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COLORADO OFFICE 1 0758 W. CENTENNIAL RD., STE. 200 LITTLETON, CO 801 27 TEL: (866) 981-4588 F A}C (720) 981-5643 October 4, 2016 ATTN: Document Control Desk Nuclear Regulatory Commission Washington, D.C. 20555-001 ***and*** Brian Wood State of Wyoming '' Department of Environmental Quality - Land Quality Division 510 Meadowview Drive Lander, WY 82520 RE: · Notification of Excursion at M0-108 Lost Creek ISR Project SUA-1598 I PT788 WYOMING OFFICE 5880 ENTERPRISE DR., STE. 200 CASPER, WY 82609 TEL: (307) 265-2373 FA}C (307) 265-2801 Mr: Saxton/Mr. Wbod, · ;- :' :: ., 1i :'! -·; 1. •. '/ This is the to NRC of the verification of an upper vertical excursion at the Lost Creek ISR in follow' up to notification via 1 e-mail 6n'September 30, 2016. The excursion detected at Mo.:.10e of the verification sample collected that same day. The location of the well is provided on the attached figure "HH1-6 Patterns and Wells". The excursion was detected in the overlying FG horizon directly above the HJ mining horizon. The excursion is based on the Opper fUC 'L ) cal ci.Jla'ted on a per well basis as approved by NRC .. However, the is riot an exc·ursion according fo'tfie LOO-approved method of determining UCLs on a per wefl group basis. ' . ' . ·i _: ' 1 In accordance wi th Operations Plan Section 3.6.4.3, this notification provides the following information: ) , ' Recent chemical trends of the monitor well on excursion The following table and charts provide data from 2016 to reveal the trends of the Upper Control Limit (UCL) parameters: . ,, Lost Creek JSR, LLC is a wholly-owned subsidiary of Ur-Ener gy In c. TSX: URE www.ur-energy.com

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  • COLORADO OFFICE 1 0758 W. CENTENNIAL RD., STE. 200 LITTLETON, CO 801 27 TEL: (866) 981-4588 F A}C (720) 981-5643

    October 4, 2016

    ATTN: Document Control Desk Nuclear Regulatory Commission Washington, D.C. 20555-001

    ***and***

    Brian Wood State of Wyoming ''

    Department of Environmental Quality - Land Quality Division 510 Meadowview Drive Lander, WY 82520

    RE: · Notification of Excursion at M0-108 Lost Creek ISR Project SUA-1598 I PT788

    WYOMING OFFICE 5880 ENTERPRISE DR., STE. 200

    CASPER, WY 82609 TEL: (307) 265-2373 FA}C (307) 265-2801

    Mr: Saxton/Mr. Wbod, · ;- :' :: ., ·~ ·~ 1~ 1i :'! -·; 1 . ·· ·~ · •. '/

    This is the writt~n - ~otification to NRC of the verification of an upper vertical excursion at the Lost Creek ISR Proje~t in follow' up to notification sub'rnitt~d via 1e-mail 6n'September 30, 2016. The excursion detected at Mo.:.10e ~a$ cohfi:rm~d · on September~:29; · 2C5ltff>Vanalysis of the verification sample collected that same day. The location of the well is provided on the attached figure "HH1-6 Patterns and Wells". The excursion was detected in the overlying FG horizon directly above the HJ mining horizon.

    The excursion is based on the Opper cb~trbi' Limit~ fUC'L) calci.Jla'ted on a per well basis as approved by NRC .. However, the · ~vent is riot an exc·ursion according fo 'tfie LOO-approved method of determining UCLs on a per wefl group basis. ' . ' . · i _: ' 1

    In accordance with Operations Plan Section 3.6.4.3, this notification provides the following information: ) , '

    • Recent chemical trends of the monitor well on excursion The following table and charts provide data from 2016 to reveal the trends of the Upper Control Limit (UCL) parameters:

    . ,, Lost Creek JSR, LLC is a wholly-owned subsidiary of Ur-Energy Inc.

    TSX: URE www.ur-energy.com

  • I ,

    . -

    '' "

    Sample ID·

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    M0-108

    ',

    Collection Date

    1/7/2016

    1/21/2016

    2/10/2016

    2/22/2016

    3/8/2016

    3/25/2016

    4/8/2016

    4/23/2016

    5/5/2016

    5/21 /2016

    6/3/2016

    6/16/2016

    7/8/2016

    7/22/2016

    8/4/2016

    8/18/2016

    8/30/2016

    9/3/2016

    9/27/2016

    9/29/2016

    Lost Creek ISR Project 12 Notification of Excursion at M0-108

    TABLE 1: 2016 UCL Data for M0-108

    Alkalinity (mg/I) Chloride (mg/I) Sp. Cond. (µSiem)

