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Copyright 2013 by CH2M HILL, Inc. • Company Confidential
Lake Gaston Water Treatment Plant Coagulant Change to Aluminum Chlorohydrate (ACH)
AWWA Senior Operators ForumAlex Echols, Chesapeake Public Utilities Doug Noffsinger, P.E., CH2M HILLOctober 9, 2014
Copyright 2013 by CH2M HILL, Inc. • Company Confidential
What are we talking about?
We will present our approach to troubleshooting a submerged-type membrane process durability problem Review the overall water system Review the plant process flow stream Discuss the key role that coagulant addition plays in the
process Discuss the approach to improve membrane durability
– Reduce effects of abrasion and membrane strand motion– Identify and implement an alternative coagulant to allow less mixing
energy (reduced membrane strand movement) Discuss the approach to identifying an alternative coagulant Discuss the full-scale implementation of the selected alternative
coagulant and results to date
City of Chesapeake Water System Background
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Water System Background
City of Chesapeake Department of Utilities Description Southeastern, Virginia City of 233,000 population Water System Summary
– 63,136 customers treating about 18 MGD– 2 WTPs
• Northwest River WTP – 10 MGD capacity treating both Northwest River surface water and brackish groundwater. Uses conventional process followed by reverse osmosis (RO) membranes and groundwater treatment with RO membranes as well
• Lake Gaston WTP - 8 MGD capacity treating Norfolk Western reservoir water supplemented by aquifer storage and recovery (ASR). Uses unique submerged membrane process.
– 832 miles of distribution pipe– Purchase water from Norfolk and Portsmouth as well
Copyright 2013 by CH2M HILL, Inc. • Company Confidential
Copyright 2013 by CH2M HILL, Inc. • Company Confidential
Water Service Systems
Lake Gaston Water Treatment Plant
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Lake Gaston Water Treatment Plant
City Council OK’s moving forward – November 2000 Five components of the project:
– Water Treatment Plant– Pipeline on Military Highway– Pipeline on Jolliff Road– Intake Structure on
In-town Lakes– Tank and Pump
Station on JolliffRoad
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Lake Gaston Water Treatment Plant Process Flow Stream
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Lake Gaston Water Treatment Plant Process Flow Stream
Air
PermeatePump
Reject
Treated Water
FlocculationManganese Contactor/Disinfection
Raw Water
Coagulant
RapidMix
10
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Lake Gaston Water Treatment Plant
Capacity:– 8 mgd for 4 trains (2 mgd/train); 7.6 mgd at 95% recovery– 6 mgd for 3 trains (2 mgd/train); 5.7 mgd at 95% recovery
Unit Processes– Rapid Mix:
• Raw Water Strainer• In-Line Rapid Mix
– Flocculation Basins• Two Stage Basin• Flocculation Mixer
– Membrane Basins• Number of active Basins: 4• Membranes: Immersed hollow-fiber ultrafiltration
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Lake Gaston Water Treatment Plant
Unit Processes (Continued)– Manganese Contact Filters (adsorbers)– Disinfection Pipeline– Gravity Thickener– Centrifuge Dewatering– 2 MG Finished Water Storage Tank– Chemical Feed
• Ferric Chloride - coagulant• Polymer – coagulant aid (for thickening and dewatering)• Sodium Hydroxide – pH and alkalinity control• Citric Acid – membrane cleaning agent• Sodium Hypochlorite – Primary disinfectant• Ammonia – Secondary (residual) disinfectant additive (formation of
combined chlorine by reaction with free chlorine)
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Production Flow Backpulse Flow
Submerged Membrane Ultrafiltration (UF) ProcessOperation
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Production Flow
Air Line
Permeate Header
500d Cassettes
Reject
Ultrafiltration Operation
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Coagulant Addition at the Lake Gaston WTP
Coagulant addition plays a key role in water treatment at Lake Gaston WTP– The only part of the process that removes dissolved organic material
which is the key to minimizing disinfection by-product (DBP) formation– Works at relatively low pH (high 5’s and low 6’s) to achieve maximum
organic removal without producing significant dissolved iron– Acidic nature helps depress pH to meet low pH coagulation goal
Initial coagulant selection was Ferric Chloride (FECL3) based on pilot scale testing – FECL3 achieved DBP goals– Confirmed that clarification process could be omitted– Did not exhibit negative material effects on membranes during testing
Approach to Improve Membrane Durability
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Membrane Durability Problems
