case study of o-ring failure
DESCRIPTION
This case study is about the O-ring failure analysisTRANSCRIPT
MUHAMMAD REHAN KHAN
CONTENTSBackgroundPVC II PolymerizerMan way specificationsSequence of eventAnalysis of failure Probable causesConclusionRecommendationsCost Analysis
BACKGROUND PVC II Polymerizer faces the VCM leakage most of the time when it
get discharges and taken on hold for next batch charging for more than 4 to 5 hours
NOTE: All the failures are of same nature and follows the same sequence, this was the reason that led to the development of this Case Study and complete investigation.
Date Event Observation Action Taken
23rd Nov 2010 VCM leakage detected from the man way of PLY-1E
Polymerizer was on hold for batch charging Man way opened and the O-ring was replaced
8th January 2011 VCM leakage detected from the man way of PLY-1E
Polymerizer was on hold for batch charging Man way opened and the O-ring was replaced
1st February 2011 VCM leakage detected from the man way of PLY-1E
Polymerizer was on hold for batch charging Man way opened and the O-ring was replaced
2nd April 2011 VCM leakage detected from the man way of PLY-1E as well as 2E
Both polymerizer were on waiting for batch charging from 48 hrs and 24 hrs respectively
Man way opened and the O-ring was replaced
2nd October 2011 Pressure test of all three Polymerizers failed while they were hold on for more than 10 hours
All the Polymerizers were on hold due to the power outage from GT B
Man way opened and the O-rings were replaced
PVC II Polymerizer Design Pressure & Temperature = 1.55MPa &
930C
Operating Pressure & Temperature = 0.85MPa & 550C
MOC: 16MnR (C-Mn-Si Steel) +304 (GB6654, A537M)
ID = 3810mm, H = 7068mm
Empty Weight = 44.7 M Tons
REACTION TEMPERATURES:
AFA Coating T = 850C
Batch Charging T = 650C
Reaction T = 590C
Discharge T = 580C
HP SEAL WATER
CATALYST
DISPERSANT SHORT
STOPSTEAM POLISHED
WATER
VCM
FLUSH WATERMODIFIER
SHORT STOP
STEAM
COATING AGENT
INJECTION WATER
HP FLUSH WATER
ABOUT MANWAYO-ring arrangement for man way
EPDM O-RING
SEQUENCE OF EVENTSPolymerizer get discharge and hold on 4 to 5 hours for next batch charging
VCM leak from the man way which is detected by the VCM detectors and then soap test
Poly get depressurize completely (2.5 hours) and the o ring is replaced (1 hour)
V/A and Leak test done (5.5 hours)
Poly takes on service and found OK (Total outage 8-9 hours)
ANALYSIS OF FAILURE
CHEWED/ CHIPPED APPEARANCE
CHEWED/ CHIPPED APPEARANCE
PROBABLE CAUSES1. Difference in thermal expansion of the mating surfaces i.e. man
way and its closure ring
2. Size of the O ring and its groove dimension
3. Softening of Elastomer due to incompatibility
4. Improper machining of O-ring gland i.e. Sharp edges (Not the case)
5. Elastomer too soft (Not the case)
Thermal expansion of mating surfaces DATA:
Material = 0Cr18Ni9 (SS304)
Ambient Temp. = 30 C Temp. Of Ring = 43 C
AFA Coating T = 850C Batch Charging T = 650C Reaction T = 590C Discharge T = 580C
THERMAL EXPANSION
▲l = L * k * ▲T (k = 17.2 X 10-6 m/m-K)
▲ l = 0.2mm
MANWAY
CLOSING RING
SIZE OF THE O-RING AND GROOVE DIMENSION
O-ring’s dimensions O ring diameter = 7.5mm OD = 633mm Volume of the O-ring (2pi2 Rr2) = 86,856
mm3 Groove’s dimensions Actual W = 6.5mm, H = 5.72mm Volume of the Groove = 92,222mm3
Standard Groove DimensionsAs per AS568B for O ring diameter = 7.5mm, W = 6.2mm, H = 6.2mm Volume of the Std. Groove = 94,345 mm3Which is greater than the total actual volume
Softening of Elastomer due to incompatibility
OBSERVATIONS
SEQUENCE OF FAILURE
POLY GETS ON HOLD FOR MORE THAN 5 HOURS AND THE COOLING OF MAN WAY LEFT THE SPACES IN THE O RING
SWELLING OF O-RING FURTHER CONTRIBUTES TO THE COMPRESSION
VCM STARTS PENETRATING AND CAUSES O-RING TO SWELL
THERMAL EXPANSION OF MAN WAY COMPRESSES IT MORE WHICH CAUSES CRUSHING
O-RING INSTALLED (OVER COMPRESSED DUE TO UNDERSIZE GROOVE)
AFTER WHICH THE O RING DO NOT SEAL ANY MORE AND VCM LEAKAGE OSERVED
VCM
CONCLUSION
As per AS568B, the groove of the man-way O-ring is undersized which after closing the man way, over compressed the O-ring and cause it to tear from the edges
The different thermal expansions of man way and its ring causes the crushing of the O-ring from its edges
EPDM is not suitable with the VCM service . During investigation PVC powder found on the d/s of the O-ring which should not be a case in 100% sealed O-ring. This EPDM O ring was suggested by the TCC vendor
RECOMMENDATIONS
Replaced the man way arrangement with a flanged arrangement like PVC I polymerizer
Use Teflon or FFKM O-rings instead of EPDM
Machined the groove for increasing its volume to suit with our O-ring dimensions
Use standard size of O-ring for this groove i.e. ID = 633.48 +- 2.92, d = 6.99+-0.15 as per AS568B # 474
COST ANALYSIS
Total Outage time = 8-9 hours
Total loss of PVC / batch = 18 Tons
1 Tons = $1,070 (Reference: www.icis.com)
For one batch, we face the loss of 19,260$ (Rs 16,37,000)
FFKM O-ring cost = $ 3,000
REFERENCES
DISCHTOMATIC O-ring handbookParker O ring handbook Standard (AS568), Metric O-Ring sizesPVC II Process description by TCCB-reports of O-ring failure
QUESTIONS