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Together. Free your energies Capgemini UK Infrastructure Outsourcing Project Arthur Improved Data Centre Efficiency Paul Feeney – Capgemini Tony Mills – Spie Matthew Hall

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Together. Free your energies

Capgemini UK Infrastructure Outsourcing

Project Arthur – Improved Data Centre Efficiency

Paul Feeney – Capgemini Tony Mills – Spie Matthew Hall

Project Arthur

The Toltec data centre, in the west country was fast approaching it’s 1990’s design capacity limitations. The infrastructure therefore required upgrading to meet existing and future customer demands as well as to maintain and improve its resilience and efficiency.

Arthur is the £9m project to refit Capgemini's existing Toltec data centre in Bristol with 'Merlin' and other new technology in order to achieve significant advances in efficiency, sustainability, capacity and flexibility.

The 9-month project was completed in October 2011 and measured impacts (including PUE reduction from 1.88

to 1.45) are already meeting the ambitious objectives that were set.

Our environmental performance is a key dimension of this programme with corporate environmental objectives

being publicly set in 2008 and ISO 14001 certification being achieved for our UK business in 2009.

Reasons for Refurbishment

Before Arthur, measurement of energy consumption was cumulative, so that it was not possible even to distinguish between office and data centre, or between IT equipment and the underlying items of basic plant supporting the IT. To fully understand our power consumption and to adhere to the TGG metrics, electrical separation and measurement was identified and implemented as part of the upgrade programme. In addition, we adopted the 'enclosed cold aisle' principles, with elevated return air temperatures using pressure based fan speed controls, to minimise energy consumption. In addition to this we developed a “top-down” cooling principle, whereby the energy consumption through the means of heat rejection was biased heavily towards our energy efficient external fans

Reduced Toltec’s infrastructure energy consumption and CO2 emissions in line with corporate objectives.

Ensure the infrastructure can support the planned growth in new business.

Increase the infrastructure resiliency to comply fully with Tier 3 requirements.

Reduce energy bills and thus enable Capgemini to offer more cost-competitive services to clients.

Enable synchronous connectivity with the new Merlin data centre in Swindon.

What we set out to achieve:

20% by 2014 750w/m2 – 1000w/m2

Fault tolerant infrastructure Removal of 2x900kw chillers Dark fibre completion

Operationally Live, Mission Critical, Business Reasons Why Arthur should WIN – No1

Toltec is a live, operational data centre, with thousands of servers running 24x7x365, serving 100’s of clients from government departments to major multinationals.

Unplanned downtime to services was not permitted at any point during the project.

Mainframes SAN’s Tape & Patch Any shape, Any Size

Reuse, Refit, Reorganise Reasons Why Arthur should WIN - 2

Efficient data centres are not always brand new projects. Arthur achieved the successful transformation of a live data centre from an inefficient legacy to a modern efficient one. This should inspire future projects by

demonstrating what can be achieved without the need for an expensive, risky IT migration to a new location.

Nitrogen Pipe Freeze (200mm) x 84

Mechanical Hot taps x 14 no.

Top Down Thinking Reasons Why Arthur should WIN – No3

Driving greater efficiency through the use of fan speed as well as temperature control.

Reduced Peak Ambient Return Water Temperature (Adiabatic Water Spray Assisted)

Re-use of such proven Merlin technology enabled significant cost savings to be achieved.

Fans @ 100% ALL YEAR

Free Cooling for Approximately 2300 Hrs p.a (27%) Mix Mode Cooling For Approximately 6360 Hr p.a (72%) Full Compressor Run Approximately 100 Hours / Year ( 1% p.a)

Supply Air Into Floor Void 23C

Return Air From Data Hall 36C

Free Cooling Achievable With Return Condenser Water up to 14.5C

Reduced Peak Ambient Return Water Temperature (Adiabatic Water Spray Assisted)

Operationally Complex, Client Challenging Reasons Why Arthur should WIN – No4

The sheer scale and complexity of the project, which involved the re-engineering of 1000sqm of existing IT floor space into hot & cold aisles to enable energy efficiencies, and moving 1000’s of servers and 100 of racks.

New Electrical 1.0MW upgrade. Complex system engineering integration and test.

