments indicate that sufficient

    anthraquinone generally reached all parts

    of the system during each injection period.

    CONCLUSIONS

    Laboratory studies confirmed field resultsthat biogenic sulfide production within this

    California oil field’s water-injection system

    can be inhibited with anthraquinone treat-

    ments. Extended-duration inhibition wasobtained in the laboratory. The presence of 

    iron does not appear to affect sulfide inhi-

    bition. Simple laboratory studies were diffi-

    cult to perform with this type of inhibitorbecause of the need for more realistichydrodynamic conditions to keep the insol-

    uble inhibitor particles small and bioavail-

    able, as they are in a field pipeline system.

    During the field trial, H2S concentrations

    remained stable for up to 9 days in both

    Systems A and B following eachacrolein/anthraquinone treatment cycle.

    After these stable periods, sharp increases

    in H2S concentrations indicated that the

    available anthraquinone concentrations

    within the biofilm had dropped below

    inhibitory levels. H2S level appears to bethe most responsive parameter for monitor-

    ing treatment efficacy. Significant increases

    in wellhead-water H2S levels could be

    detected more easily and reliably than TSS

    or SRB levels.As with H2S concentrations, steady

    increases in TSS were expected during the

    cycle period but were not observed during

    the field trial. Instead, TSS concentrationsfluctuated throughout the trial and controlperiods. Therefore, no correlation could be

    made between TSS concentration and each

    acrolein/anthraquinone treatment or con-

    trol period. The observed TSS concentra-tion fluctuations likely were caused by

    changes in influent-water quality rather

    than the effects of downstream SRB activity.

    The SRB population in the wellhead-

    water samples generally remained stablethroughout both water-injection systems.

    As with TSS levels during the first and sec-

    ond treatment cycles, variability most like-ly was the result of changes in the influent-

    water quality.The increased H2S concentrations toward

    the end of each acrolein/anthraquinone

    treatment, coupled with a relatively stable

    SRB population throughout the field trial,

    indicate that anthraquinone was acting as a

    sulfate-reduction inhibitor rather than as abiocide. If the treatment program was per-

    forming as a biocide, a decline in the SRB

    population would have been observed

    immediately after each treatment. This

    decrease would have been followed by anincrease in SRB population over time. The

    anthraquinone treatment was acting to con-

    trol any further growth and reproduction of 

    the SRB population, resulting in a stablepopulation over the period of each

    acrolein/anthraquinone treatment.

    Additional field work is required to

    determine the treatment life of anthra-

    quinone in other systems. Anthraquinonemust penetrate biofilms to contact sessile

    SRB, and, therefore, treatment periods and

    concentrations may be influenced signifi-

    cantly by the biofilm thickness. It is possi-

    ble that less-heavily-fouled systems wouldrequire fewer anthraquinone treatments or

    lower concentrations to achieve adequate

    inhibition of SRB sulfate reduction for

    extended periods.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the

     synopsis has been taken has not been peer reviewed.

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    78 MARCH 1999 •

    Oil and gas production in the Appalachian

    basin is characterized by mature, water-sen-

    sitive wells. Many wells have been produc-

    ing for more than 25 years. Most of the stor-age wells have been in use 40 years or more.

    These wells often are plagued with entry

    problems caused by restrictive fittings,

    valves, or tubing that hinder the repair and

    replacement of corroded, faulty, or under-sized wellheads and casing top joints. The

    conventional approach uses coiled tubing(CT) with inflatable packers that are set

    through the restriction into the good casingdownhole, allowing uphole repairs. These

    tools are expensive and pose stability and

    safety problems in old casing. An alterna-

    tive is to use CT to place crosslinked-poly-

    mer plugs to protect the formation from thekill fluid used to isolate the formation pres-

    sure during repair operations.

    BACKGROUND

    Many additives and fluid systems have been

    introduced to control fluid loss or to pro-vide a nonmechanical means to isolate

    intervals. These systems usually are high-

    viscosity fluids and can contain solid partic-

    ulates. Tests have shown that these systems

    can be difficult to remove and can damagethe intervals they are designed to protect.

    Crosslinked-polymer plugs provide a

    clean method of protecting a producing

    zone from damaging workover fluids.

