heat straightening repairs to a steel road bridge
DESCRIPTION
Heat Straightening Repairs to a Steel Road BridgeTRANSCRIPT
Simon K. ClubleyBridge Engineer,Winchester Bridges Group,Mott MacDonald, Winchester, UK
Stephen N. WinterSenior Bridge Engineer,Winchester Bridges Group, MottMacDonald, Winchester, UK
Keith W. TurnerDesign Team Leader, WinchesterBridges Group, Mott MacDonald,Winchester, UK
Proceedings of the Institution ofCivil EngineersBridge Engineering 159March 2006 Issue BE1Pages 35–42
Paper 14232Received 07/10/2004Accepted 29/06/2005
Keywords:bridges/stress analysis/thermaleffects
Heat-straightening repairs to a steel road bridge
S. K. Clubley PhD, S. N. Winter MA, CEng, MICE, MIStructE and K. W. Turner BSc(Hons), CEng, MICE
On 16 July 2002 a low-loader lorry carrying heavy
machinery travelling eastbound on the A27 struck the
underside of Brockhampton Road new bridge. The bridge
suffered structural damage to the main beams and
bracing. From an initial emergency inspection, the damage
was found to be located close to the point of contraflexure
in an area where the bottom flange was in tension. It was
not considered necessary to impose immediate closures
or traffic restrictions. A heat-straightening repair of the
damaged beams was proposed. Detailed analysis using
both hand calculations and the finite-element method
confirmed the structural adequacy of the bridge to
undergo the heat-straightening process. These checks
encompassed the temporary conditions prior to, during
and after the heating. The major heat-straightening
process was successfully completed on site in ten days.
Impact damage to the beams was repaired within
acceptable tolerances and the straightened steel was
subjected to hardness and magnetic particle investigation
testing. The repairs to Brockhampton Road new bridge
were concluded without undue disruption to the travelling
public or local residents.
1. INTRODUCTION
Brockhampton Road new bridge replaced an earlier bridge on the
same alignment. It carries a busy local road over the A27 Havant
bypass in Hampshire, UK. The structure was designed by Scott
Wilson and constructed in 2001 by Costain under a Highways
Agency design-and-build contract.
On 16 July 2002, Mott MacDonald as agent for the Highways
Agency was informed by the Hampshire Police in Netley that a
vehicle travelling eastbound on the A27 had struck the underside
of the bridge. The bridge had suffered structural damage to the
main girders and bracing, resulting from the impact of
construction plant carried on the rear of a low-loader lorry.
Following an initial emergency inspection by Mott MacDonald in
July 2002, the structure was inspected in detail by Fairfield
Mabey using access equipment and traffic management in
December 2002. From the emergency inspection, the damage was
found to be located close to the point of contraflexure in an area
where the bottom flange was in tension. It was not considered
necessary to impose immediate closures or traffic restrictions.
The horizontal force from the impact was redistributed by the
bottom flange to the cross-bracings. The reaction generated in
Bridge Engineering 159 Issue BE1 Heat-straighte
the ‘K’ bracing caused a punching-type deformation in the web of
the first beam. This force was relieved once it reached a
magnitude large enough to shear the M24 bolts attaching the web
stiffener to the bracing. At this moment, the bottom chord of
the bracing buckled. The lorry continued to scrape the underside
of the next three beams before being pushed up into the fifth
beam causing damage to the bottom flange. Fortunately, the
reaction generated in this bracing was insufficient to fail either
the web or connection bolts.
Brockhampton Road new bridge was built with a square,
three-span, composite steel plate girder and concrete slab
structure. This is supported on reinforced concrete bank seats at
the north and south ends, and by two intermediate leaf piers
which are 600 mm in thickness. Transverse concrete deck
diaphragms are built into the supports making the bridge fully
integral. The piers are protected from traffic on the A27 by safety
fencing. The span of the centre section is 34.60 m, and the side
spans are 14.90 m, to the centreline of the supports. There are two
3.65 m carriageways and two combined cycleway/footways of
2.40 m in width.
