00027892
TRANSCRIPT
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SPE 27092
Coiled-Tubing Completion Procedure Reduces Cost and Time forHydraulically Fractured Wells
D.A. Harms, Mobil E&P U.S. Inc.
SPEMember
Copyright 1994, SocMy of Petr oleum Engineer s, Inc .
This peper wee prepsred for presenta tion a t t he Western Regional Meeting bald in Long Seach , CaffiOr nf a, U .S.A. , 22-25 Mar ch 1~.
This paper wee eeleofed for presentat ion by an SPE Program Committee following review of information c or rt it na d I n a n e bs t rs ct submtied by t he aut hor (e ). Cont ente of thepaper .se present ed , heve not been r ev iewed by t he soc ie ty of Petr oleum Engineers and are sub ject to cor rec tion by t he author( a) , The mat erial , se presented, doea not neceaserily ref fect
,.. . e-any pmbori m me WCWIY”1 , e. . - e-. .. -. .=...
.., .’ D ,,A ,,~ Fnoi_rs. its ~ffi=, or ~m~m, papem Wa~nted at SPE ~~nga em s@ecf t o pubf i iat ion review by Edhorial COmmlffWa of the %Oiefy,,,. ._...-m ,,,.. .ti * ~n~, The ~r~ eh~~ oon~in ~nspicuous acknowledgment
o f Petr oleum Engineers . Parmisei in t oCOPYisrest rict ed t oan ah- t o f not mcfe t hm w me. I II IWULU~WB-S-J ... . - .-.
of where and by whom the pew is presented. Wrne Librtisn! SpE, p.o. Sox m, ~mhwd~n, TX 7~1 U. S.A.,Telex 1SS24S SPEUT.
ABSI’RACT
A unique completion procedure has been developed to
reduce the cost and time to hydraulically fracture welis.
In the procedure, coiled tubing is used to replace
conventional tubing in most of the operations. This
procedure is made possible by a wellhead design that
enhances safety and simplifies switching from oneoperation to the next.
Hydrauiic fracturing coats comprise the majority of the
total cost for new diatomite welia. Muitiple stimulations
can be compieted in a single day by using coiled tubing to
cleanout or piace sand plugs which are used to isolate the
perforated interval between hydraulic fracture
stimulations. This allows significant savings to be realized
by fuiiy utii izing the service company’s entire minimum
daiiy charge. The coiled tubing also functions as a dead
string during fracture stimulations which allows real time
monitoring of downhole fracturing pressures.
The new wellhead incorporates two unique ideas: 1) a
hammer union tree cap which replaces the conventional
tlangeii tree *p. ~=~wm! te ~he ~r~ ~p iS a blast joint
that provides protection from sand erosion
when using coiied tubing as the dead string. The wellhead
design enables the tree cap (with attached blast joint) to be
References and illustrations at end of Paper
quickiy and easily exchanged with a fullbore lubricator
2) a full opening gate valve located between the casinghead
and the fracture wellhead. The valve is a safety device
that ailows any part of the wellhead to be removed whil
ensuring a completely controlled condition.
INTRODUCTION
The coiled tubing completion procedure was developed fo
diatomite welia at Mobil’s Lost Hills field. The field
located on the southeast nose of the Lost Hilis Anticiine i
the San Joaquin Basin (Kern County, Caiifomia). Th
reservoir consists of 600 to 800 ft of three m~”o
iithologies: interbedded diatomite, diatomaceous shale an
diatomaceous silt.
These three iithologies have different mechanica
properties that greatly affect their abiiity to fracture
Attempting to fracture stimuiate intervais greater the
200’ has proven ineffective in the past due to the partiavertical coverage of the intervai. Therefore muitipl
fracture stimulations are required to effectively deplete th
reservoir.
Hydrauiic fracture completions comprise approximatel
65% of the total weil cost. A procedure to reduce the co
and make new well economics more attractive w
required to continue the development of the fieid. Th
paper outlines anew procedure that effectively reduces t
cost and time required to complete the weiis.
