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export compressor instability detection using system 1* and proficy ** smartsignal software BP MAGNUS PLATFORM part 1 ORBIT Vol. 32 • No. 3 • Jul. 2012 DEPARTMENTS CASE HISTORIES

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Page 1: ORBIT Vol. 32 • No. 3 • Jul. 2012 - Home Page | GE ... · PDF file2 ORBIT Vol. 32 • No. 3 • Jul. 2012 DEPARTMENTS CASE HISTORIES. ... towards the antisurge control system on

export compressor instability detection using system 1* and proficy** smartsignal software

BP MAGNUS PLATFORM

part 1 ORBIT Vol .32 • No.3 • Ju l .2012

DEPARTMENTS

CASE HISTORIES

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Linda Alrabady

GE Oil & Gas Machinery Diagnostic

Services (MDS) Lead Engineer

[email protected]

The problem occurred when the multistage centrifugal

natural gas compressor was operated at significantly

reduced loads. Happily, BP had recently deployed real time

condition monitoring & anomaly detection technologies

in order to improve the reliability of the offshore rotating

equipment. These included GE’s Bently Nevada System 1

and Proficy SmartSignal Shield software, which were

deployed per BP defined practices. The software

installations were combined with a GE Supporting Services

Agreement (SSA) to ensure access to the right skills.

SmartSignal Shield software had been installed four

months before the events described here, and was

able to flag the compressor instability at a very early

stage. Additionally, System 1 software provided

confirmation of the problem by accommodating

deeper diagnostic analysis. The rotating equipment

team was quickly notified of the problem. Working with

the offshore team, they routed the wells differently to

manage load on the affected compressor. They also

opened the compressor anti-surge valve manually

to increase recycle flow and stabilize the rotor.

These prompt actions implemented a short-term solution,

which avoided failure of the compressor and unplanned

shutdowns of the affected system. A future article will

describe Part 2 of this case study, which will address

long-term solutions to the root cause of the problem.

Historically, there have been several instability-related

failures to the compressor thrust bearing, and in the

past six months there have been at least 4 trips. This

case history demonstrates how effective use of the

software platform enabled quick sharing of important

information across the region - enhancing plant safety

while at the same time avoiding the lost production

that a compressor failure would have caused.

Peter Griffiths

Production Enhancement

Team Leader

BP North Sea

Dave Watson

Reliability and Maintenance

Team Leader

BP North Sea

THIS CASE STUDY DESCRIBES AN EXAMPLE OF A GAS COMPRESSOR THRUST POSITION INSTABILITY PROBLEM ON A BP OFFSHORE DRILLING & PRODUCTION FACILITY.

Jul .2012 • No.3 • Vol .32 ORBIT

DEPARTMENTS

CASE HISTORIES

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Site Overview

The BP Magnus platform is a

combined drilling and production

platform in one of the UK’s most

northerly fields, located in the North

Sea, 160 km northeast of Shetland,

Scotland. The oilfield was discovered

in 1974. At peak production times,

the platform can produce 156,000

bpd oil, 12,000 bpd gas condensate

and 60 mmscfd natural gas.

The platform’s gas processing

plant includes two separate trains

which each have three sections:

flash gas, gas drying and chilling &

export compression. Before export

compression, the gas is first fed to

a suction drum where liquids are

accumulated and drained. The gas is

then compressed in the Low-Pressure

first stage (LP Compressor) after

which it passes through the first stage

aftercooler to the High-Pressure

second stage (HP Compressor) and

the second stage aftercooler.

Machine Train Description

The compressor described in

this case study is one of two

multistage vertically split centrifugal

compressors with electric motor

drive via a speed increasing gearbox

(Figure 1). The axial thrust due to the

gas pressure difference is mostly

balanced using a balance drum.

However, since some residual axial

load may exist during operation, a

tilting-pad double thrust bearing

is used to avoid the possibility of

damage to the labyrinth-type shaft

seals (Figure 2). Both the LP and

the HP compressor use fluid-film

bearings, and vibration is monitored

using XY radial vibration transducers.

Events SequenceThe first indication of the problem

came when the SmartSignal Shield

software flagged an advisory of

a thrust position problem due to

significant and persistent deviation

from the normal condition. It

was clear at the time that there

was a high correlation between

the changing compressor load

and the rotor thrust position.