The deck consists of six grade S355 steel plate girders supporting
a 210 mm thick solid reinforced concrete slab. Each main beam is
continuously braced in pairs and is 1000 mm deep with 480 mm
wide bottom flange and 300 mm wide top flange. The plate
thickness is reduced between splices in the main span
approximately at the point of contraflexure. A bottom flange
thickness of 25 mm and web thickness of 12 mm occurs at the
location of impact.
A major concern was how the structure could be restored to its
original condition or at least within the geometrical tolerances
given by BS 5400 part 6.1 It was clear from the inspection that
sections of steel would have to be cut out and replaced from the
web. Although the A27 at this location is a dual two-lane
carriageway, it is heavily trafficked by up to 82 000 vehicles per
day (average annual daily traffic (AADT) two-way flow).
Although it was fortunate that the damage occurred at the point
of contraflexure, this was offset by the fact that access for repairs
would necessitate total closure of the eastbound carriageway.
Any diversions would have to be through Havant town centre.
This was acceptable between 2100 and 0500 h, but not during the
daytime and in particular in the peak rush hours. Any delay or
disruption to the road would have been very unpopular.
To reduce the work to manageable sections which could be
achieved overnight, Mott MacDonald suggested that heat
ning repairs to a steel road bridge Clubley et al. 35
36
straightening be used to repair damage to the bottom flanges and
restore the plan straightness of the first and fifth beams. In
conjunction with the heat straightening, a series of additional
repairs were required to reinstate buckled stiffeners, ‘K’ bracing,
web and cracked welds near the impact zones. New protective
paint coatings were also needed on all affected areas.
The heat-straightening method provided the most cost-effective
solution for repairing the damage to the bridge beams. Heat
straightening has many advantages over beam replacement with
respect to the issue of reduced delay and disruption to the travelling
public. The justification for the use of heat straightening was based
on the knowledge that the mechanical properties of steel return
unchanged for temperatures up to 6008C. Advice was sought fromthe Highways Agency regarding previous repairs using
heat straightening. The mitigation for this method was based upon
the following estimated added value.
(a) Monetary: heat straightening, £90 000 versus beam
replacement, £450 000.
(b) Non-monetary: reduction in delay and disruption when
using heat straightening.
This equated to an added value of £360 000.
Figure 1 shows a recent photograph of the structure illustrating
the general arrangement and the position of the A27 dual
carriageway.
2. THE HEAT-STRAIGHTENING PROCESS
Heat straightening is a relatively new method of repair for
highway structures in the United Kingdom. By comparison, the
technique has been used quite successfully for many years in the
United States, combining both ongoing research and practical
experience.
The heat straightening of Brockhampton Road New Bridge was
carried out in accordance with the guidance of US Department of
Transportation—Federal Highway Administration document:
Heat Straightening Repairs of Damaged Steel Bridges—A
Technical Guide and Manual of Practice.2 Two formal departures
from standard were required to cover the use of this document
and the method of heat straightening structural steelwork.
Concentrated local heating of certain areas will produce
expansion of the steel and a lowering of the yield stress.
Fig. 1. General view towards southern abutment
Bridge Engineering 159 Issue BE1 Heat-straightenin
If surrounded by cooler steel, a restraining action will occur
which will cause the heated area to yield if a sufficiently
high temperature has been used. This restraint produces a
contraction as the metal cools, the effect of which is to yield
and deform its profile. By using carefully designed heating
patterns, this process of deformation can be used to return
damaged steel to its original profile. The careful placement of
additional external jacking forces can improve the recovery
during the cooling phase.
The most critical aspect of the heat straightening is the
through-thickness temperature of the metal. Any applied heating
must remain clearly below the lower transition temperature
(approximately 7238C), to prevent permanently changing the
physical properties. A maximum temperature between 600 and
6508C should not be exceeded for steels manufactured in the UK—
a ‘cherry red’ colour will be visible on the steel surface if the
temperature is too high. The attainment of the correct
temperature is indicated by a silver colour under the flame,
surrounded by a brown and blue area. During this process the
yield stress of the material will reduce temporarily by
approximately 50%.
A molecular phase change in steel occurs when the temperature
exceeds the lower transition point. At this temperature, the
body-centred cubic structure of the steel begins to assume a
face-centred cubic form. This composition carries a larger
percentage of carbon in solution. A careful cooling process is
required to return the molecular structure successfully to the
body-centred cubic arrangement. Uncontrolled cooling of the
steel may not allow this reversal to occur, which will produce
a hard but brittle material known as martensite. This material
has low fracture strength and is particularly susceptible to
cyclic loads.