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Coiled Tubing Completion Procedure Reduces Cost
2 and Time for Hydraulically Fractured Wells SPE 27892
COi+iiTmTIaWL mommwu
To identify major cost drivers for the conventional
completion procedure, 1992 completion charges were
tabulated on a Pareto diagram (see fig. 1). As expected,
the fracture stimulation costs accounted for most of the
total completion cost. The sum of the six fracture service
company expenses comprised 73% of the total completion
cost during 1992.
I i ’m rt h.r rcw im.y ~D&@ed that of the six fracture service“, ..-. .- ..-,
company categories, hydraulic fracture pump charges
were the most significant. These charges accounted for
30$10of the total. The cost of the saiid mid the frac gel.
were ZiSO i%CO@W&Xi having a rn.~”or effect on
completion costs resulting in 18%and 17%of the expenses
respectively.
Increasing or decreasing the cost of the other company
services (workover rig, perforating etc.) has little effect on
the overall completion cost. The Pareto diagram
corroborates this by showing that none of the non-fracture
services or equipment account for more than 10% of the
overaii cost.
In addition to having high stimulation costs, considerable
time was required to complete the well using the
conventional procedure. Time intensive operations
included: running in and out of the hole with the tubing,moving and pressure testing the bridge plug, and switching
the wellhead cotilguration in preparation for fracturing.
An overview of the conventional procedure is outlined in
table 1.
Using this procedure, only one perforated interval could be
fmctured per day. Typical Mobil Lost Hills fmcture
stimulations require pump times between 1 hour and 1.5
hours per perforated intervaL However, since the service
company charges a four hour minimum for their pumping
equipment, by performing otdy one fmcture stimulation
per day, 65% to 75% of the pump expenses incurred were
not used.
Additionally, a snubbing assist unit was required to work
on these wells since they would flow after being fmcture
stimulated. An average of 2 days was required when using
the snubbing assist unit to remove the bridge plug and run
a production string. W]th the conventional completion, a
well with 5 perfomted intervals requires 8 days of
opemtions prior to placing the well on production.
COILED TUBING PROCEDURE
The conventional completion procedure was altered in
three main areas during the 1993 progmm: 1) coiledtubing replaced the conventional tubing for most of the
opemtions. The coiled tubing could be run in and out of
the wellbore more quickly than conventional tubing and
did not require a snubbing assist unit if pressure was
encountered. The coiled tubing was used as the dead
string when fracture stimulating, and was used in cleaning
out or placing sand plugs between perfomted intervals. 2)
a unique wellhead was deveioped to faetii’mte s-witckdng
from one opemtion to the next and to accommodate a
hlass joht to protect the coiled tubing from erosion. 3)
use of sand plugs instead of a retrievable bridge plugs to
isolate intervals between fracture stimulations. A
summary of the coiled tubing procedure is outlined inA&seuaule ~.
The new procedure enhances safety by eliminating the
requirement for a snubbing assist unit. The crossover
depth from snubbing to “stripping” (depth where the
weight of the tubing is greater then the upward force due
to pressure) is less than the depth of the sand plug.
Therefore, the tubing can be run in the hole without weiipressure to the crossover depth. Next, the tubing can be
stripped in the hole while circulating sand out of the
wellbore.
The tubing used to circulate out sand becomes the
production string. Once the sand is circulated out, the
tubing is landed, and the producing tree installed. The
one way circulating valve installed in the tubing is then
sheared out and the well turned over to production.
A second Pareto diagram (see fig. 2) was created to
identify the coat drivers when the coiled tubing completion
procedure is used. Again, the fmcture service company
accounts for the mqjority of the charges. However, with
the new procedure, only 20% of the total completion cost
was due to the hydrati:c fmcture pump charges, which
results in a 33% reductjon (compared to 30% with theconventional procedure). The sand expense, however, is
the most significant cost of the coiled tubing completion
procedure. (Sand is 28% of the total@ compared to 18%
using the coiiveiitkmd procetkre.)
Again, as with the conventional procedure, increasing or
decreasing the cost of the non-fmcture company services
and equipment does not have a noticeable effect on the
ovemll completion costs. Therefore, the cost of a coiled
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SPE 27892 D. A. fiIlllS 3
overall completion costs. Therefore, the cost of a coiled
tubing unit over a conventional w-orimvei fig dk! not add
an appreciable amount to the total cost.
