nuclear middletown. pennsylvania 17057 writer's direct diallicensee event report narrative...

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I l . . Nuclr Office of Inspection and Enforcement Attn: Hr. Ronald c. Haynes, Director Region I US Nt•clear Regulatory Colssion 631 Park Avenue King of Prussia, PA 19406 Denr Sir: June 18, 1982 4400-82-L-0104 P.O. Box480 Middto. Pennsylvania 17057 717·944-7621 Wri ter's Dirt Dial Num Three Hile Island Nuclear Station, Unit 2 (I-2) Operatin& License No. DPR-73 Docket No. 50-320 Licensee Event Report 82-016/0JL-0 ,\ttached please find Licensee Event Report 82-010/0JL-0 conceing the inoperable deluge sprinkler heads in the H 2 Purge and the Auxiliary Building Exhaust Filter Cabinets on Hay 19, 1982. This event conces Section 3.7.10,2 and ts considered reportable under Section 6.9.1.9(b} of the Interim Recovery Technical Specifications. JJB/SDC/jep Attachments CC: L. II. Barrett, Deputy Program Director, THI Program Office Dr. B. J. Snyder, Program Director, I Program Office V. Stcllo, Deputy Executive Director 8207020237 820618 PDR AK 0� 03 20 5 P GPU Nuclear •s a part of the General Pubhc Uhht•es Sys!e

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Page 1: Nuclear Middletown. Pennsylvania 17057 Writer's Direct DialLICENSEE EVENT REPORT NARRATIVE REPORT THI-II LER 82-016/03L-O EVENT DATE - Hay 19, 1982 I. F.XPLANATION OF OCCURRF.NCE Attachment

I

• l . .

Nuclear

Office of Inspection and Enforcement Attn: Hr. Ronald c. Haynes, Director Region I US Nt•clear Regulatory Col!llllssion 631 Park Avenue King of Prussia, PA 19406

Denr Sir:

June 18, 1982 4400-82-L-0104

GPU ......_ P.O. Box480 Middletown. Pennsylvania 17057 717 ·944-7621 Writer's Direct Dial Number:

Three Hile Island Nuclear Station, Unit 2 (THI-2) Operatin& License No. DPR-73

Docket No. 50-320 Licensee Event Report 82-016/0JL-0

,\ttached please find Licensee Event Report 82-010/0JL-0 concerning the inoperable deluge sprinkler heads in the H2 Purge and the Auxiliary Building Exhaust Filter Cabinets on Hay 19, 1982.

This event concerns Section 3.7.10,2 and ts considered reportable under Section 6.9.1.9(b} of the Interim Recovery Technical Specifications.

JJB/SDC/jep

Attachments

CC: L. II. Barrett, Deputy Program Director, THI Program Office Dr. B. J. Snyder, Program Director, THI Program Office V. Stcllo, Deputy Executive Director

8207020237 820618 PDR ADOCK 0�000320 5 PDR

GPU Nuclear •s a part of the General Pubhc Uhht•es Sys!ern

Page 2: Nuclear Middletown. Pennsylvania 17057 Writer's Direct DialLICENSEE EVENT REPORT NARRATIVE REPORT THI-II LER 82-016/03L-O EVENT DATE - Hay 19, 1982 I. F.XPLANATION OF OCCURRF.NCE Attachment

LICENSEE EVENT REPORT U. a. NUCLEAR IUGULATORV C:O.WISSION

Attachment 1 4400-82-L-0 104

� CONTROL II LOCI(: 1 J0 "u"" Pt�INT oR TYH ALL RIOUtRID INFDAMATIONI

IP lA IT IH 1112 l(!)lo I ol -1 ol ol ol o! ol - 1 ol ol@l4llltlll tl01 I I(V I �ltl�SU CODE It 11 LIClloiSl tjiJMilll :l5 2e �IClloiSl TV'l J0 �

CON'T

roTil, :��� l..!:...X!)IO 15 10 to 1 o I 3 I 2 I o (Dio I sl 1 I 91 sl 2 (!)! o I 61 1 I sl sl 2l@ � 10 II DOCK IT tjUiotiEII • .. lVEtjT OATI lt � III'OIIT DATE 10 EVENT OESC:RI"ION ANO 'ROBAIILE CONSEQUENCES @ 1,\t 1100 hours on Mny 19, 1982. whtl(' performing Suryclllgnce Procedure 4333-JYI

[[]]] J(Fire System Deluge/Sprinkler System flow Test), it was determined that the three (3) []]!] 1112 J>urgc nod 18 of 90 Auxiliary Building Exhaust Filter Cabinet Deluge Sprinkler

[[I!) Jhcnds were lnopernble. Tills condition plnced the Unit in the nction statement of

(]Jj] J'fl'ch Spec 3. 7 .10.2 nod ls considered reportable under Tech Spec 6.9.1.9(b). This

[]]I) levent had no effect on the plant, its operation, or the health and snfety of the

[]JI] ubi I c. f I I

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SYSTH• CAUSE CAUSE COM... VALV( COOl CODE SUICODl C()M"'tjE .. T COOl SUICOOl SUICOOE

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CAUSE DESCR"TION ANO CORRECTIVE ACTIONS @ .. 41

