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19 th National Award for Excellence in Energy Management -2018 My Home Industries Private Limited. Mellacheruvu Cement Works

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19th National Award for Excellence in Energy Management -2018

My Home Industries Private Limited.

Mellacheruvu Cement Works

❖ My Home Industries Pvt Ltd (MHIPL) is established in the year 1998 with an installedcapacity of 0.2 mtpa and rose to 10.0 mtpa.

❖ MHIPL entered into a Joint Venture with CRH Plc, Ireland in 2008 an internationallyreputed group having the business in cement and building materials in 35 countries.

❖ Other core businesses of the group are Construction & Real Estate, Power, Transport,Power Consultancy and Education.

❖ MHIPL-MCW is an ISO 9001:2015, ISO 14001:2015, OHSAS 18001:2007,ISO 50001:2011certified company.

❖ MHIPL-MCW received CII Green Co GOLD Rating in June’2017

❖ MHIPL is the members of CSI (Cement Sustainability Initiative ) and also have theroad map for sustainability.

Company Profile

MY HOME INDUSTRIES PVT LIMITEDMCW

MY HOME GROUP

Company Profile

Cement Process Flow Diagram

Sl. No. Projects 2015-16 2016-17 2017-18

Achieved

Total Annual Savings

(Rs in Lakhs)

Co2 Reduction MT

1 No Investment 7 5 4 116 2350

2 Investment 12 10 12 4704 98156

Total 19 15 16 4820 100506

Energy Saving Initiatives Takenfrom 2015-18

Total investment made in last three years -148.43 Crores

Sl. No

Title of Project

Annual Electrical

(Million kWh/MT Coal)

Total Annual Savings

(Rs. lakhs)

Investment Made

(Rs Lakhs)

Co2 Reduction

MT

No Investment

1Modification of Unit-3 Cooler fan-8,9 suctionsilencers

0.16 8.3 0 166

2 Modification of Unit-3 Cooler fan-2 outlet duct 0.05 2.3 0 48

3Reduced pressure drop across cement mills CAfan damper

0.25 12.3 0 252

4Avoided damper loss across Cooler ESP fan(Line 3)

0.05 2.6 0 53

5Reduced Pressure Drop across Damper in RABHfan (Line-3)

0.15 7.4 0 150

6 Avoided compressed air leakage in the plant 0.48 24 0 480

7Optimization of Unit-2&3 RABH RAL on/off toreduce power consumption

0.1 4.7 0 96

Investment

8Modified the Unit-3 preheater fan inlet duct toreduce pressure drop.

0.4 4 3 396

9 VFD for Coal mill-3 Booster fan 0.14 6.1 3 140

10 VFD for Unit-1 RABH RA fan 0.03 2.2 3 34

Energy saving projects implemented during 2015-16

Sl. No

Title of Project

Annual Electrical

(Million kWh/MT Coal)

Total Annual Savings

(Rs. lakhs)

Investment Made

(Rs Lakhs)

Co2 Reduction

MT

Investment

11Optimization of Coal firing blowers volume –Kiln & PC in (Line-1)

0.08 4 0.1 76

12Optimization the operation of packing plantbag filter

0.11 5.4 0.6 111

13Avoided damper loss across identifiedauxiliary bag filter- Raw mill section

0.03 1.2 0.5 25

14Avoided pressure drop across identifiedauxiliary bag filter- Kiln section

0.03 1.2 0.5 25

15Lighting circuit distributed and separateswitch provided for minimum lighting ,whennot in use.

0.05 2.6 0.9 53

16141no's of 70w HPSV lamps are replaced with35w LED lights in critical areas

0.03 1.4 6.2 29

17Thermal savings with Increase of PH Topcyclone efficiency and reduce the Dust lossfrom Pre-heater system (Line-2)

437 17 100 795

18Kiln-1 inlet riser duct modified to reducepressure drop.