COILED TUBING
Ftw Sandcleammt
After fracture stimulating, the 1.5” coiled tubing unit is
used primarily to clean out sand.. . ..# +haThe ~it i~fi w c =
sand plugs is critical since sufllcient sand is required to
ko!a& the pressure resii!ting from previously stimulated
intervals. However, the sand can not cover the next
interval to be perforated. The coiled tubing provides a
method for cleaning out the sand to the desired depth1 -c h .vo hem e~c Qunt eA in liftingaccuratdy, No prcb.a... . .--------
the frac sand using the 1.5” coiled tubing in 7“ casing.Gelled KC] water (Marsh Funnel Vkcosity of 35 to 40 sec.)
is used as the circulating fluid. A circuiting pump wfiii
shale shaker is employed to retain as much of the gelled
water for m-use as possible. The time to circulate the
sand out of the well and pull the coiled tubing averages
two hours.
In addition, several improvements were made in the 1993
project to help the frac sand settle faster in the wellbore:
1) the crosslinking agent was cut out of the gelled fluid
during the last two minutes of the fracture stimulation.
(The sand laden gelled fluid was pumped into the wellbore
and the near wellbore area as a linear fluid.) 2) KCIwater was pumped as a flush instead of gelled fluid. The
difference in sand settling is significant. For example, on
the wells pumped with all crosslinked gelled fluid and
flushed with gelled fluid, over 3 hours is required for the
sand to settle. Tailing in with a linear gelled fluid and a
KC1water flush allows the sand to settle in 30 minutes.
On occasion, the sand plug ieft in the weiiimre after
completing a fracture stimulation was not of suftlcient~e~g~~ tO pFOVMe pressure integrity. In these cases sand
can be pumped dQwnthe coiled tubing to provide a larger
sand plug. The sand is pumped at low concentrations (1
to 2 lb./gaL) using KCI water. No bridghg of sand in the.coiied tubing has ‘*ii experwimi.
As ADead Strhqg
The coiled tubing is also employed as a “dead string” when
fracture stimulating. The coiled tubing, run in the hole
just above the perforated interval, is used to monitor
bottom hole pressure during the stimulation. To prevent
excess sand from falling around the coiled tubing after
fracturing, the tubing is pulled slowly up the hole at theend of the jQb.
A blast joint is used as a sleeve in the wellhead to prevent
sand from eroding the coiled tubing. The thickness of the
coiled tubing is monitored before and after fracturing. No
incremental metal loss has been detected on the coiled
tubing when it was used as the dead string. However, the
blast joint has shown noticeable wear at the point of sand
entry into the wellhead. Without the blast joint such~ro~ion ~ouid have possibly parted the coiled tubing.
A unique wellhead was designed to improve the eftlciency
of the coiled tubing completion procedure (see fig. 3).
Two features have been combinwi to ensure the eom@etimiwellhead is secure and accessible. A tree cap was devised
ti,tii an =ttt&d sieve t Q protect the coiled tubing from
sand and a full opening master valve has been employed
to enhance safety. With a total height of 5.5’ the
wellhead allows service company personnel to switch the
tree cap with a lubricator while standing at ground level.
The most diathwtive part of the completion wellhead is the
hammer union tree cap (see fig. 4). It has been designed
to allow connection of the coiled tubing blow out
prevention equipment (BOPE) to the top of the cap. A
blast joint can then be threaded into the bottom. Since
the blast joint has to be removed prior to conductingintermediate operations (logging, perforating etc.),
attaching the tree cap to the coiled tubing BOPE, allows
both to be treated as an integral unit. This enables the
tree cap and blast joint to be quickly removed when
placing a lubricator on the completion wellhead.
A hammer union connection was designed to attach the
tree cap go~iiew~ilii=d, The tree cap connection matched
the perforating company’s lubricator connection. With
this design, the tree cap/ coiled tubing BOPE equipment
and a lubricator can be exchanged hi apprdmatciy 15
minutes.
In order to remove the tree cap and lubricator under
controlled conditions, the well pressure has to be isciated.
A master valve has been incorporated between the casing
head and the fracture stimulation wellhead for this
purpose. The valve is a full opening gate valve with the
internal diameter sized to match the internal dhuneter of
the production casing. This ensures that there are no
restrictions for equipment entering the well.
