case history - tam international · 2020. 4. 9. · case history the information and/or data in...

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WELL INTERVENTION DRILLING & COMPLETIONS UNCONVENTIONAL RESOURCES RESERVOIR OPTIMIZATION Heel Producing Excessive Water TAM-J Inflatable Packer Location: Canada CHALLENGE: A 6-1/4 inch open hole horizontal well in a fractured carbonate reservoir was producing 500 BPD with 90% water cut. Selective testing identified the heel of the well as the source of excessive water. SOLUTION: A 5-1/2 inch OD TAM-J inflatable packer with a “J” type release sub above was run. The packer was inflated and released the work string. Then, a hydraulic set packer with fiberglass tubing and “J” latch overshot below was run. Operators latched the release sub and set the hydraulic packer, isolating the heel and placing the well back on production. (Note: Fiberglass tubing was run due to corrosive fluids in the heel section.) RESULTS AND BENEFIT: The well tested at 240 BPD with less than 35% waster cut, resulting in oil production increase of 100 BPD and payout in less than 15 days. Gas/Water Shut-off: Scab Liners CASE HISTORY The information and/or data in this publication is supplied solely for informational purposes and TAM International makes no guarantees or warranties, either expressed or implied, with respect to its accuracy, completeness or use. ©2019. 05/19. 066. tamintl.com Excellence at the Wellsite ®

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Page 1: CASE HISTORY - TAM International · 2020. 4. 9. · CASE HISTORY The information and/or data in this publication is supplied solely for informational purposes and TAM International

WELL INTERVENTION DRILLING & COMPLETIONS UNCONVENTIONAL RESOURCES RESERVOIR OPTIMIZATION

Heel Producing Excessive Water TAM-J Inflatable Packer

Location: Canada

CHALLENGE: A 6-1/4 inch open hole horizontal well in a fractured carbonate reservoir was producing 500 BPD with 90% water cut. Selective testing identified the heel of the well as the source of excessive water.

SOLUTION: A 5-1/2 inch OD TAM-J inflatable packer with a “J” type release sub above was run. The packer was inflated and released the work string. Then, a hydraulic set packer with fiberglass tubing and “J” latch overshot below was run. Operators latched the release sub and set the hydraulic packer, isolating the heel and placing the well back on production. (Note: Fiberglass tubing was run due to corrosive fluids in the heel section.)

RESULTS AND BENEFIT: The well tested at 240 BPD with less than 35% waster cut, resulting in oil production increase of 100 BPD and payout in less than 15 days.

Gas/Water Shut-off: Scab Liners

CASE HISTORY

The information and/or data in this publication is supplied solely for informational purposes and TAM International makes no guarantees or warranties, either expressed or implied, with respect to its accuracy, completeness or use. ©2019. 05/19. 066. tamintl.com

Excellence at the Wellsite®