There are several possible methods for monitoring the
temperature during the heat-straightening process. Typically,
this is most easily achieved by observing the colour of the steel,
which is a skill that is largely dependent upon experience.
Unfortunately, this method can be significantly erroneous.
Research by Roeder3 and Avent et al.,4 has shown that even
experienced practitioners when judging temperature consistently
misjudged by 568C and in some instances in excess of 1008C.Alternative methods of surface temperature measurement are
possible using special heat-sensitive crayons, thermocouples or
digital infrared pyrometers. Although it is not advisable to
overheat the steel above the transition temperature during heat
straightening, it does not immediately necessitate the
replacement of the member. Further engineering judgement is
always required.
During the heat straightening of Brockhampton Road new
bridge, digital infrared pyrometers were used. This form of
temperature monitoring proved to be very convenient as the
pyrometers were used from remote distances on the carriageway
below.
3. IMPACT DAMAGE
As previously mentioned, Brockhampton Road new bridge
suffered structural damage to two main beams and ‘K’ bracing,
following the impact of a low-loader lorry. Both global and local
g repairs to a steel road bridge Clubley et al.
deformation of the bottom flanges and web were immediately
visible after the accident.
The structure was inspected in detail which established,
fortunately, that the impact was located close to the point of
contraflexure. Fig. 2 illustrates the bending moment and shear
force profile at the location of impact. At the damage point, the
bottom flange of the beam is in tension. The flexural stresses in
the steel were calculated to be low.
The low-loader lorry struck the first main beam on the
eastbound carriageway, subsequently scraping the bottom of
the next three beams and finally striking the bottom flange
of the fifth main beam. Despite a satisfactory loaded trailer
height, impact occurred due to improperly secured machinery
bouncing upwards as the vehicle moved. All of the damage to
the structure had occurred before the driver could stop the
lorry in time. Fig. 3 shows the damage to the first and fifth
main beams.
A summary of the localised and global damage is given in the
following subsections.
3.1. Beam 1
At 8.0 m from the face of the north pier, the outer (west) half of
the bottom flange was bent upwards by 70 mm. This deformation
occurred over an 800 mm length. The web adjacent to the
damage was found to be out of verticality by 30 mm over a
Fig. 2. Location of vehicle collision (dimensions in mm)
Bridge Engineering 159 Issue BE1 Heat-straighte
600 mm height. The bottom flange adjacent to the damage was
found to be out of level by 12 mm over its 480 mm width.
At 9.0 m from the face of the north pier, the web was pushed
outwards at the nearest bracing. There was a large crack in the
web parallel to the bottom flange just above the web-to-flange
fillet weld. The ‘K’ bracing between the first and second beams
closest to the point of impact buckled at the bottom chord level.
This bracing was fabricated from 120 � 120 � 12 mm rolled
steel angle. The end of the bracing on the first beam was no
longer attached to the web stiffener. A tapered global
deformation of 50 mm lateral deflection was recorded. This
global displacement ceased at approximately 8 m either side of
the impact point.
3.2. Beam 5
At approximately 3.5 m from the splice plate, the west side of the
bottom flange was bent upwards by 20 mm. This deformation
occurred over an 800 mm length—the web adjacent to the
damage was found to be still vertical. The bottom flange was
found to be horizontal. There was no visible damage to the
bracing between the fifth and sixth beams. Permanent formwork
used during construction prevented inspection of the concrete
deck soffit. There were no visible defects in the formwork or
signs of distress.
Damage to the beams in between comprised of superficial paint
scraping only. The minimum headroom of the structure was
maintained at 5.4 m.
ning repairs to a steel road bridge Clubley et al. 37
Fig. 3. Damage to the main beams: (a) beam 1, west elevation;(b) beam 5, view towards south abutment
38
4. ANALYSIS AND MODELLING OF THE
STRUCTURE
A heat-straightening repair of the damaged plate girders required
the application of selective heating patterns. These comprised vee
heats for global deformation and line heats to correct
local distortion in the bottom flange. Passive restraint by
using hydraulic jacks was proposed in order to improve the
straightening during cooling. The heat-straightening process
was to be applied on the bottom flanges of the first and fifth
beams, and to a lesser extent, the web of the first beam.