As part of BP’s existing SSA coverage,

a GE Machinery Diagnostic Engineer

in the UK observed the alarm in

the BP Dyce office, performed

initial evaluation of the situation

and discussed the issue with the

SmartSignal team in Chicago USA,

quickly notifying the customer of the

evolving situation. Further analysis

of the situation was required as the

data from the SmartSignal installation

was sampled every 10 minutes.

When the thrust instability occurred,

the System 1 platform had been

online for less than a week, but had

been acquiring data at high sampling

rates. The System 1 data (Figures

3 through 7) clearly indicated that

thrust displacement started to ramp

up along with significantly reduced

load, high pressure ratio, low flow

rate and no significant response from

the antisurge valve on 04APR12.

FIGURE 1: This simplified machine train diagram shows Export Compressor Train 1. Not shown here are the suction drum before the LP Compressor, and the aftercoolers after each compressor’s discharge.

0 ORBIT Vol .32 • No.3 • Ju l .2012

DEPARTMENTS

CASE HISTORIES

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FIGURE 2: This photo shows the self-equalizing tilting pad double thrust bearing from the HP Compressor described in this article.

FIGURE 3: HP Compressor Thrust Position Trend. The horizontal red line (labelled) indicates the trip setpoint for axial thrust position. Rotor position closely approached the trip setpoint (at +0.72 mm) during the period of low flow and instability on 04APR12. But after corrective actions were implemented, the rotor position returned to normal.

FIGURE 4: Export Compressor A Motor Load (Current) Trend. The lower than normal motor load on 04APR12 corresponds to the period of low compressor flow and instability described in this article.

Jul .2012 • No.3 • Vol .32 ORBIT 1

DEPARTMENTS

CASE HISTORIES

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FIGURE 6: HP Compressor Flow Rate Trend. Following the period of low flow on 04APR12, compressor flow was restored to normal on 05APR12.

FIGURE 7: HP Compressor Antisurge Valve Opening Position Trend. Observe that the valve did not respond as anticipated during the period of the flow instability on 04APR12.

FIGURE 5: HP Compressor Pressure Ratio Trend. The higher than normal pressure ratio on 04APR12 corresponds to the period of low compressor flow and instability described in this article.

2 ORBIT Vol .32 • No.3 • Ju l .2012

DEPARTMENTS

CASE HISTORIES

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The anti-surge control system is

used to prevent the compressor

from surging by recycling gas from

the compressor discharge side to

the suction drum. This provides

the minimum flow rate required

to keep the compressor running

at an adequate margin from the

surge threshold. Several different

parameters are fed to the control

system to allow it to calculate the

required recycle valve position.

These include compressor suction

flow rate and inlet temperature and

differential pressure between the

compressor suction and discharge

pressures (used to compensate

for varying conditions of suction

pressure and gas molecular weight).

Although both the LP and HP

Compressors were running at reduced

load only the HP compressor suffered

from a condition of instability.

The situation directed suspicions

towards the antisurge control

system on the HP compressor. As

seen in Figure 7, the valve position

showed no significant changes

i.e. less than 4% even though the

compressor was in surge mode. To

support this finding, System 1 data

was reviewed in several different

steady-state and transient formats.

Figures 8 through 10 show the

vibration spectrums from thrust

bearing position measurements for

the HP and LP Compressor and the

Gearbox High Speed Shaft.

THIS CASE

HISTORY WAS

A GREAT

EXAMPLE OF

HOW THE

CONDITION

MONITORING

PLATFORM

ALLOWED

ENHANCING

THE SAFETY

OF THE PLANT

OPERATION,

WHILE AT THE

SAME TIME

AVOIDING LOST

PRODUCTION.

With the machine train speed at

12,450 rpm, 1X vibration frequency

is 207.5 Hz. This 1X peak can be

seen for all three thrust bearings.

However, the HP compressor thrust

bearing vibration also showed a very

dominant frequency peak at 0.22X

(45 Hz), while the LP Compressor

and Gearbox did not. A potential

cause for such subsynchronous

vibration is aerodynamic

excitation (i.e., stall or surge).