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Coiled Tubing Completion Procedure Reduces Cost
4 and Time for Hydraulically Fractured Wells SPE 27892
During the 1993 completion project, we discovered that the
master valve seats require reconditioning after 5 to 6
million pounds of sand (typically 3 to 4 wells) have been
pumped through it. In the latter stages of the project, two
completion wellheads (master valve and frac valve) are
employed. The inactive completion wellhead can be
reconditioned and installed on the next well to be
Cmnp:eted.
REsuL’rs
The coiled tubing has worked well in circulating sand out
of the wellbore. The time required to circulate and pull
out of the hole with the coiled tubing averages two hours.This allows a fracture stimulation treatment to be
performed every three hours. Additionally, sand plugs
can be safely placed through coiled tubing using KCI water
and low sand concentrations (1 lb./gal. to 2 lb./gaL). No
sand bridging has been observed in the coiled tubing.
Coiled tubing has been used successfully as a “dead string”
to monitor the bottom hole pressure during fracture
stimulations. No incremental metal loss has been detected
on the coiled tubing. However, the sleeve around the
coiled tubing has exhibited noticeable wear at the point of“--J ..-4-. :..4...qL. ...mIIL. .Sauu C1lL1 y l l l LU UK w cul l -u .
w k . .“—..AIAI. .1-.,. h ..s l lC cApUluuusG v--r G u
worked well to prevent the coiled tubing from erosion and
possible parting.
The new wellhead has reduced the time required for
switching from one operation to the next. An average of
15 minutes were required to switch out the coiled tubing
BOPE to a lubricator and vice versa. The seats in the
master valve have required redressing after completing
three to four wells. Similar results have been observedw it h t hm v ml vx in fhm nnder l fmdmw h-d. I t ~St~g~~f~~~. . . . . . . . . . . . - . . . . .. . . . ..& J.—------- - -—-.
recommended that on large projects, two wellheads be
used alternately. One wellhead could be redressed while
the other is being used.
With the coiled tubing procedure, a well with 5 fracture
stimulated intervals can be placed on production in 4 days.
This has resulted in a 50% reduction in completion time
when compared to conventional methods. During 1993 an
average of 3 intervals were fracture stimulated per day.
Although it was necessary to increase the hours worked
per day from 10 to 12, use of the 4 hour minimum service
company pump charge was maximized.
conventional and the 1993 coiled tubing completion
procedures. Both in the conventional procedure and the
coiled tubing procedure, fracture service company charges
account for the majority of the costs. However, the coiled
tubing procedure reduces the completion costs by an
average of $60M. Fully using the 4 hour minimum
charged for the hydraulic pumps accounts for $35M (orEOOZ.\f + k . WARM c d rdmdinn.J 7 W J u. .“ . v “ ” ... w “ . . .“ ” -..” .. .
Additional savings were realized by reducing the rental
time, not using bridge plugs, and eliminating the snubbing
assist unit.
When compared to the average completion costs for Lost
Hills wells in the past five years (see fig. 5), the new
completion procedure lowers costs by 21%.
ACKNOWLEDGEMENTS
The author would like to acknowledge the technical-- ..,.
assistance of J. Ryan, Halliburton Energy Services and i?.
Litzel, Dowell Schhnnberger, and the significant
contribution of W. Johnson, Mobil Exploration and
Producing U.S. Inc. in implementing the procedure. The
author also wishes to thank Mobil Exploration &
Producing U.S. Inc. for granting permisdon to publishth:. ---bm pp. .
REFERENCES
1. Coats, E. A., and Johnson, K. J.: “Realed-Tubing
Technology Accelerates Coalbed Methane
Production in the Black Warnor Basin” paperSPE 23697, nresented at the Production–_––-–--—
Operations Symposium of the Society of
Petroleum Engineem, Oklahoma City, Oklahoma,
April 7-10, 1991.
2. Fast, R. E., Murer, A. S., and Timmer, R. S.:
“Description and Analysis of Cored Hydratilc
Fractures, Lost Hills Field, Kern County
California” paper SPE 24853, presented at the
67th Annual Technical Conference and Exhibition
of the Society of Petroleum Engineers,
Washington , D.C., October 4-7, 1992.