Cold Aisles Temperature Sensors Pressure Sensors +8pa/12pa Supply T @ 24C Return T @ 36C

Best Practices

Redundancy = N+N Cooling solution, N+N Power solution, N+1 BMS

Load efficiency = Flywheel UPS, Thermal load balancing Cost minimization = By maximise free cooling within the CRAC units and running the Dry Cooler fans at 100% Management = New BMS system monitoring and reporting upon all critical plant Electrical cost separation of IT and non-IT load ( via metering)

•Energy efficiency to be improved by 20% - achieved! •No batteries – achieved! •Green Grid annual PUE of 1.5 or better when fully loaded and from Day 1 – achieved! •Cooling load of 1000w per sqm, with ability to expand to 2000w per sqm without disruption to service – achieved! •Maximum use of free/mixed cooling, at least 99% of yearly operation – achieved •Concurrent maintainability, no breaks to service for standard maintenance activities – achieved to date! •Significant ( 20%+) cut in water use – achieved! •Environmental certification in ISO 14001- achieved! •Metering and energy measurement to meet highest EEC requirement in accuracy – achieved!

Design & Technical challenges V Requirements

Cooling Upgrade & Cold Aisle Impact

0

200,000

400,000

600,000

800,000

1,000,000

1,200,000

1,400,000

1,600,000

1,800,000

01/01/20

10

01/03/20

10

01/05/20

10

01/07/20

10

01/09/20

10

01/11/20

10

01/01/20

11

01/03/20

11

01/05/20

11

01/07/20

11

01/09/20

11

01/11/20

11

01/01/20

12

01/03/20

12

01/05/20

12

01/07/20

12

01/09/20

12

01/11/20

12

Total Kwh

use by Data

Centre

Total Kwh

used by

Technical

Floor

Total

KwHours

(cooling,

lighting,

losses etc.)Costs

Change over point from old to new Cooling

Completion of Cold Aisle no 9

Cost Reduction Profile

0

10,000

20,000

30,000

40,000

50,000

60,000

70,000

80,000

90,000

Jan-10

Mar

-10

May

-10

Jul-1

0

Sep

-10

Nov

-10

Jan-11

Mar

-11

May

-11

Jul-1

1

Sep

-11

Nov

-11

Jan-12

Mar

-12

May

-12

Jul-1

2

Sep

-12

Nov

-12

month£

Total costs for IT(cooling, lighting, losses etc.)

Change over point from old to new Cooling

Completion of Cold Aisle no 9, monthly cost saving est £17k

Advice to another organisation planning a similar facility

Strong governance in place to ensure effective business representation communication and input to the project

Rigorously applied change process to ensure appropriate impacting to remove risk of change Reiterative migration review process to identify and drive out risks from the project Appointing a prime contractor who embraced our requirement for service continuity and who

worked with Capgemini from design through to final IST to ensure we met our goals without disruption to our business or our clients.

There are a lot of efficiencies to be gained in existing data centres – largely by improving cooling

and air flow management in a systematic way.

CAPGEMINI – TOLTEC DATA CENTRE

Full Compressor Run Approximately 100 hrs / Year ( 1% p.a)

Approximately 494,040 kWhr / Annum Energy Saving During The Free Cooling Period

(No Compressors Running, Dry Cooler Fans At 100% Run) 2300hrs

227,259 kg CO2 Emissions Saved During The Free Cooling Period (Based On an Average of 0.46

kg CO2 / kWhr). 6300hrs

Approximately 165,810 kWhr / Annum Energy Saving During The Mixed Mode Cooling Period

(Partial Compressors Running, Dry Cooler Fans At 100% Run)

Total Power Consumption From Compressors is Approximately 1,237,518 kWhr’s / Annum

Power Consumption From Dry Cooler Fans at 100% Load is 956,592 kWhr’s / Annum

Approximate Energy Saved / Annum is 1,383,474 kWhr’s

Approximate 636,398 kg CO2 Emissions Saved / Annum Data provided by Hurley Palmer Flatt

Work done

Replace old chillers with new dry coolers = 1800kw

Replace old CRAC upflows with new down flow = 1300kw

Install new HV switch gear + 2xTXF

Install new switch board

Install new 2 x 625kva UPS

Install new 3 x 1800kva Generators

Replacement of existing fire system

Replacement of existing BMS system

Removal of redundant legacy equipment.

84 pipe freezes – on live systems

14 Hot pipe connections

Re align/turn around over 250 Customer racks Restack over 100 servers Install over 500m of cold aisles IST test New electrical system IST test New Mechanical system IST test New Fire control system Remove legacy Cause & Effect Plant “shutdowns” Re align existing lighting Install new lighting Replace 500 floor grilles Re locate data cabling and tray works Migrate across dual cooling systems Implement pressure controls

PUE reduction

2010

2.0Mw site load ( 500kw cooling, Electrical 200kw, 200kw office ) 1060kw IT

PUE 2.0/1060 = 1.88

2012 Site load estimated 1600kw (300kw cooling, 100kw office)

PUE 1600/1060

Summary, Q and A