    These crosslinked gels contain higher con-centrations of polymer than other

    crosslinked fluids, such as fracturing fluids.

    CROSSLINKED-POLYMER PLUG

    The crosslinked-polymer plug used in this

    application consists of a carboxymethyl-hydroxyethylcellulose at a concentration of 

    1.2 wt% when mixed in fresh water. The

    system is buffered with an organic acid to a

    pH of 3.5. To ensure complete hydration,

    the polymer is preslurried in isopropylalcohol. A water-soluble zirconium salt is

    added at 0.15 vol% as the crosslinker. The

    system has a delayed, or retarded, crosslink

    that occurs as a function of time and tem-perature. This delay allows proper place-

    ment of the plug downhole before

    crosslinking. The plug can be placedthrough casing, tubing, or CT, and a wide

    variety of breaker systems can be used toremove the plug.

    LABORATORY DATA 

    The crosslinked-polymer plug has been

    successfully hydrated and crosslinked in

    many fluids, including fresh water, 2%potassium chloride (KCl), 3% ammonium

    chloride, and 16.0-lbm/gal fluid spiked

    with zinc bromide. Crosslinking of the sys-

    tem is both a function of temperature and

    pH. The optimum pH of the system isbetween 3.5 and 4.0. The system is normal-

    ly placed as a linear fluid, with crosslinking

    occurring once the fluid is in place.

    Typically, the higher the temperature and

    lower the pH, the faster the crosslink.These variables need to be taken into

    account when designing job procedures.

    The crosslinked-polymer plug is stable

    at downhole temperatures up to 200°F forseveral days. For temperatures higher than

    175°F, gel stabilizers and extra polymer can

    be added for stability. Tests indicate that

    the crosslinked-polymer plug can help pre-

    vent damaging workover fluids from enter-ing a productive zone even in high-perme-

    ability formations.

     When zonal isolation is no longer

    required, the crosslinked-polymer plug

    must be removed without causing damageto the formation. Breaker systems evaluated

    included oxidizers, enzymes, and acids.

    Return permeability of almost 100% was

    obtained in all cases.

    CASE HISTORIES

     Wellhead Changeout and Pipe Repair.

    The first case history with the crosslinked-polymer plug was for wellhead changeouts

    on 12 Pratt storage-pool wells in Greene

    County, Pennsylvania. The wells were

    drilled in the late 1920’s and recompleted as

    storage wells during 1945–50. The storage-pool sand is a moderately clean conglomer-

    ate. Well depths range from 2,700 to 3,000

    ft. Pool pressure during the project ranged

    from 450 to 500 psi. The wells were com-

    pleted with 51 / 2-in. casing with the cementtop 1,000 ft off-bottom. Approximately half 

    the wells were openhole completions, andthe rest were openhole with 31 / 2-in. perfo-

    rated liners. All the wells have a restricted

    entry above the “T” caused by a weldedswedge and a 4-in. restricted inside-diame-

    ter valve.

    Changeout Procedure. Wellhead change-

    outs were performed with a CT unit. Once

    on bottom, the CT was pulled up 25 to 30ft and 250 gal of the crosslinked-polymer

    plug was mixed. The pH of 4.0 provided

    adequate pumping time. To water wet the

    pipe, 1 to 2 bbl of 2% KCl was pumped; this

    was followed by the crosslinked-polymerplug. The plug was displaced out of the

    tubing with 10 bbl of 2% KCl, and the CT

    was pulled to the estimated top of the plug

    at 2,600 ft. After approximately 1 hour, 2%

    KCl water was pumped at 1.0 bbl/min untilthe pressure increased to 200 psi higher

    than the pool pressure to allow the

    crosslinked-polymer plug to set fully. The

    pressure was bled off into the flowbacktank, and pumping resumed at 1.0 bbl/min.

    This procedure was continued until the

    well was killed at 750 psi overbalanced

    pressure. The CT was pulled to surface, and

    the CT unit was moved off the well whilethe operator changed the wellhead and

    made repairs to the top joints of pipe with-

    out experiencing any problems.

    Removing the Crosslinked-Polymer Plug.

    Nitrogen was used to unload the well whiletripping in with CT to the top of the poly-

    mer plug. Then, 15% HCl was pumped in

    as an external breaker. As the gel started

    breaking, the acid was jetted to the bottom.

