cold forging process and product development - case study

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Process and Product Development Valve Tappet Cold forging Process Abdullah Ansari

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Cold forging, Head type Valve Tappet Process improvement, reduction in rejection and waste by right engineering

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Page 1: Cold forging Process and Product Development - Case study

Process and Product Development

Valve Tappet Cold forging Process

Abdullah Ansari

Page 2: Cold forging Process and Product Development - Case study

INDEX• Introduction

• Nature of Problem

• Existing Blank & Forging Die Analysis

• Cold Forging Standard

• Existing D2/d2 & l/d Ratios

• Corrective Actions

• Recalculations,  Results Of Recalculations

• Trials & Decisions

• Previous Process & Revised Process

• Results with Revised Tooling & Conlusion

• Support During Development

Page 3: Cold forging Process and Product Development - Case study

INTRODUCTION

The problem of head offsetting while cold forging of item R 708‐13 is observedin since new product development.

To avoid the same several corrective actions [short method] were initiated suchas using flat ejector etc. but effectiveness of the actions taken was not 100%satisfactory. The results were not consistent.

After all above it is concluded to analyze and re‐design of cold forging tooling &process.

While analyzing the same whatever the calculations, observations and theactions taken by undersigned are recorded here, which will be one guide line toattend this kind of problems in future.

A. T. ANASRI              Date : 22.08.2000

Page 4: Cold forging Process and Product Development - Case study

Nature of Problem 

( Tappet R 708‐13 )While cold forging 1st stage Head Diameter of Tappet getting more offsets & not getting controlled after 

several adjustments.

Page 5: Cold forging Process and Product Development - Case study

Existing Blank & Forging Die analysis • .Size of Cold forging blank: Total Length            = 85mmOuter diameter ( d ) = 12.5mm• .Size of cold forged part:Head diameter ( D )  = 30mmHead thickness          = 5.5mmTotal length               = 61mmOD of stem               = 12.8 & 12.6mm• .Size of Cold forging Die:Length of die                                    =  90mmLength of blank outside the die  ( l ) =  30mm

( From flat face ) 

Page 6: Cold forging Process and Product Development - Case study

Cold forging standard

Cold forging standard states that:D2/d2 and  l/d should not exceed 3. Where 2 is ideal.

In our caseD = 30mmd  = 12.5mml  = 30mm

Page 7: Cold forging Process and Product Development - Case study

D2/d2 = 302/12.52 = 5.76l/d = 30/12.5 = 2.40 By above calculations it is noticed that value D2/d2 is 

exceeding the standard and l/d is almost in range. So we may conclude that above exceeding value is 

affecting to forged head diameter offsetting.

In light of Cold Forging Standard Existing D2/d2& l/d ratios

Page 8: Cold forging Process and Product Development - Case study

What to do now ???

Corrective action planned : 

–Recalculate the die design as per coldforging standard. And manufacture thecold forging die as per new calculateddimensions.

Page 9: Cold forging Process and Product Development - Case study

Recalculations as per Cold forging standard

D2/d2 = 2 ( as per standard )Hence D2/12.52 = 2D2 = 2 x 12.52

D = 17.67mm.‘l’ of ‘D’ will be 17.67x17.67x l x /4 = 12.5x12.5x30x /4

l = 15.01mm

Page 10: Cold forging Process and Product Development - Case study

What Recalculations Indicating!!!

Recalculations indicating that the forging is not possible in one operation& it will need double operation. For second operation stepped blank willbe required, while first operation stepped blank will be produced.

For preparing stepped blank separate die isrequired

Page 11: Cold forging Process and Product Development - Case study

Trials .

For trials stepped blank is prepared by machining. While trials forming punch is used. 

Trials are taken with stepped blank on 22.08.2000Results found satisfactory in all aspects.Head offsetting is very low & will not create anydefect while head turning.

Dimensions are found consistent.Trials are successful.

Page 12: Cold forging Process and Product Development - Case study

Way Forward.

Based on successful  trials, die designed for first operation for preparing the stepped blank (cold forging 1st operation).

Page 13: Cold forging Process and Product Development - Case study

# PREVIOUS PROCESS

Fig. Shows the 

blank ready for 

forging of R708‐

13 tappet. 

85

12.5

Page 14: Cold forging Process and Product Development - Case study

1 ‐ PREVIOUS PROCESS

Fig. Shows the 

forging drawing of 

R708‐13 tappet. 

Previously this was 

created in single 

setting.

30 12.8

5

40

12.6

Page 15: Cold forging Process and Product Development - Case study

# REVISED PROCESS

Fig. Shows the 

blank ready for 

producing 

stepped blank 

for forging  of     

R708‐13 tappet. 

85

12.5

Page 16: Cold forging Process and Product Development - Case study

1 ‐ REVISED PROCESS 

Fig. Shows the 

stepped blank

ready for finish 

forging of R708‐13 

tappet. 

12.6 12.5

40

17.7

15

Page 17: Cold forging Process and Product Development - Case study

30 12.8

5

40

12.6

2 ‐ REVISED PROCESS

Fig. Shows the finish 

forging  of R708‐13 

tappet. 

Now it is created in 

second stage from 

stepped blank.

Page 18: Cold forging Process and Product Development - Case study

Die drawing for stepped Blank

Page 19: Cold forging Process and Product Development - Case study

Results with revised tooling.

Implemented the new tooling & monitored for 1000nos forcold forging 1st & 2nd operation.

No problem while preparing stepped blank. I.e. 1stoperation.

No problem of head forming while 2nd operation.Improved consistency in dimensions while cold forging 2nd stage.

Setting time for cold forging is  reduced.Minimizes rejection at cold forging drastically . Hence reduction in wastage. 

Page 20: Cold forging Process and Product Development - Case study

FINAL CONCLUSION.

The newly designed tooling is OK & Proven

for production.

05.11.2000

Page 21: Cold forging Process and Product Development - Case study

Mr. V RamgopalMr. M. GANAPATHY

For Giving A Opportunity To Work On Such A Special Task.

Mr. S.C.SALVI & Mr. P.S.KULKARNI Team members

Acknowledgements

Page 22: Cold forging Process and Product Development - Case study

Thank You

[email protected]