0.48 23.2 100 475

19Avoided damper loss across auxiliary bagfilter- kiln section

0.04 1.9 1.5 40

Energy saving projects implemented during 2015-16

Energy saving projects implemented during 2016-17

Sl. No

Title of Project

Annual Electrical

(Million kWh/MT of coal)

Total Annual Savings

(Rs. lakhs)

Investment Made

(Rs Lakhs)

Co2 Reduction

MT

No Investment

1Convert identified Motors From delta to starConnection

0.03 1.6 0 33

2Reduced pressure drop across silencer incooler fan no 6 in line-2

0.11 5.5 0 113

3Avoided Bag filter pressure drop acrossauxiliary Bag Filter- Cement mill section

0.025 1.2 0 25

4Mill vent BF product diverted to final productin CM-2

0.36 17.6 0 360

5Modification VRM-3 Mill feed chute to reducemain drive power

0.195 9.555 0 195

Investment

6 Reduce false air in Pre heater (Line-1) 0.075 4 0.1 75

7 Reduce false air in Raw mill Circuit (Line-1) 0.05 2.3 0.3 47

8 Reduce false air in Raw mill Circuit (Line-3) 0.0325 1.6 0.3 32.5

Energy saving projects implemented during 2016-17

Sl. No

Title of Project

Annual Electrical

(Million kWh/MT Coal)

Total Annual Savings

(Rs. lakhs)

Investment Made

(Rs Lakhs)

Co2 Reduction

MT

Investment

9Optimize cooler loss in line-3 by modifyingStatic and 1st grate of the cooler

2887 172.27 606 6593

10Optimize Lighting Voltage in Plant byproviding energy savers

0.02 1 1.58 20.76

11 Replaced Identified Faulty Capacitors 0.028 1.4 1.27 28

12 Replaced HPSV/MV lamps with LEDs 0.04 1.7 7.5 35

13Turbo Blower installed in Unit-3 kilnprimary air to reduce primary air %.

0.396 19.404 50 396

14Vrm-3 Recirculation modified to increase %of recirculation air

0.3465 16.9785 5 346.5

15Installed waste heat recovery system 12.5MW

87.5 4375 14000 87500

Energy saving projects implemented during 2017-18

Sl. No

Title of Project

Annual Electrical

(Million kWh/MT Coal)

Total Annual Savings

(Rs. lakhs)

Investment Made

(Rs Lakhs)

Co2 Reduction

MT

No Investment

1Increased the OFF time of RABH RAL's in kiln-1,2,3 to reduce power consumption

0.03 1.58 0 32

2Reduced pressure drop across the damper inClinker Extraction Bag Filter Fan by interchangechange fan and motor pulley

0.06 3.00 0 60

3Unit-2 RABH DP intervals optimized to reduceRABH fan power consumption

0.24 11.88 0 238

4Air lift system installed in place of Pneumaticpump system for cement bag branding toavoid packer stoppages

0.05 2.5 0 50

Investment

5Reduce pressure drop across the damper in U-3LS crusher bag filter fan(VFD provided)

0.10 4.86 4 97.2

6Reduce pressure drop across the damper inCM-1A Extraction Bag Filter fan by reducing fanRPM reduced from 1920 to 1450

0.02 0.9 0.05 18

7Excess venting reduced in unit-3 swirl airblower

0.02 1.19 0.05 24

Energy saving projects implemented during 2017-18

Sl. No

Title of Project

Annual Electrical

(Million kWh/MT Coal)

Total Annual Savings

(Rs. lakhs)

Investment Made

(Rs Lakhs)

Co2 Reduction

MT

Investment

8Avoided higher capacity Compressor (GA-75) forbulk loading operation by providing airline fromother compressor

0.05 2.25 0.05 45

950 No's of 70w HPSV lamps are replaced with 35wLED lights in critical area

0.00875 0.44 1.8 9

10150 no's 36 watts tube lights replaced with 18WLED tube lights

0.0144 0.72 1.26 14

11Reduced pressure drop across the damper in CM-4hopper top bag filter fan (VFD provided)

0.12 6 1.75 120

12Reduced false air in Cement mill-2 by providingnew expansion joints and arrested cycloneleakages