In conjunction with the design of the main heat-straightening
process it was necessary to assess the bridge in its temporary
condition during the additional repairs. These repairs fell into two
categories. First, it was necessary to investigate a possible 50%
reduction in strength due to the heat-straightening process and
second, supporting calculations were required to confirm that
repairs could be conducted subject to dead and superimposed
dead loading without temporary supports to the damaged beams.
These repairs included the removal of web stiffeners, lateral
bracing and a section of buckled web to be cut out.
The maximum stresses in the bottom flange and web were
checked in accordance with an expected 50% reduction in the
yield strength of the steel beam when heated to a maximum of
6008C. Traffic management over the bridge was required to
prevent live loads from acting on each beam during the repairs.
This dictated the position of traffic flow so that all vehicular loads
were moved to the opposite side of the deck.
Fig. 4. Construction of the finite-element model
4.1. Frame analysis
The temporary condition defined the effects on the structure
during the initial repair process and in preparation for the
heat-straightening works. An analysis of the temporary
condition was required to investigate the following.
(a) Flexural stresses in the flanges incorporating a potential
temporary reduction in yield strength.
(b) Combined bending and shear in the web plate, including
the web cut-out.
(c) Removal of vertical web stiffeners.
(d) Yield and buckling of the web panel.
The bridge was modelled using the software Lusas Bridge Plus.
A portal frame was constructed to represent the integral
Bridge Engineering 159 Issue BE1 Heat-straightenin
arrangement. The frame was supported on elastic springs
modelling the thrust and retardation of the soil strata.
A transition between cracked and uncracked section properties
occurred at the main span splices, approximately 5.2 m after
the leaf pier support. The analysis was linear elastic.
Stresses in the flanges and web plate were calculated using staged
composite construction. The factored tensile design strength for
Grade S355 steel plates subjected to heat straightening was
reduced by 50% to 161 N/mm2, including the partial factor for
material properties, gm, in accordance with Federal Highway
Administration document: FHWA-IF-99-004 1998.2 Fig. 2
illustrates the bending moment and shear force profile for
reference.
For dead and superimposed dead loading the analysis found that
stresses in both the damaged first and fifth main beams did not
currently exceed 70 N/mm2, a satisfactory value less than the
factored tensile design strength of 161 N/mm2. Results were
output between a location 1 m either side of the impact point.
This 2 m region encapsulated the expected area of heat
straightening.
Loading on the beam comprised only dead and superimposed
dead loads, as before. The structural integrity was checked for
each stage of repair. This included the addition of new cruciform
stiffening and finally, removal of the damaged web section.
The modified steel section with web cut-out was checked in
accordance with BS 5400 Part 3: 20005 for yield and buckling.
However, this guidance does not directly incorporate an
allowance for deformed or damaged sections when checking
these criteria. A plate panel check for an undamaged web, using
BS 5400 Part 3: 20005 produced a structural adequacy of 2.6
and 4.8 for the yield and buckling criteria, respectively.
4.2. Finite-element analysis
A finite-element model of the damaged beam was constructed to
confirm the results derived using the frame analysis, particularly
the effects of localised damage on yield and buckling. Using
volumetric meshing the stress conditions in the steel were
examined in detail. In accordance with the portal frame analysis,
the model represented the first beam as that was the most
severely damaged. This was subjected to identical dead and
superimposed dead loads. The entire composite beam over the
full length was modelled with restraints representing the bracing.
Fig. 4 shows the finite-element model.
To improve the numerical accuracy of the solution in the region
of the heat straightening, further refinement of the mesh was
g repairs to a steel road bridge Clubley et al.
Impact damage
(a) (b)
Fig. 5. Local stress analysis: (a) in-service flexural stresses, (b) shear stresses with web cut-out
incorporated. The web cut-out was conservatively approximated
without a smooth corner radius. As a result, a small stress raiser is
shown at the corners. The analysis type was again linear elastic.