    Nitrogen was used to circulate the hole

    clean to total depth. The CT was tripped

    out of the hole while pumping nitrogen and

    the wellhead pressure monitored as itreturned to pool pressure.

    NONDAMAGING POLYMER PLUGS

    FOR TEMPORARY WELL ISOLATION

    This article is a synopsis of paper SPE

     51054, “Novel Application of 

    Nondamaging Polymer Plugs With

    Coiled Tubing Improves Efficiency of 

    Temporary Well-Isolation Projects,” by

    Brian B. Beall, SPE, and Thomas E.

    Suhy, SPE, BJ Services Co., originally

     presented at the 1998 SPE Eastern

    Regional Meeting, Pittsburgh,Pennsylvania, 9–11 November.

    P R O D U C T I O N O P E R A T I O N S

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    • MARCH 1999 79

    Shale Control. A crosslinked-polymer plug

    was used to control caving shales. While

    drilling the Berea formation at approxi-

    mately 2,400 ft, a 4-MMcf/D open-flow gaszone was encountered. Rather than cement

    the 41 / 2-in. casing, the decision was made

    to set the casing on a formation packer at

    1,350 ft, just above a sloughing shale.Below the shale, the well was completed asa 61 / 4-in. open hole. After producing the

    well for several months, cavings from the

    Sunbury shale bridged off over the produc-

    ing zone and shut off gas production.

    Several attempts were made with a conven-tional service rig to remove the bridge and

    reset the 41 / 2-in. casing approximately 120

    ft lower to stop the caving. After each

    cleanout attempt, the shale caved back in

    before the tool string could be removed andthe casing released and lowered.

    CT Cleanout. CT was tripped into thewell with a 2.875-in. drill motor on 11 / 4-in.

    tubing. The bridge was drilled out at 2,500

    ft while circulating with gelled water. Oncethe 10- to 20-ft bridge was drilled through,

    the tubing and tools were run in the hole

    until a solid bridge was encountered at

    2,900 ft. While continuing to circulate,

    500 gal of crosslinked-polymer plug was

    pumped through the tubing and drill

    motor. The tubing was then pulled into the

    casing to allow the polymer plug to set.After 1 hour, the CT was tripped out of the

    hole and the 41 / 2-in. casing packer released.

    Four joints of pipe were added, and the cas-

    ing packer was reset at 1,470 ft. The CT was

    tripped back into the hole with a jettingnozzle, and 500 gal of 15% HCl was used tobreak the gel and remove any additional

    bridges. The well was cleaned out with

    nitrogen, the tubing tripped out of the well,

    and the well returned to production.

    Fluid-Loss Control for Cementing Water

    Zones.  While drilling a well near Brandy-

    wine, West Virginia, two water-producing

    zones were encountered in high-fluid-loss

    shales before total depth could be reached.A crosslinked-polymer plug was pumped

    ahead of the cement plug as a fluid-lossmaterial to avoid losing the cement volume.

    A volume of 250 gal/zone was pumped

    through the drillpipe, each zone pluggedoff successfully, and the well completed

    as planned.

    Cement Retainer To Plug and Abandon a

    Salt-Solution Mine. This well was drilled

    in the 1950’s and used to produce salt-brine

    solution for the retrieval of minerals and

    chemicals. Repairs to the casing were per-

    formed frequently because of the corrosiveenvironment. The 6,500-ft well was com-

    pleted with 7-in. casing to the top of the salt

    cavern. The plant was abandoned in the

    late 1980’s, and the well and plant revertedto the original owner. Plugging and aban-

    donment was required. The 7-in. casing

    was highly scaled, with the inside diameter

    reduced to 2 in. Usually, inflatable packers

    are set in the casing just above the cavern;in this case, however, no CT unit was avail-

    able to set the plug. A 500-gal crosslinked-

    polymer plug was pumped ahead of the

    cement and balanced in the casing with

    3,200 psi cavern pressure. The polymerplug held the cement in place during the set

    time without any problems.

    Please read the full-length paper for

    additional detail, illustrations, and ref-

    erences. The paper from which the

     synopsis has been taken has not been

     peer r