high voltage studies, 10/06 – 02/07 j. long, indiana university system modifications conditioning...
TRANSCRIPT
High Voltage Studies, 10/06 – 02/07
J. Long, Indiana University
System Modifications
Conditioning tests
Amplification, leakage current (preliminary)
Future plans
HV System - Changes Made for 10/06 run
Control purity and surface contaminants systematically
Complete solvent cleaning of interior
RF Plasma discharge cleaner (for Hydrocarbons)
Dry pumps only for all applications
No LN2 pre-cooling: use cold, filtered He gas from LHe supply dewar
LN2 trap on LHe bath pumping line
LHe (and gas) filter on transfer line outlet
Charcoal backed by glass filter paper, Quantum Technologies
RGA monitoring
Further reduced surface roughness
Electrodes polished to ~ 8 -inch finish
Attempt conditioning of electrodes at small gaps in vacuum
Changes made for 10/06 run
Attempt operation below 1.8K
Colder LHe transfers
New transfer line operates with HV system below lambda point
Heat load reductions (also important for eventual operation with DR):
Tie central volume lateral support posts to 77 K
Tie supply cryostat upper neck to 77 K shield
Remove all unnecessary (conducting) instrumentation from supply cryostat upper neck
Cover open viewport holes in 77 K shield with quartz windows
Tie actuator rods to 77 K shield
Previous heat load 2 W
1 W
0.5 W
0.1 W
0.1 W
0.02 W
Other
Video monitoring of gap
Improved level sensing
Changes made for 12/06, 02/07 runs
Replaced LHe filter with simpler home-made model
5/16” OD tube on end of stinger packed with copper wool
No copper residue observed in leak tests
Did not attempt conditioning in vacuum
Reduces LHe flowrate by factor ~2 relative to open stinger
Replaced “temporary” smooth G-10 insulators with custom ribbed ceramic
10/06 results likely limited by severe pitting on electrodes
Also slight contamination of charcoal leaking from filter
Dismounted, re-polished electrodes to #16 finish
12/06 data limited to single amplification/ leakage current test after moveable ground electrode broke off its support
Combination of thermal shrinkage, embrittlement, slight anti-parallelism and misalignment of electrodes – shear force on screws during electrode contact enough to break (?)
Plastic screws holding electrode to support broke at heads
Cryogenic performance
Heat load (all runs)
Unchanged
Copper “77 K” radiation shield rarely cools below 120 K
Pre-cooling (all runs)
(boil-off still 50 l/min He gas at 18 C, or 0.1 g/s and 2.5 W)
Cooling below lambda point (10/06 run only)
System cools to 4 K at steady ~ 15 K/hr with 400 l/minute of cold gas flow
400-500 l LHe used
Insufficient flow rate for low-pressure LHe top-off
Reduced conductance of stinger with filter
System reached 3.4 torr (1.5 K) with existing pumps while 40% full of LHe
Vacuum Conditioning tests - 10/06
Time since start of
training (min)
Breakdown voltage
(kV)
5 -31.0
10 -30.6
15 -31.9
20 -27.0
44 -33.27
50 -33.00
74 -33.41
116 -33.61
129 -33.47
145 -33.55
151 -33.28
193 -33.96
Ramped ~ 10V/s for final 2-3 kV
Monitored current across gap and insulators (by eye)
Waited for current surges (~ microamps) to subside before proceeding higher (usually 10-60 s)
4 mm gap, P = 2E-6 torr
Time since start of training
(min)
Breakdown
voltage (kV)
10 28.6
20 32.3
24 27.2
26 25.2
32 28.0
54 31.3
79 28.5
81 26.0
92 28.2
Damage during final runs with V < 0 ?