0.15 7.5 0.2 150

13 CM silo -2 areation blower volume optimization 0.0030 0.15 0.1 3

14 Reduced pressure drop cross coal mill-3 outlet duct 0.10 4.95 1.6 99

15Installed new TAD damper in Kiln-1 to reduce falseair entry

132.00 7.92 10 264.95

16Modification of kiln feed bag filter ducting and eliminate one bag filter

0.04 1.98 0.2 40

Specific thermal energy Consumption Reduction Kcal/Kg Clinker

Power consumption up to clinkerisationkWh/Ton of clinker

Energy Performance in Last 3 Years

2015-16 2016-17 2017-18

718.2

710.8

713.0

2015-16 2016-17 2017-18

49.5

47.747.9

Remarks: In 2017-18 kiln-1 is running continuously compared to 2016-17(Kiln -1 Power & Fuel Consumption high due to 5stage PH)

Reduction of Specific Power ConsumptionkWh/Ton of Cement

Energy Performance in Last 3 Years

2015-16 2016-17 2017-18

79.35 78.76 78.48

32.228.9

25.1

SEC per Ton of Cement %PPC Production

Benchmarking with National Performance

Benchmarking with National Performance

Top 10 plants MHIPL-Line-1,2,3

65.20

78.48

Overall Electrical SEC kWh/Ton of Cement

Top 10 plants

MHIPL

703

713.0Thermal Energy kCal/kg Clinker

Energy benchmarking for Cement Industry 2018 Version 3.0

Top10 MCW Line-1,2,3

49.20

47.90

Electrical SEC. Up to Clinkerisation kWh/Ton of Clinker

Electrical SEC. Up to Clinkerisation kWh/Ton of Clinker

NATIONAL BENCH MARKING

Energy benchmarking for Cement Industry 2018 Version 3.0

Top10 MCW Line-1 MCW Line-2 MCW Line-3 MCW Line-1,2,3

49.20

52.68

43.95

49.0047.90

NATIONAL BENCH MARKING Specific Heat Consumption kCal/kg Clinker

Top10 MCWLine-2

MCWLine-3

678

709708

Thermal SEC in 6 Stage Preheater(kcal/kg clinker)

Top10 MCW Line-1

721

731

Thermal SEC in 5 Stage Preheater(kcal/kg clinker)

Energy benchmarking for Cement Industry 2018 Version 3.0

National Benchmarking

Sr.No Section Electrical Energy Consumption(kWh/MT Material)

Bench Mark Unit-1Achieved

Unit-2Achieved

Unit-3Achieved

1 Raw mill 11.10 11.52 10.48 12.97

Raw mill-2 Electrical SEC is Lower than the National Bench marking.

Energy benchmarking for Cement Industry 2018 Version 3.0

Sl.No

Proposed Major Energy Saving projects(2018-2021)

Investment Rs. Lakhs

Saving Kw/hr(or)

kcal/kgclinker

Co2 Reduction

Tons/Annum

1Install new high efficiency fan for line 1PH fan

50 60 kW/hr 848

2Increase the Efficiency of PH Top cycloneand reduce the Dust loss from Pre-heatersystem (Line-1)

2005

kcal/kgclinker1256

3Improve heat transfer in identified pre-heater cyclone (Line-1)

3505

kcal/kgclinker1250

4Increase the Efficiency of PH Top cycloneand reduce the Dust loss from Pre-heatersystem (Line-3)

2002

kcal/kgclinker 880

5Replacement of shell cooling fan bladeswith FRP(Fiber Re-enforced plastic)blades

14 30 kW/hr 163

6Replacement of 1000 No’s HPSV lampswith LED lights

30 35 kW/hr 153

Road map to achieve National benchmark

Observation :❖ High pressure drop across the coal mill-3 outlet duct.

Analysis:❖ Inadequate Mill outlet duct area (OEM Design)❖ High pressure drop across the mill outlet duct (60 mmwg)

Action taken:❖ Mill outlet duct modified with In-house design

Parameter Units Before After

Mill outlet

pressure

mmwc -340 -290

Fan power Kw/hr 210 195

Savings Rs-Lakhs/Annum 4.0

Project: Reduction of power consumption in Coal mill-3

Case Study-1

Benefits:

Project: Reduction of power consumption in Coal mill-3

Case Study-1

Before After

Observation:

RABH fan power high

Analysis:

The power consumption of the bag housefan is varying significantly during differentoperating conditions like direct mode andcompound operation.