Since the start of operations in 2005, membrane durability has not met expectations (5-10 year service life)– Membranes are designed to achieve primary disinfection of protozoa
and most bacteria through particle removal– High rate of membrane failure reduced the required removal
performance measured as a Log Removal Value (LRV) of 3.– Membranes needed replacement on a 2-3 year basis to avoid non-
compliance with LRV requirements. Evaluation Results
– Abrasion and/or material fatigue appears to be the cause of reduced membrane durability
– The abrasion effects may be reduced with lower applied mixing energy – A change to an alternative coagulant may be beneficial in support of
reduced mixing energy operation
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Identification of an Alternative Coagulant
Coagulant Selection Goals: Water Quality Compliance
– Keep THM/HAAs at or below existing levels– Keep lead & copper below the Action Level– Keep NPDES discharge non-toxic– Keep residuals (sludge) aluminum leachate at
acceptable levels. Process
– Reduced floc size for better performance in membrane basin (reduced mixing energy)
– Gravity thicken well and produce a low-solids overflow (decant)
– Produce less solids– Operate at a higher pH
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Alternative Coagulant Testing Approach
Testing Objective Evaluate candidate coagulants for DOC reduction performance Full-scale testing of the coagulant that may achieve both DBP
compliance and an increase in membrane life.Evaluation Program Framework Step 1 – Desk-top coagulant screening Step 2 – Jar-test potential coagulants to determine DOC reduction Step 3 – Confirm DBP control performance of the selected
coagulant identified in Step 2 using a laboratory simulation of the plant and distribution system
Step 4 – Full(plant)-scale implementation of the selected coagulant to confirm the above and determine adjustments needed for long-term operation
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Step 1 – Alternative Coagulant Screening ApproachCriterion Discussion
A benchmark coagulant must be selected for comparison of alternatives
Ferric chloride (FeCl3) is currently used and was selected as the benchmark comparison coagulant.
An alternative coagulant must be selected that:
• Is approved for potable use.
• Meets or exceeds current DBP formation potential performance.
• Does not coat or foul the submerged membranes.
• Produces a “pin” floc.
• Does not produce undesirable by-products, such as high soluble metals or negative impacts on residuals operations.
Coagulants with relatively high unit-cationic charge density are considered to be the best candidates for DBP control.
The more likely coagulant candidates to meet the criteria were thought to be aluminum-based.
Therefore, products that contain aluminum oxide contents equivalent to the typical aluminum sulfate solution (alum) were tested.
Alum was also tested as a benchmark for comparison.
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Step 2 – Coagulant Jar Testing
Four alternative coagulants were identified as good candidates for consideration based on dissolved UV 254 adsorbance and dissolved organic carbon (DOC) removal:
– 2 poly-aluminum chloride (PACL) products – Aluminum chloride– Aluminum chlorohydrate (ACH)
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Step 3 – Lab Simulated Distribution System Testing
Simulated Distribution System lab scale testing for DBP levels
– Simulated free chlorine contact time – Quenched free chlorine residual using ammonia at a dosage that
simulated plant effluent residual chloramine levels.– Held the chloraminated sample for a time period equivalent to the
Locational Running Annual Average (LRAA) “High TTHM” sampling site travel time period (approximately 23 hours)
– Simulated sample site pH as well
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Step 3 – Simulated Distribution System DBP Testing Results
0
10
20
30
40
50
60
70
80
0 12 24 36 48 60 72 84 96 108 120
Tota
l TH
M (u
g/L)
Time (hrs)
THM Formation
Jar Test 1 - Ferric Chloride
Jar Test 2 - DelPAC XG (ACH)
Jar Test 3 - Aluminum Chloride
Jar Test 4 - DelPAC 1525
Jar Test 5 - DelPAC 2950
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Step 3 – Simulated Distribution System DBP Testing Results
A few interesting things to note from lab THM testing:
– All coagulants produced DBP results in compliance with the LRAA DBP limits of 80 μg/L for THMs and 60 μg/L HAA5 respectively.
– While there is some relative variation in the observed DBP levels for each alternative coagulant treatment regimen, the differences are very minor and can be understood to be effectively equivalent in performance.
– The data confirm that even though ammonia is added to “quench” the effect of free chlorine on DBP formation, formation of DBPs continue to some extent.