!The lno(ll'rabllltv Wn!l cnused bv reduced flowrntc capacity resultins from l) installatiof\

£III] !of :1 hllnd flnnsc ln the supply llne for tht! 112 Purse Exhnust Filter Cabinet, nnd 2)

o:IIl 1 the co I lect lun of vet)' fIne sed lment or debris cloggtn� the nozzles of the Aud liary

£III) lllulldln1� J,;xhnust Filter Cnblnet deluge heads. The he01ds were returned to operable

[!J!J 1 status nn :-lnv 28, 1982, nfter dcanlnl!,and re1:10vat of the hllnd flan�,tc. l I I

,ACI�ITY ljQI. STA1VS .. "OWl II OTH(II STATUS \::::1 [IlD LxJ@ I 0 I 0 I 0 !@I Recovery mode I f I I ID 12 1l tt ACTIVITY CptjT('<T � �II(UASIO 0' IIlLI AS( AUOUNT OF ACTIVITY® � l.U@ UJ®I N/A I 7 I I ID 11 tt

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M(TH 00 0' f.:::\ OISCOVIRY OISCOY(IIY OISCIII"IOtj � lJtj�IObserved during surveillance u 41

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lJJIJ I 0 I 0 I 0 r&lt.J�..__--:" __________ _:.:,Nic.:,.A:...._ _________ � ' I ' 11 11 u . 10 'EASQf< .. (L ltjJUIIIU 1:':\ ltjU"'Itll OUCII.,TIO!i� � lo to !o 1�..__-----------�N�A�------------� ' • • 11 12 10

lOSS OJ Oil OA ... AG( TO ,ACIUTV '4J'; TYP( DUCR.,TIO.. �

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'VIllgTV 8207020245 820018 10 r.::-r.:'1 ·�ucp/0\ouc"'"IOtj@ PDR ADOCK 05000320 L!....WU UW�I S PDR 1 I I ID

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I 1111111111111� NAMEOF,AE,ARER�S-t•e•V�e�n�D-·�C�h�a•p�l�i�n---------------

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'HONE: (717) 948-8461 � ..

Page 3: Nuclear Middletown. Pennsylvania 17057 Writer's Direct DialLICENSEE EVENT REPORT NARRATIVE REPORT THI-II LER 82-016/03L-O EVENT DATE - Hay 19, 1982 I. F.XPLANATION OF OCCURRF.NCE Attachment

LICENSEE EVENT REPORT NARRATIVE REPORT

THI-II LER 82-016/03L-O

EVENT DATE - Hay 19, 1982

I. F.XPLANATION OF OCCURRF.NCE

Attachment 2 4400-82-L-Ql04

At 1100 hours on Hay 19, 1982, while performing surveillance procedure 4333-3Y1 (Fire System Deluge/SprinklPr System Flow Test), it was determined thnt the three (3) H2 Purge Exhaust Filter Cabinet (AH-F-34) deluge sprinkler heads and eighteen (18) o f the ninety (90) deluge sprinkler heads in the Auxiliary Building Exhaust Filter Cabinet (AH-F-lOB) were inoperable.

This condition placed the unit in the action statement of Technical Specification 3.7.10.2 and is considered reportable under Technical Specification 6.9. 1.9(b).

11. CAUSE OF TilE OCCURRENCE

The deluge heads were declared inoperable as a result o f reduced or no flow conditions observed during compressed gas flow testing. Investigation has shown that the loss of flow in the H2 Purge Exhaust Filter Cabinet was the result of installation of a blank flange in the supply line, upstream of the deluge heads. It has not been determined when the blank flange was installed. However, it should be noted that the deluge system is installed for the prott>ction of the charconl adsorber bank in the 112 Purge Exhaust Filter Cabinet. TI1e charcoal adsorbers were removed from the Filter Cabinet in September. 1980. Therefore, the inoperability o f the three (3) deluge heads has been of no safety significance since that time.

Investigation has shown the loss of or low flow conditions ln the 18 Auxiliary Bullding Exhaust Filter Cabinet deluge heads was the result of very fine sediment and/or debris blocking the nozzles.

lll. CIRCUMSTANCES SURROUNDING TilE OCCURRENCE

At the time of the occurrence, the Unit 2 facility was in a long-term cold shutd�� state. The reactor decay heat was being removed via loss to ambient. Throughout the event there was no efCect on the Reactor Coolant System or the core.

IV. CORRECTIVE ACTIONS TAKEN OR TO BE TAKEN

The deluge sprinklers were checked and cleaned as necessary. In addition, the blind flange in the supply line to AII-F-34 was removed. At 0935 hours on Hay 28, 1982, the deluge sprinkler heads in both AH-F-34 and �l-F-lOB were declared operable.

Page 4: Nuclear Middletown. Pennsylvania 17057 Writer's Direct DialLICENSEE EVENT REPORT NARRATIVE REPORT THI-II LER 82-016/03L-O EVENT DATE - Hay 19, 1982 I. F.XPLANATION OF OCCURRF.NCE Attachment

-2- Attachment 2 440D-82-L-0104

The sediment found 1n the MI-F-lOB sprinkler heads hns been sent for analysis in order to determine its origin.

V. COMPONENT FAILURE DATA

N/A