Project: Reduction of Specific power consumption in Unit-2 RABH fan

Case Study-2

Operating condition

DP RABH fan Power

Compound Mode 100-110 300

Direct Mode 120 314

Action taken :➢ Operate with different RABH DP settings of – 90 mmWC, – 100

mmWC, –110 mmWC by increase the reverse-air fan flow rate, whichwill reduce the DP across the bag house.

➢ Monitor the total power consumption of the BH fan and RA fan.➢ Optimized the operation of reverse air fan based on the optimum ‘DP’

across the bag house and Fix the ‘DP’ setting, which gives the lowesttotal power consumption.

➢ Bag house DP settings changed from 120-100 to 110-90 mmwc.

Benefits Achieved:Power saving -30 kW/hrAnnual saving -10.80 Lakhs/Annum

Project: Reduction of Specific power consumption in RABH fan

Case Study-2

Project: Optimization of Unit-1,2&3 RABH RAL’s

Observation:❖ After commissioning of WHR project ,

as per observation dust collection inRABH-1,RABH-2,RABH-3 is reduceddrastically.

Action taken:❖ Increased the off time interval from

30 min to 45 min.❖ As a precautionary measure continue

running of RAL given whenever anyhopper high level sensor acts.

Benefits Achieved:Total saving per day – 97 kWh/DayPower saving:Rs.1.60 Lakhs/annum

Case Study-3

Observation:❖ Two separate bag filters in operation

for kiln feed bin & kiln feed solid flowmeter.

Analysis:❖ Both the bag filters operating with

50% damper causing power loss.

Action taken :❖ Modified the ducting and avoided

one bag filter totally.

Benefits:❖ One bag filter totally stopped.❖ Power saving -5 kW/hr

Project: Modification of kiln feed bag filter ducting

Case Study-4

Project: Reduction of Power consumption in packing plant

Observation:❖ Packer stoppages due to Failure of cement bag branding machine pump

Analysis:❖ Frequent failure of piston & O-rings.

Action taken :❖ Air lift system installed in place of Pneumatic pump system

Benefits:❖ No packer stoppages due to bag branding machine pump problem.❖ Power saving-5 kW/hr

Case Study-5

v v

INK

PRINT HEAD

PUMP

BELTCONVEYOR

Problem area

AIR + INK

COMPRESSED AIR

FRL

INK CONTAINER

OPERATION OF BRANDING MACHINE

DRYER

INK

PRINT HEAD

BELTCONVEYOR

AIR + INKCOMPRESSED AIR (15 PSI)

FRL

OPERATION OF AIR LIFT SYSTEM (BOTTLE SYSTEM)

Compressed air goes to the ink Bottle. Due to air pressure acting on ink, the ink moves to print head through pipe line for printing.

INK BOTTLE

DRYER

RENEWABLE ENERGY SOURCES

Solar Plant

Sl.No Capacity Annual kWh Generation % Consumption

1 1.2 MW 18.43 Lakhs 0.86%

2 12.7Kw 4148 (5Months) ---

RENEWABLE ENERGY SOURCES

12 Kwp Solar Plant at Mines (Nov-17)1.2 MW Solar Plant

RENEWABLE ENERGY SOURCES2x 500 LPD ROOF TOP SOLAR HEATER AT GUEST HOUSE

Commissioned in Nov-2016 -(Units saved @3000Units/Annum)

RENEWABLE ENERGY SOURCES SOLAR FENCING AT MINES MAGZINE

Solar Fencing

Waste Management System

Waste Management System

❖ Well developed technology steps like Waste Heat Recovery power plant (12.5MW) incorporated in process.

❖ Usage of alternative fuels (pharmaceutical waste) 1.90 % (TSR) in kiln’s to reduce usage of natural resources.