Vacuum Conditioning tests - 10/06
Ramped in 10V steps
Recorded all current surges across gap and insulators
Waited for current surges to return to (within few % of) resting current
4 mm gap, P = 2E-6 torr
Ground electrode surges Insulator surges
No obvious breakdown precursor event
LHe Conditioning tests - 10/06
Ramped in 10 V steps for final 2-3 kV
Recorded all current surges across gap and insulators AND resting current
Waited for current surges to return to (within few % of) resting current
3 mm gap, P = 890 torr (could charge 4mm to ~ 50 kV)
Ground electrode surgesTime since
start of training (min)
Breakdown voltage
(kV)
10 33.2
20 36.7
70 34.7
270 34.4
Absence of trend unusual
Maxima plotted only, “surges” usually several minutes
LHe Conditioning tests - 10/06
Trend in ground electrode resting current – possible breakdown precursor?
0 1000 2000 3000 4000
6 1010
5 1010
4 1010
3 1010
2 1010
1 1010
currentAvs ts
LHe Conditioning tests - 02/07
PC-based DAQ ready
Stop ramp at first clear sign of resting current increase; resume only after recovery of several minutes
0 1000 2000 3000 4000
34
33
32
31
mean VkVvs ts, with cuts
0.0
-0.2
-0.4
-0.6
Current (nA) vs time (s)
-30
-32
-34
Voltage (kV) vs time (s)
0 1 2 3 43 1010
2.5 1010
2 1010
1.5 1010
1 1010
5 1011
currentAvs VkV
0 1000 2000 3000 4000
6 1010
5 1010
4 1010
3 1010
2 1010
1 1010
currentAvs ts
LHe Conditioning tests - 02/07
PC-based DAQ ready
Stop ramp at first clear sign of resting current increase; resume only after recovery of several minutes
0 1000 2000 3000 4000
34
33
32
31
mean VkVvs ts, with cuts
0.0
-0.2
-0.4
-0.6
Current (nA) vs time (s)
-30
-32
-34
Voltage (kV) vs time (s)
0.0
-0.1
-0.2
-0.3
Current (nA) vs V (kV)
-30 -31 -32 -33 -34
Amplification tests – 10/06
Six runs with valid data
Breakdown at ~ 2cm gap
Previous record at 890 torr
(Followed by single test with V > 0: + 510 kV)
Could not charge initial gap any further
Mean voltage (~15% error)
V < 0, P = 890 torr, max gap = 7.8 cm
Amplification tests – 10/06
Breakdown at ~ 2cm gap
Previous record at 890 torr
(Followed by single test with V > 0: + 510 kV)
Could not charge initial gap any further
Mean voltage (~12% error) Best mean voltage vs gap
Six runs with valid data
V < 0, P = 890 torr, max gap = 7.8 cm
Pitting and Contamination – 10/06
Ground electrode surface
Area ~ 1 cm2, depth ~ 1 mm
Residue from bottom of LHe volume
(Previous < 1 mm2, microns depth)
Particles with r < 1mm
Filter leaks charcoal into open-neck dewar
CHG
HVPS
50 kV
A C
CHC
CHP
DAQ for 12/06, 02/07 runs
A PA G
Meters on charger, ground electrode, insulator support plate
CHG
HVPS
50 kV
A C
CHC
CHP
HC
HCHG C
QV
DAQ for 12/06, 02/07 runs
• Use SR570 current amplifiers (pA)
• Readout with ADC at 10 Hz
)( dtiQ HCHC
A PA G
Meters on charger, ground electrode, insulator support plate
Amplification tests – 12/06, 02/07
12/06: single run only (broken ground electrode), 4 K
V = (520 ± 60) kV, 5.7 cm gap (ceramic insulators longer, shimmed)
20 30 40 50 60 70 80 90
80
60
40
20
0
20SR570 Output GND PLATE
A PA G
CHARGER
A C
- - - - - - - - - - - -
++ ++++ ++++ ++
A PA G A C
- -
- - - - - - - - - - - -
+++ ++++++ ++++ +
+ i - i - i
A PA G A C
-
- - - -
++ +++
+ i + i
- i
02/07: 15 runs, 4 K:
Happens on all runs when V exceeds ~ ± 150 kV
Current (nA) vs time (s)
Amplification tests – 02/07
Single test without breakdown:
Initial voltage: -7 kV at 5mm gap
Result: V = 121 kV, 5.7 cm gap (amplification factor = 17)
Maximum initial voltage in 02/07 runs: ± 34.5 kV
Theoretical maximum in absence of breakdown: 596 kV (4 K, 5.7 cm)
Record 4K test from 2004, cut off at 5.7 cm: 670 kV
HV – Ground capacitance vs. minimum gap
Ground-HV capacitance saturates below 3 mm
Hair-line gap visible when electrodes in electrical contact
HV or Ground electrode likely skewed ~ 0.5 degrees
Capacitance of initial gap, amplification smaller
Leakage current tests – 12/06
Traditional method: difference between charge as measured from outward and inward strokes, divided by time:
t
Q
C
Ci HC
HC
HVLEAK
= (276 nC – 212 nC) (60.15 pF/ 0.56 pF) = 6870 nC/ 800s
0 200 400 600 8000
2.5 1095 109
7.5 1091 108
1.25 1081.5 108
1.75 108currentAvs times
0 200 400 600 8000
1000
2000
3000
4000
integrated currentnCvs ts
Q = 4370 nC after 800s
Direct monitoring of current through insulators (plate):
Leakage current tests – 12/06
Traditional method: difference between charge as measured from outward and inward strokes, divided by time:
t
Q
C
Ci HC
HC
HVLEAK
= (276 nC – 212 nC) (60.15 pF/ 0.56 pF) = 6870 nC/ 800s
Q = 2206 nC after 800s
Direct monitoring of current through ground electrode:
0 200 400 600 800
8 109
6 109
4 109
2 109
0currentAvs times
0 200 400 600 800
2000
1500
1000
500
0integrated currentnCvs ts
Expect: QG = QHV (CG/CHV)
= 6870 nC (22 pF/60 pF) = 2519 nC
Modified Standoff Design for Acrylic Breakdown Tests
6” long, 2” diameter acrylic tube replaces ceramic
Steel end pieces same dimensions as on ceramic, mimic recesses
Modified Standoff Design for Acrylic Breakdown Tests
Spring-loaded retaining ring holds acrylic annulus in place against slipping from thermal contraction
Schedule
February 19
Acrylic insulators delivered
Coat insulators (?)
Shim electrodes for parallelism
Install insulators
February 19 - March 12
March 12 - 18
Recover 7.8 mm gap
Open system; inspect HV electrode and charger, polish
March 19 -
Next tests
~ July 1
HV insert for dual-use cryostat completed
Expect ~ 1 month dedicated use for initial debug/test
~ 2-3 weeks for any additional test
Acrylic Breakdown Tests
Method 1: Acrylic slab between electrodes
Advantages
Closely match actual perimeter of reference cell design
Reference cell perimeter = 2 (50 cm + 10 cm) = 120 cm
HV test system electrode diameter (flat portion) = 112 cm
Uniform fields > 50 kV/cm possible (for thickness < 1cm)
Inexpensive
Disadvantages
Leakage current monitoring comparable to baseline (pure LHe)
Inexpensive method (clamp and hold slab between electrodes during assembly, operation) not straightforward; long intervention if slab falls
Thickness limited to ~ 1 cm if desire fields > 50 kV/cm
Hollow construction not practical
Acrylic Breakdown Tests
Method 2: Replace ceramic standoffs behind HV electrode with acrylic
Advantages
Poor match of actual perimeter of reference cell designReference cell perimeter = 2 (50 cm + 10 cm) = 120 cm
Total perimeter of standoffs = 44 cm
More expensive (?)
Disadvantages
Hollow construction possible
Leakage current monitoring comparable to baseline (ceramic)
Avoids problems associated with holding objects between electrodes
Much stronger fields (60 kV/cm) available at gaps comparable to reference gap
Mimic electrode recesses without modifying electrodes
Field behind HV electrode less uniform