    Assay UCL % Assay UCL % Assay UCL % NRC* Di ff NRC* Diff NRC* Diff

    98 118 -17 6.1 20 -70 500 513 -3

    99 118 -16 5.7 20 -72 496 513 -3

    96 118 -19 6.9 20 -66 494 513 -4

    97 118 -18 6.3 20 -69 500 513 -3

    100 118 -15 6.7 20 -67 502 513 -2

    100 118 -15 6.1 20 -69 505 513 -2

    97 118 -18 7.6 20 -62 504 513 -2

    100 118 -15 6.2 20 -69 507 513 -1

    105 118 -11 6.0 20 -70 489 513 -5

    106 118 -10 6.0 20 -70 486 513 -5

    108 118 -8 6.0 20 -70 489 513 -5

    101 118 -14 6.2 20 -69 506 513 -1

    103 118 -13 7.2 20 -64 506 513 -1

    104 118 -12 9.1 20 -54 525 513 2

    107 118 -9 10.7 20 -47 547 513 7

    111 118 -6 11.4 20 -43 556 513 8

    114 118 -4 12.6 20 -37 551 513 7

    115 118 -2 13.8 20 -31 548 513 7

    136 118 15 14.9 20 -26 589 513 15

    121 118 3 18.3 20 -8 583 513 14

    *UCLs calculated on a per-well basis Italics indicates % difference exceeds UCL but by less than 20% over

    Lost Creek JSR, LLC is a wholly-owned subsidimy of Ur-Energy Inc. ·· TSX: URE

    www.ur-energy.com

    I

  • 1

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    190

    180

    170

    160

    150

    140

    . 130

    - 120

    110

    100

    Lost Creek ISR Project 13 Notification of Excursion at M0-108

    - - -----------M0-108 Alkalinity

    I .... - ·· - ·· -· · - ·· - ·· - ·· - ·· -· · - ·· i ·· -· · - ·· - , · - ·· - ··

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    90 L ··::::··: _ ~ . ! .} '., ! 12/2212015 1/2112016 2/20/2fJ16 3/2112016 4/20/2016 512012016 6/19/2016 1/19/2016 8/18/2016 9/11/2!316 1011112016

    --· Alkalinity (mg/I) - - - UCL NRC - • • UCL LQD ......... Linear (Alkaiinity (mg/I))

    '-----

    25.0

    20.0

    15.0

    10.0

    5.0

    0.0

    ,., --: 1 • . . ' .

    ~ · I

    - . ! - . . - ... . - .. ~ . - ~-. ·} _· ... ~ . : -- .... ; - ~ - ·-:.: ·,..·: - · ! · -T · --:~~ ·· - .. v· - - - - - ::- - - - ~-; -~, - - ~-:: - - 7 - -- - - . -: - - - - ~- - - - - --:- ~ .-: - - - -

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    12/22/2015 1/21/2016 2/20/2016 3/21/2016 4/20/2016 5/20/2016 6/19/2016 7/19/2016 8/18/2016 9/17/2016 10/17/2016

    --Chloride (mg/I) - - - UCL NRC - • • UCL LQD .. . .. . .. . Linear (Chloride (mg/I))

    Lost Creek JSR, LLC is a wholly-owned subsidimy of Ur-Energy Inc. TSX:URE

    www.ur-energy.com

  • Lost Creek ISR Project 14 Notification of Excursion at M0-108 ,

    960

    910 I

    860

    810 r

    760 l

    610

    560

    510

    ~.' '. ~ . ' M0-108 Conductivity .,.

    '; ..• ·1 .. \•"' '·' ''·· ' .

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    .. ..................... !···· ......

    - - - - - - - - - - - - - - - - - • .2'9' .. -·-··~ · ~··.:.. - - - - - -················ ························

    460 "

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    12/22/2015 1/21/2016 2/20/2016 3/21/2016 4/20/2016 5/20/2016 6/19/2016 7/19/2016 8/18/2016 9/17/2016 ,10/17/2016

    --Sp. Cond. (µS/cm) - - - UCL NRC - • • UCL LQD ......... U~ear (Sp. Cond. (µS/~m)) _ __J

    • The reason for the excursion

    . "

    The reason for the excursion is unknown at this time but is under investigation. Current investigation elements include:

    o Injection and production well flow rates are being reviewed to determine if an effect was the result of flow scheme;

    o Historic borehole records have been reviewed to determine if there were any historic boreholes in the area that had not been found and re-abandoned. Records show one historic borehole located approximately 170 feet to the south-southeast of M0-108 was searched for but never found and thus not re-abandoned. It is unknown if this is a potential source.

    • Actions to be taken to recover the excursion Injection in the area was terminated, in accordance with License Condition 10.10, by shutting off injection wells 11171, 11527, 11161, 11162, 11181, 11305A, 11306, 11307, and 11284, if they had not already been shut off. Well 1P1531 will be converted back into a pumping well which will supplement the production flow in the area. The effects of the adjustments will not be known until successive samples are collected and analyzed.

    Lost Creek JSR, LLC is a wholly-owned subsidia1y of Ur-Energy Inc. TSX:URE

    www.ur-energy.com

  • :j

    Lost Creek ISR Project 15 Notification of Excursion at M0-108

    Please contact me at the Casper office if you have any questions regarding this submittal.

    Regards,

    Michael D. Gaither Manager EHS and Regulatory Affairs Ur-Energy USA, Inc.

    Attachments: Figure as stated

    Cc: Deputy Director, Decommissioning and Uranium Recovery Licensing Directorate

    : ·:

    • 1 ~: .....

    Division of Waste Management and Environmental Protection Office of Federal and State Materials and Environmental Management Programs U.S. Nuclear Regulatory Commission Mail Stop T-8F5 11545 Rockville Pike, Two White Flint North Rockville, MD 20852-2738

    John Saxton, NRC Project Manager (via email) Theresa Horne, Ur-Energy Littleton Office (via email)

    ...... _ I .

    .) . . .. ~ '

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