❖ Fly ash addition in cement is 30.8%

❖ Slag addition in raw meal is 0.57%

❖ Fly ash addition in raw meal is 0.59%

❖ Shale consumption in raw meal is 0.36%

❖ Internally generated wastes like cotton waste , waste bags, grease are also being fired in kiln.

❖ STP water (200 KLD) is being used for plantation .

WHR system Installation at MHIPL

❖MHIPL-MCW installed and commissioned 12.5MW Waste Heat RecoverySystem in Jan’2017 with a capital expenditure of about Rs 140 croresand started utilizing waste heat from preheater and cooler of all thelines for power generation.

❖ Waste Heat Recovery System was installed by M/s LNVT/SINOMAEnergy Conservation Ltd and achieving PLF of 85% an average.

Suspension Preheater Boiler Air-Quenching Boiler (AQC) Turbine -Generator

WHRPP – 12.5MW

CO2 Emission reduced by 75440 MT/Annum in 2017-18

Fool proof AFR firing system for firing hazardous waste in kilns with the

technological support from FLSmidth,Denmark.

Utilization of AFR Consumption for Pyro Processing

Scrubber system for odour control

2015-16 2016-17 2017-18

2.48 2.58

1.9

Alternative Fuels (TSR)%

*In 2017-18 low TSR % due to non availability of solvent with specified quality .

Utilization of AFR Consumption for Pyro Processing

GHG INVENTORISATIONCo2 (Kg Co2/Ton of clinker)

GHG reduction due to Encon Projects,Installation of 12.5 MW WHR,and Thermal saving in Unit-3 Cooler upgradation.

2015-16 2016-17 2017-18

1087

1024

937

GHG Emission Reduction

YearScope-1

emissionsScope-2

emissionsScope-3

emissions TotalKg Co2/MT of Clinker

2015-16 1080.70 0.78 5.65 1087

2016-17 1013.87 3.64 6.37 1024

2017-18 929.40 0.77 7.21 937

Scope Emission Sources Considered

Scope 1 EmissionsCement process-Calcination, Fuel Burning in Kiln & HAG, CPP -Coal Consumption etc.

Scope 2 Emissions Electricity Consumption from Grid

Scope 3 EmissionsRaw material Transport, Cement dispatch through rail & Road, Employee commute etc.

Best Practices Implemented on Energy front inGreen Supply Chain

Best Practices Implemented on Energy front inGreen Supply Chain

❖ Training critical vendors on green initiatives like waterconservation, wastage and energy Consumption.

❖ Visual aids-training for better understanding on greeninitiatives.

❖ Display of posters-on shop floor for better understanding andto create the awareness in every individual.

❖ Recognition letters shall be issued to the vendors afterassessment on environmental performance by the end ofMarch every Year as a part of encouragement.

❖ Emphasizing on rail/bulk transportation for inward andoutward transportations to continual improvement ofenvironment performance.

Best Practices Implemented on Energy front inGreen Supply Chain

➢ Rain harvesting pit -1 No. constructedby Padmaja Poly Packs Pvt Ltd.

Rain harvesting pit details:

Size: 3000mmx2000x2000mm

➢ M/s Webber India, Coimbatore,one of major supplier for supply ofcastings principally agreed to applyfor ISO 14001 previously andreceived the certification recently.

❖ M/s Neo Techniques, Secunderabad is authorized dealer for AtlasCopco compressors, Kluber lubricants, Asco pneumatic and Shantigears etc.,

➢ After completion of the training, M/s Neo Techniques, Secunderabadreplaced their existing conventional lighting system with LED lightsconsidering environmental benefits and energy savings.