Figure 5(a) illustrates the flexural stresses in the first damaged
beam subject to identical loading and shows the point of
contraflexure using a white colour. The finite-element model
exhibited better load distribution with a maximum bottom flange
stress of 50 N/mm2. Introduction of a 500 mm � 500 mm
web cut-out and cruciform stiffening produced stresses
approximately 30 to 40 N/mm2 higher. Fig. 5(a) confirmed
the fortunate location of the lorry impact near the point of
contraflexure.
Figure 5(b) visually illustrates the concentrated shear stress in the
web panel with the damaged steel removed. The finite-element
model was modified to approximate the localised deformation
recorded during the detailed inspections. Both the hand
calculations and finite-element analysis confirmed a satisfactory
web plate buckling factor of 0.21.
The finite-element analysis was further extended to examine the
same beam given a localised failure of the bottom flange due to a
hypothetical gross mis-heating. During the heat-straightening
process the applied temperature is restricted to below 6008C.Should the maximum permissible temperature be exceeded, the
material properties of the steel will become permanently altered.
This would potentially have serious consequences on both the
immediate and future in-service performance, particularly
fatigue. A section of the bottom flange was removed from the
finite-element model at the location of heat straightening.
The analysis conservatively showed the stresses in the web
and flanges did not exceed 130 N/mm2, still below the
reduced factored tensile design strength.
Beam 1:globaldamage
Beam 1:local damage(plan view)
Beam 1:local damage
(elevation view)
Beam 5:local
damage
Strain ratio, m 5.56 30.06 25.07 3.85Assessment status Acceptable Acceptable Acceptable Acceptable
Table 1. Damage strain ratios
5. DESIGN OF THE HEAT
STRAIGHTENING
Design of the heat straightening was
based upon advice from experienced
contractor Fairfield Mabey and
information gathered from desk
studies. The structure was inspected
in detail using access equipment and
Bridge Engineering 159 Issue BE1 Heat-straighte
traffic management in December 2002. This report included
magnetic particle inspection (MPI) testing to all impacted areas
plus MPI and hardness tests to all yielded steel.
The decision whether to use the method of heat straightening
was based upon a damage strain ratio calculation. Federal
Highway Administration document FHWA-IF-99-004 19982
recommends heat straightening can be carried out on North
American steel products if the damage strain ratio is less than
100. As the manufacturing process of steel in the UK differs from
that used in North America, the Highways Agency has currently
adopted a maximum strain ratio of 50. The strain ratio is
calculated using equations 3.1, 3.2 and 3.9 in Federal Highway
Administration document FHWA-IF-99-004 1998.2 For brevity,
the damage strain ratio calculation is summarised in equation
(1).
Damage strain ratio m ¼Eymax
Rf y1
where E is the modulus of elasticity of steel; ymax is the distance
from the centroid to the extreme fibre of the element; R is the
radius of curvature; and fy is the yield stress.
The strain ratio was calculated for local and global damage
considering both the first and fifth beams. A damage strain ratio
not exceeding 30 was determined based upon the detailed survey
measurements. This confirmed an acceptable assessment status
for all the proposed heat-straightening repairs. A summary is
shown in Table 1.
A series of passive jack restraints were designed for use during
the heat-straightening process. The careful placement of
additional jacking forces can substantially improve the
recovery during the cooling phase, therefore reducing the
ning repairs to a steel road bridge Clubley et al. 39
40
number of heating cycles. A different arrangement was required
for local and global straightening. Fig. 6 shows the set of
inclined jacks restraining global movement while a single
vertical jack assists local flange straightening. It was very
important that none of the jacks was over-pressurised
causing cold mechanical straightening of the steel. A strict
monitoring programme was designed to prevent any damage
occurring in this manner.
The permissible jack restraint forces were calculated in
accordance with FHWA-IF-99-004 1998.2 To prevent
mechanical straightening, they were required to satisfy two
key criteria.
(a) First two heating cycles: loads should not produce bending
moments greater than 16% of the plastic moment capacity
of the member.
(b) Subsequent heating cycles: loads should not produce
bending moments greater than 33% of the plastic moment
capacity of the member.
Based upon the plastic moment capacity of the bottom flange, the
jacking loads at 16 and 33% were 33 and 67 kN, respectively.
