8d report - team oriented problem...

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8D REPORT - TEAM ORIENTED PROBLEM SOLVING Complaint Information: Complaint No Apex Ref: E252 Complaint Date: 14 September 2012 Complaint 32 nos 20mm L1RF1S SS Cl 150 Flanged Ball Valves, Bore Dia. in one side of flange found to be 20mm but other side (Insert Side) found to be 13mm. Customer Name Apex Valves Pvt Ltd, Kolkata Part No. L1RF1S Part Description DN20 Reduced bore ball valve class 150 Customer Contact Rakesh Manoj Location: Kolkata Quantity Rejected nil 8D Updation Revision date NIL Date Of Root cause Identified 15 September 2012 Date of Permanent Corrective action implementation 20 September 2012 Date Of Permanent Corrective action verification 21 September 2012 Date Of Closing 25 October 2012

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8D REPORT - TEAM ORIENTED PROBLEM SOLVING

Complaint Information:

Complaint No Apex Ref: E252 Complaint Date: 14 September 2012

Complaint

32 nos 20mm L1RF1S SS Cl 150 Flanged Ball Valves, Bore

Dia. in one side of flange found to be 20mm but other side (Insert Side) found to be 13mm.

Customer Name Apex Valves Pvt Ltd, Kolkata

Part No. L1RF1S Part Description DN20 Reduced bore ball valve class 150

Customer Contact Rakesh Manoj Location: Kolkata

Quantity Rejected nil 8D Updation

Revision date NIL

Date Of Root cause Identified

15 September 2012

Date of Permanent Corrective action implementation

20 September 2012

Date Of Permanent Corrective action

verification

21 September 2012

Date Of Closing 25 October 2012

1D – Problem Solving Team:

NAME FUNCTION CONTACT

S.Kannan L& T--Quality control

R. Ganesan L& T--Quality control

L. Harikanth L&T----Production

Rakesh Manoj L&T-----Sales

J.Mahendran SGP-Quality control

A. Paramasivam SGP-Production

Raja SGP-Production

2D- Problem Description:

Problem Summary – Defect Photo/which

Where Reduced bore

No of defects

1

Defect details

Insert side Run bore diameter less

Specification Dia 19/19.5

Observed Dia13.0/13.5

Supplier Reference

L&T valves-VMU

3D – Containment Actions: Product Stock details: In hand qty information for

Date Location Total Stock

Inspected qty

Rejected Qty

Rework Qty

% Of Rejection

% of Confidence

20/09/2012

VMU 160 160 NA 160 NA 100%

Transit information

Skid Nos Where

(in transit / Ware house)

Certification Status

NOT APPLICABLE

Containment Action details for Reduced Bore Dimension variation: Sr No Action Status

1

Machining arranged for available WIP @ SGP, After machining the valve at insert side checked using Go Gauge for dimension, chamfer

Under machining

4D – Identification and Verification Of Root Cause : Identification Of Root Cause: Cause Effect Diagram for Reduced bore dimensional variation

- A team Brainstorming session carried out on 15 September 2012 resulted in the identification of the following possible Root Causes for the problem.

MACHINE

ENVIRONMENT

20mm Reduced bore

Dimensional variation

MAN

MATERIAL MEASURMENT

METHOD

Random inspection –

not done in insert side

Not machined

Not inspected at insert side due to valve

placed opposite to insert side

Program for machining

not available

Interchangeable as per

design

WHY AND WHY ANALYSIS FOR Reduced bore dimension less at insert side

Why the Reduced bore dimension less in insert side, Due to machining not done , interchangeable insert Why machining is not done Separate Machining program is not available for 20mm Reduced l bore Why separate machining program is not available for 20 mm Reduced bore Because the operator is not inspected the machined insert against the relevant drawing no: LT332077M

5&6D - Define, Implementation and Verification of Permanent Corrective Action : Permanent Corrective Action details for Full bore dimension less at insert side in 20mm Reduced bore:

Sr No

Action Responsibilit

y/Target

Implementation date with

Status

1 Operator awareness training Ganesan/

Mahendran 17 Sep 2012

2 Machining program is created Raja/

Paramasivam 16 Sep 2012

3. 100% inspection during assembly and final inspection

Ganesan/ Mahendran

17 Sep 2012

Gauge for 1P DN15 mm Ball valve , 1P DN 20 mm Ball valve

Corrective Action Effectiveness Verification Details:-----Not applicable

First Lot Skid No : Shipment Date : ETA :

Date

Qty/checked produced

Direct Ok

Rejection qty

Audit Result

Verified By

7D – Action to Prevent Reoccurrence: Sr No

Action Yes / No

Responsibility/

Target

Implementation date with Status

1 Have similar parts / processes been considered?

NA

2 Have operator Work Instructions been upgraded?

Yes

Mahendran/ Raja/Ganesan ON 17 SEP

2012

Completed

3 Have all Gauging requirements been considered?

Yes

Mahendran/Ganesan

ON 17 SEP 2012

Completed

4 Have all drawings been upgraded? N/A

5 Has the FMEA been updated? NA

6 Has the Control Plan been updated? NA

7 Others: One point lesson. N/A

8D – Recognize the team effort and Closing:

Reported By S.KANNAN Sign &Date

25 OCT 2012

Customer Appreciation and Conclusion

NA

Customer Sign & Date

NA