– The laboratory-scale SDS testing data is consistent with observed full-scale, real-time results experienced during water delivery operations.
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Step 3 – Lab Testing Summary Information
Coagulant
Coagulant Test Dosage
Test Dosage SDS LRAATHM Level
Approx. Chemical Unit Cost
Est. Cost/ MG
Unit Sludge Production Factor
Estimated Unit Sludge Production
mg/L μg/L $/lb. $/MG mg/mg lbs./MG
Ferric Chloride(FECL3) 17 23.64 $0.23 $33 0.66 94
Aluminum Chloride 65 22.52 $0.35 $190 0.21 115
Aluminum Chlorohydrate(DelPAC XG) (ACH)
38 22.20 $0.25 $79 0.36 114
PolyaluminumChloride(DelPAC 2950)
62 21.26 $0.23 $119 0.27 141
PolyaluminumChloride(DelPAC 1525)
64 18.44 $0.16 $85 0.17 88
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Step 3 – Lab Testing Summary Information
The data indicates that a change in coagulant can achieve the same DBP control performance as the current coagulant.
A change to one of the alternative coagulants will double the unit treatment cost for coagulant addition. However, the coagulant may not require as much (or any) addition of sodium hydroxide for pH control.
The lowest cost alternative coagulants were aluminum chlorohydrate (ACH) and a poly-aluminum product (PACL).
The relative dosages and calculated sludge production impacts are essentially equivalent due to the complexity and nature of the reactions involved and the methods used for residuals production estimation.
The use of ACH is common at similar membrane installations. The DBP, cost performance, and sludge production results indicate no barrier for potential use at the LGWTP.
Therefore, ACH was recommended for full-scale testing
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Step 4 – Full-Scale Coagulant Testing
Full Scale test– Why: To evaluate coagulant under actual Plant and distribution system
conditions and determine:• UV254, TOC removal, and distribution system DBP control.• Operational effects/impacts such as membrane LRV, fiber effects, TMP, and
fouling• Solids production, impact on thickener, impact on DEQ discharge permit,
etc.• Process adjustments such as chemical dosages, pH levels, etc.
– How:• Duration: 12 months• Develop plant operational scheme to accommodate the use of ACH• Obtain VDH approval• Obtain DEQ NPDES and VPA approval
ACH Full Scale Implementation
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Key Implementation Actions
Prepared Summary Reports for Regulatory Approval
Virginia Department of Health – Drinking Water Quality– Alternative Coagulant and Test Plan Approval– Requirement to perform full-scale lead and
copper compliance monitoring Department of Environmental Quality –
Surface Water Discharge and Residuals Disposal Monitoring– Acute and chronic toxicity testing of thickener
overflow (decant) and NPDES permit compliance confirmation
– Residuals dewatered cake testing for aluminum and other metals
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Key Implementation Actions
Plant facilities preparation– Chemical systems prep –
storage tanks and feed pumps– Process tankage draining and
purging of FECL3 floc– Turn-down of mixing blowers
and durations
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ACH Conversion
ACH conversion occurred on June 15, 2014 Operational Actions:
– Current polymer works well with thickener and centrifuge– Maintaining thickener Depth of Blanket (DOB) between 5 to 10 feet – looking good– Perform normal routine membrane operation:
• Perform routine Pressure Integrity (PIT) Tests – looking good• Perform routine Clean In Place (CIP) actions – looking good• Log Reduction Value (LRV) calculations – looking good• Few fiber repairs needed to date
Monitoring Actions:– Inspecting solids accumulation in fibers– Monitor thickener performance– VDH: Performing Lead and Copper testing in accordance with VDH test approval
conditions– VPDES: Performing testing of Gravity Thickener Overflow for chronic toxicity and
aluminum– VPA: Perform additional aluminum testing of LGWTP residuals, NWRWTP
residuals, and combined residuals
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Results to Date
Much improved LRV performance– High initial LRVs– LRV values are maintained – very little reduction
DBP levels are equal to or less than FECL3 Has drastically reduced membrane strand repairs Lower energy operation does not produce any process or
maintenance issues Thickener performance drastically improved (unexpected!) Dewatering performance appears to be equal to or better than
FECL3 All other regulatory testing to date appears to indicate compliance
requirements are being met City is considering using ACH at the NWR WTP
Discussion