5.1. Heating patterns
There are four main damage categories that can be repaired using
heat straightening.
(a) Category S: bending about the ‘strong’ or major axis.
(b) Category W: bending about the ‘weak’ or minor axis.
(c) Category T: torsion or twisting about the longitudinal axis.
(d) Category L: localised flange or web buckling, web crippling,
small bends or crimps in the plate.
Heat straightening should only be applied in the vicinity of a
yield zone. A yield zone is an area in which inelastic deformation
has occurred. Any permanent bulges or thickening found in the
heated zone after cooling is called ‘upsetting’.
The different heating patterns available for selection were: vee
heats, line heats, spot heats, strip heats and edge heats. Repair of
the local and global damage to the beams utilised a careful
combination of line heats and vee heats, applied to both sides of
the bottom flange. Vee heats are the most fundamental heating
pattern used to straighten Category S bending about the major
axis. Direct heating causes an expansion which increases the
deflection but cooling causes a subsequent larger contraction
correcting the original damage. The largest contraction occurs at
Fig. 6. Repair of damage to beam 1: (a) passive jacking restraints to(b) jacking restraint to correct local damage (concentrated vee heatrepair stiffening
Bridge Engineering 159 Issue BE1 Heat-straightenin
the open mouth of the vee causing the section to move in the
direction of the vee. If the initial expansion is restrained, the
overall movement is increased.
Importantly, the welding torch passes across the vee shape in a
snake ‘S’ shape on both sides of the plate. With care, this
technique helps prevent an undesirable concentrated heating
effect.
Line heats are a heating pattern used to repair Category W
bending about the minor axis. This method of straightening is
conducted using a straight transition of the welding torch
between two points. Line heating can in some circumstances
require an external jacking restraint to accelerate the
straightening. Successful heat straightening is largely dependent
upon operator skill and for line heats the speed of the torch
over the metal is crucial to success.
Figure 6 shows the pattern of heating used to correct both local
and global damage of the first beam. A combination of vee heats
and line heats together with the raking restraints guided the
global correction of the bottom flange. A vertical restraint and
concentrated vee heat on both sides of the flange was used to
straighten the localised damage.
6. SITE OPERATIONS
All site operations were conducted at night during the closure
and temporary diversion of the eastbound A27 carriageway.
Work commenced on 17 November 2003 and by 29 November
2003 the site had been cleared and all aspects of the project had
been completed with the exception of the application of a full
protective coating system to the steel.
Following the removal of the buckled bracing and web
stiffeners, a series of trial heat cycles were carried out at
ground level on sections of steel plate. These were of similar
thickness and grade to those occurring in the bridge where
heat straightening was required. The trial sections were
heated, using vee heat patterns, until the colour of the steel
below the flame was silver, with a brown and blue surround.
An infrared digital pyrometer was used to confirm that
temperatures in the range 550 to 6208C were attained. All
operatives working on the bridge carried out the trial. One
trial section was marked up such that tensile and Charpy
impact tests could be carried out on both heated and unheated
steel. The results of these tests confirmed that no significant
correct global damage (alternate vee heat pattern shown);pattern shown); (c) local restraint and web cut-out; (d) cruciform
g repairs to a steel road bridge Clubley et al.
Fig. 7. Repaired bottom flange following heat straightening
changes in tensile strength or ductility occurred during the
trial heat cycle.
Global heat straightening of beam 1 began after the completion
of the trial heat cycles. Blast cleaning of the steel was carried out
and the lateral restraints were jacked to the design loads before
the heating started. Once a series of clearly marked vee heat
patterns had been marked on the bottom flange the first heat
cycle was carefully applied. The steel was subsequently allowed
to cool to below 1208C before beginning the second cycle.
Temperatures were monitored by observing colour and by using
infrared digital pyrometers.
After the second heat cycle, it was ascertained that the maximum
horizontal deflection had reduced from 52 to 31 mm. Three more
heat cycles were applied, reducing the maximum horizontal
deflection further to 21 mm. This was considered within
tolerance and it was decided to carry out no further global
straightening. In contrast, a series of nine heat cycles using line
patterns and vee heats were required to straighten the local
damage in the bottom flange to within an acceptable tolerance.
