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Root Cause Analysis Case Study 1 Case Studies Engine Roll-back Investigation Following a number of in-service events of roll- back (uncommanded power reduction) on one or more engines WEC engineers undertook a complex root cause investigation. The rollback events occurred during operation at over 27,000ft in particular icing conditions found under the anvil of cumulonimbus cloud formations, which was outside of the natural icing certification envelope. The root cause was initially thought to be a problem with engine fuel control on maximum thrust limits, but following substantial analysis of data from flight recorders, the root cause was found to be ice accretion on the engine compressor supercharger stage vanes causing the engine core flow to be restricted. The transient nature of icing meant that the evidence was lost when the aircraft was on the ground, so that after the occurrences all maintenance checks showed that engine operation was normal. The problem was cured by providing additional heating of the supercharging vanes. Rob Hardman, Senior Engineer

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Page 1: Case Study 1 - Woodford Engineering Consultancy · Root Cause Analysis Case Study 1 Case Studies Engine Roll-back Investigation Following a number of in-service events of roll-back

Root CauseAnalysis

Case Study 1

Case Studies

Engine Roll-back Investigation

Following a number of in-service events of roll-

back (uncommanded power reduction) on one

or more engines WEC engineers undertook a

complex root cause investigation. The rollback

events occurred during operation at over

27,000ft in particular icing conditions found

under the anvil of cumulonimbus cloud

formations, which was outside of the natural

icing certification envelope.

The root cause was initially thought to be a

problem with engine fuel control on maximum

thrust limits, but following substantial analysis

of data from flight recorders, the root cause

was found to be ice accretion on the engine

compressor supercharger stage vanes causing

the engine core flow to be restricted. The

transient nature of icing meant that the

evidence was lost when the aircraft was on the

ground, so that after the occurrences all

maintenance checks showed that engine

operation was normal.

The problem was cured by providing additional

heating of the supercharging vanes.

Rob Hardman, Senior Engineer

A4 2pp. Root Cause (2)_Layout 1 11/06/2015 09:14 Page 1

Page 2: Case Study 1 - Woodford Engineering Consultancy · Root Cause Analysis Case Study 1 Case Studies Engine Roll-back Investigation Following a number of in-service events of roll-back

Woodford Engineering Consultancy (UK) Ltd.

HEAD OFFICE Metropolitan House | Station Road | Cheadle Hulme | Cheshire | SK8 7AZ | United Kingdom

BRISTOL OFFICE Unit 6 Brabazon Park | Golf Course Lane | Filton | Bristol | BS34 7PZ | United Kingdom

www.wecuk.com

Case Study 2

Fuel System Level Sensors

Level sensors were frequently being removed from aircraft because of incorrect indication of

fuel levels. The sensors indicated FUEL/WET when the sensor was not covered with fuel, and

indicated AIR/DRY when the sensor was covered with fuel.

Subsequent examination and analysis of sensors returned to the equipment supplier identified

that the electronics potting material had suffered expansion resulting in micro cracks. These

micro cracks allowed ingress of water droplets and contamination of the internal circuitry of the

sensors. This altered the response of the circuitry, resulting in false indication of the fuel levels.

Expansion of potting material could also result in damage to the internal electrical connections

and components.

The potting material was found to have a glass transition temperature and coefficient of thermal

expansion that was significantly different to the potting material used in other similar

components. Testing by the supplier confirmed that the potting material exhibited expansion

and cracking at elevated temperatures.

The supplier replaced the potting material with an improved compound.

Stewart Webb, Senior Engineer

Case Study 3

Fuel Tank Inlet BallValve Failures

After 10 years successful in-service operation the customer was experiencing premature failure

of fuel tank inlet valves on a significant number of in-service aircraft. The fuel tank inlet valve

would not open during tank refuel, leading to delays and cancellations.

Examination of failed in-service valves showed that the ‘O’ ring seal in the valve ball/seat

interface was found to have extruded thus jamming the valve. Investigations concluded that the

seal extrusion was caused by the expansion of fuel trapped within the valve housing following

fuel transfer. The very cold fuel trapped inside the closed valve following transfers at altitude

expanded significantly as it was warmed during descent and on the ground. The consequent

increase in pressure extruded the seal.

The equipment supplier replaced the failed valve type with a similar valve type but with

provision for pressure relief.

Wayne Jones, Senior Engineer

A4 2pp. Root Cause (2)_Layout 1 11/06/2015 09:14 Page 2