Best Practices implemented on energy front inGreen Supply Chain

Saving : 143 Units /Month

Before After

530

387

Energy Consumption (KWh)

Director (Technical) /Sr. President (Operations)

Unit Head

DGM

(QC)

GM (E&I)

Sr.DGM(OP)

V.P

(CPP)

Sr. DGM

(Mech)

GM

(Mines)

Energy Management Team

Section Heads

Energy ManagerSr.GM (O&M)

Online Energy Monitoring❖ Energy Management System is

developed to monitor and controlthe consumption of various formsof energy through an effectiveenergy management system

❖ Discussion on Variances againstthe target during DailyCoordination Meeting

❖Monthly review by EnergyConservation cell

❖Monthly review by TopManagement for actions

❖ Energy Audits Once in 3 years byrecognized External Agency

Energy performance Review Methodology

Energy Projects Implementation Methodology

❖ Identifying the potential Energy saving equipment's /Areas by Plant Engineers.

❖ Data collection , shop floor involvement, brain storming , energy audit

❖ Categorized into No investment, Low investment and High investment.

❖ Categorized into Short term, Medium term and Long term.

❖ No / Low investment project Implementation - Immediately.

❖ High investment projects proposals – Put up for CAPEX approval.

❖ Approved Proposals are being Implemented with time frame.

❖ Review of project implementation ,Completion status and HOTO.

❖ Reporting the benefits / savings through monitoring and reviewing theperformance.

Strategies Adopted for Employee Involvement

❖ Trainings for Employee/Contract work man- 16 Training hours

❖ Participation in Seminars LAUNCHING QUALITY CIRCLE

❖ Quality circle – 21 Circles

❖ Kaizen

❖ Knowledge share through live demos

❖ Energy conservation Day Celebrations

❖ CSI Member company

❖ BEE- KEP SGA

QUALITY CIRCLE TRAINING

❖ The two days training and capacity building

workshop was organized at My Home

Industries Limited, Mellacheruvu Plant on

13th – 17th June, 2017 under KEP-SPARC

(Service package for advancing resource

conservation) membership.

❖ SGA Group are formed to identify and

implement appropriate solutions within their

area of operation to achieve energy efficiency,

higher productivity, zero defects, zero

breakdown and zero waste.

Strategies Adopted for Employee Involvement

MCW has undertaken the Capacity build-up project and Small Group Activity (SGA) under KEP – SPARC membership by forming 9 groups

.

SPARC -SGA TEAMS

Sr.No TEAM NAME TARGET

1 FARADAY 50 KW/HR

2 SPARKS 50 KW/HR

3MAHA ENERGY

SAVERS30 KW /HR + 2K.CAL/KG

4ENGRGY EXPERTS

30 KW/HR

5 POWER PILOTS 30 KW/HR

6 POWER SAVING 30 KW/HR

7ENERGY SAVING

ACTION30 KW/HR

8 SEE60 KW/HR +5K.Cal/Kg.

9 MAHA VGU 65Kw/Hr

Target from 9 Groups :375 kW and 7 kcal/kg clinker

Achieved Saving : 145 kW

Conducted KEP 2nd ‘’WORK SHOP ON BEST PRACTICES in ENERGY EFFICIENCY’ under Cement Sector on 07&08th June ’16

Internal Training Energy Cell

Awareness program on energy conservation to employees

External trainingTraining for workmen's

Implementation of ISO 50001/Green Co

CERTIFICATION OF ISO 50001

Total investment made in last three years -148.43 Crores

WON “ GOLD AWARD” IN CII GREENCO SUMMIT– PUNE IN 2017

Green Co rating 2016 – Gold Rating

17th National Award for Energy Efficiency from CII in Hyderabad in August 2016

18th National Award for Excellent Energy Efficient Unit from CII in Hyderabad in Sep 2017

Best QC Supporting Management Award received on 12th September from Home Minister, Telangana. Awarded by CCQC

Quality Circle Awards - 04 Gold Rating from Hyderabad Chapter – 13th Sep’ 17

Par Excellence 3 no’s and Excellence award 1 no received at NCQC ,

Mysore on 05.12.2017 two case stidies on safety innovations in Mines

PATH FORWARD TO BEST PRACTICES

Green Co rating – Platinum

Energy Saving projects implementation by SGA teams under KEP-SPARC

PAT-2 Cycle target Achievement

Increase of AFR to achieve 5% TSR

Development of Biodiversity Park

Aim to participate in QC International convention