The waterfall plot for the HP

Compressor Drive End (DE) bearing

for the duration of 22MARCH2012

to 21APRIL2012 is shown in Figure

11. This plot shows several regions

of instability with two main

subsynchronous components

(0.22X & 0.459X). Both of these

components are “forward” in the full

spectrum plot, which indicates that

their precession is the same as the

direction of rotation for the machine.

The origin of the 0.459X will be

discussed in Part 2 of this case study,

which we will share as a future

Orbit article. For now, we can say

that this frequency is in the range

of a classic fluid induced instability

condition such as oil whirl or whip.

We know that tilting pad bearings

typically do not show such behaviour,

so our next candidate would be

the shaft seals on the compressor.

These include both labyrinth type

gas seals and sleeve type oil seals.

Jul .2012 • No.3 • Vol .32 ORBIT 3

DEPARTMENTS

CASE HISTORIES

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FIGURE 9: LP Compressor Thrust Vibration Spectrum. Again, the 207.5 Hz peak corresponds to 1X vibration, and it is obvious that there is only a very small component at 0.22X.

FIGURE 8: HP Compressor Thrust Vibration Spectrum. The 45 Hz peak corresponds to a vibration frequency of 0.22X. This is a classic symptom of stall/surge in turbocompressors.

ORBIT Vol .32 • No.3 • Ju l .2012

DEPARTMENTS

CASE HISTORIES

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Figures 12 through 14 show the

orbit timebase (waveform) plots

and spectrums before, during and

after the period of compressor

instability for vibration measured

at the HP Compressor DE bearing.

These plots show conditions for

compressor load that was normal,

significantly lower than normal,

and normal, respectively. Observe

that the 0.22X component (circled)

appeared when the compressor

was running at significantly reduced

load and then disappeared when

load was restored to normal.

Corrective Actions

After confirming the root cause of

the instability (using System 1 and

SmartSignal Shield software) to

be a combination of significantly

reduced load and a problem with

the HP Compressor antisurge control

system, the rotating equipment

team was notified. Working with

the offshore team, they ensured

that the production wells were

routed differently to manage the

compressor load and that the anti-

surge valve was manually opened

to increase the recycle flow rate

and stabilize the rotor (Figure 3).

As levels were approaching the thrust

position trip level (+ 0.72 mm), timely

intervention saved the platform from

the consequences of a machine trip

and a potential thrust bearing failure

resulting in the avoidance of a $1

million (USD) net cash deferral. As a

result of this event, BP demonstrated

the ability to quickly share important

information across the region to

prevent similar future events.

FIGURE 10: Gearbox High Speed Shaft Thrust Vibration Spectrum.

Jul .2012 • No.3 • Vol .32 ORBIT

DEPARTMENTS

CASE HISTORIES

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FIGURE 11: HP Compressor DE Bearing waterfall plot.

Conclusions

The export gas compressor loading

is dictated by production demand

at any particular time. Ideally, the

compressor should be operated

very close to its Best Efficiency Point

(BEP) whenever possible. However,

it is also very important to avoid

operating the compressor beyond

its surge threshold, which occurs at

a combination of high head and low

flow. When compressor surge occurs,

the rapidly fluctuating thrust loads

can be very destructive, and can

cause major damage to the machine.

The second part of this case study

will address long term solutions

to the instability conditions

described in this article, and will

provide additional detail into the

observed 0.459X subsynchronous

vibration component and its

relation to the rotor instability.

Copyright © 2012 General Electric Company. All rights reserved.

* denotes a trademark of Bently Nevada, Inc., a wholly owned subsidiary of General Electric Company.

** Trademark of GE Intelligent Platforms, Inc. SmartSignal is a trademark of SmartSignal Corporation, a wholly owned subsidiary of GE Intelligent Platforms, Inc.

ORBIT Vol .32 • No.3 • Ju l .2012

DEPARTMENTS

CASE HISTORIES

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FIGURE 12: Orbit timebase and spectrum plots BEFORE the period of reduced compressor load.

FIGURE 13: Orbit timebase and spectrum plots DURING the period of reduced compressor load. Observe the subsynchronous peak at 0.22X (circled).

FIGURE 14: Orbit timebase and spectrum plots AFTER the period of reduced compressor load. Observe that the subsynchronous peak at 0.22X is no longer present.

Jul .2012 • No.3 • Vol .32 ORBIT

DEPARTMENTS

CASE HISTORIES