Restraining jacks were utilised between the top and bottom
flanges to assist the corrective movement during the cooling
phase.
Following the global and local straightening of beam 1, work
began to rectify the buckled web plate. This involved the removal
and reinstatement of the damaged section using flame cutting
followed by manual metal arc welding. Prior to cutting out the
deformed web, a cruciform arrangement of four web stiffeners
was welded in position to restrain the adjacent web areas in the
temporary condition (see Fig. 6). After repair of the web, some
cruciform stiffeners were removed to allow the installation of the
new vertical web stiffener. Accordingly, the replacement ‘K’
bracing system was then attached to the vertical web stiffener by
HSFG Part 1 bolts. Fig. 7 shows the final straightened profile
of the first beam.
The heat straightening was completed by the repair of beam 5.
The distortion caused by impact damage was straightened using
passive restraints between the top and bottom flanges, and a
series of four line heating cycles. Overall vertical distortion was
reduced from 22 to 8 mm. This marginally exceeded the target
value of 6 mm but, after consideration of the likelihood of further
heating improving the distortion by a final 2 mm, it was decided
to accept the correction value.
7. MATERIALTESTING
Magnetic particle investigation testing was carried out on all
areas of steel where heat cycles were applied, prior to and after
certain stages of the work. A final MPI test was carried out on
completion of the heat treatment. No defects were recorded. All
new fillet welds were tested by MPI and all new butt welds were
tested by MPI and ultrasonic testing. Again, no defects were
recorded.
Hardness testing was carried out on the distorted bottom flange
areas prior to the heat straightening and after certain heat cycles
for both beams. It was noted that, following the heat
straightening, the hardness test results (Vickers) reduced from
approximately 165 to 125 HV where the maximum heat had
Bridge Engineering 159 Issue BE1 Heat-straighte
been applied. Using comparisons with BS 970,6 this would
indicate a reduction in tensile strength at ultimate limit state
from 550 to 400 N/mm2. The ultimate tensile strength (UTS)
requirement to BS EN 100257 for grade S355 steel of this
thickness is 490 N/mm2.
It should be noted that the application of one heat cycle to the
trial sections did not cause the UTS to be reduced when tested
by destructive methods, producing a value of approximately
580 N/mm2. Accordingly, the estimated UTS using hardness
values was considered to form an indicative guide. In view of the
apparent reduction in hardness readings resulting from the
application of multiple heat cycles, it was recommended that for
future similar projects, the number of cycles applied to trial
panels is increased to six. Destructive testing of the trial sections
prior to starting work would thereby be more representative of
the heat straightening.
After consideration of the location of the repairs, which was close
to the point of contraflexure, a reduction in UTS to 400 N/mm2
would not constitute a theoretically overloaded section of girder.
The maximum factored tensile stresses resulting from 30 units
HB and associated HA loading at the locations where heat cycles
were applied did not exceed 90 N/mm2. If the factored tensile
design strength for grade S355 steel is reduced from its normal
value of 307 N/mm2 in proportion to the apparent decrease in
UTS, a maximum stress of 256 N/mm2 is obtained, which
exceeds the applied stresses by a considerable amount.
8. SUMMARY
Heat-straightening repairs to structural steelwork on
Brockhampton Road New Bridge were successfully completed,
pending new protective coatings, in ten days. Impact damage
to the beams was repaired within acceptable tolerances and
the straightened steel was subjected to hardness and MPI
testing. The implementation of the repair works reinstated the
affected members to their original designed strength
capacities.
This case study illustrates the future potential of the
heat-straightening method for structural steelwork repairs in
the UK. The mitigation for the scheme demonstrated an added
value of approximately £360 000. Repairs to Brockhampton Road
ning repairs to a steel road bridge Clubley et al. 41
42
New Bridge were completed without undue disruption to the
travelling public or local residents.
9. ACKNOWLEDGEMENTS
The assessment and analysis of Brockhampton Road New Bridge
was conducted by Mott MacDonald on behalf of the Highways
Agency Area 3 commission. Gratitude is extended to the
Highways Agency for permission to publish this paper.
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tor at [email protected]
ineers and related professionals, academics and students. Papersferences. Please visit www.thomastelford.com/journals for author
g repairs to a steel road bridge Clubley et al.