Table 3 compares the average costs for both the 1992
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Figure 1. Pareto chart identifying conventional completion cost drivers.
40 -“-... .-
Frac Company Charges
Non-Frac Company Charges
1 100
Step 1.Step 2.
Step 3.Step 4.Step 5.
Step 6.~~q 7
Step 8.
Step 9.
Repeat
seep 10,
Step 11.
Move in production rig, install necessary equipment.Set retrievable bridge plug (RBP) below bottom stage (withtubing) .Perforate interval to be fracture stimulated.Run tubing in hole.Fracture stimulate down tubing/casing annulus (with tubing used
to monitor bottom hole pressure) .
Force ciose fracture with limited floiiback.cleanQut sand with tubing.
Retrieve, reset RBP above perforated interval and pressure test.Pull out of hole with tubing.
steps 3 through 9 for each interval to be stimulated.
Move in snubbing assist unit, install necessary equipment.
Snub RBP out of hole and snub/strip in production string
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.
Table 2. Coiled tubing completion procedure outline.
Step 1.Step 2.Step 3.Step 4.
Step 5.
Step 6.
Step 7.
Repeat
Step 8.Step 9.
Step 10.
Step 11.
Move in coiled tubing unit, install necessary equipment.Perforate interval to be fracture stimulated.
Run coiled tubing in hole.Fracture stimulate down tubing/casing annulus (with coiled
tubing used to monitor bottom hole pressure) .
Force close fracture with limited flowback and allow timefor sand to settle.Clean out sand to bottom of next perforated interval, or
place sand through coiled tubing if necessary.Pull coiled tubing out of hole.
steps 2 through 7 for each stage.
Rig down coiied tubing unit and equipment.Move in production rig, install necessary equipment.
Run conventional tubing in hole, circulate out sand to totaldepth.
Land production string.
Figure 2. Pareto chart identifying coiled tubing completion cost drivers.452
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Figure 3. Wellhead developed for coiled tubing completion procedure.
Hammer union treecap
10” threaded to API 7“ flanged crossover
API 7“ by API 1 Iii flanged fracture
head with 3“ API flanged gate valves
Apl 1 1“ to API 7“ flanged adapter
API 7“ flanged gate valve
Internal diameter 6.75”
API 7“ flanged tubinghead
Surface casing
7“ production casing
3.5” 8 Round internal upset threads
(to connect to Coiled tubing BOPE)
10” Hammer WIiOn
(same threads as lubricator)
10” threaded to API 7“ flanged crossover
2.375” internal upset threads
u ~ 2/375” blast joint
Figure 4. Hammer Union Treecap with attatched blast joint.
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.
Co n v e n t i o n a 1 Cc mp l e t i o n ~ Co i l e d T b g Co mp l e t i o n
( 1 9 9 2 Av e r a g e ) I ( 1 9 9 3 Av e r a g e )tt
c o s t I Coat
(M$) P er c e n t I ( MS) Pe r c e n t. - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
D, —1 OI a d. . I Iru , ~,o . c ,luc ,
?f.~ 70 0G.. . 1~~.~ ~Q.~
S a n d I 4 3 . 6 1 8 . 2 I
I I
4 9 . 1 2 7 . 5
F r a c F l u i d t 4 0 . 1 1 6 . 8 iI 2 5 . 9 1 4 . 5
Mi l a g e / Oe l i v e r y , 8 . 7 3 . 6 6 . 5 3 . 6
F r a c Va n I 5 . 3 2 . 2 5 . 2 2 . 9
Ot h e r 1 5 . 1 2 . 1 5 . 2 2 . 9- - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
F r a c Su bt o t a l I 1 7 4. 3 7 2 . 8 4 t 1 2 8. 1 7 1 . 7 6
Ri g 1 1 . 5 4 . 8 2 . 8 1 . 6
~ Qi ! e d T@ o 0 , 0 7 . 8 4 . 4
Eq u i p me n t Re n t a l s ~ 9 . 5 4.0 I 3.6 2.0P e r f o r a t e I 9 . 2 3 . 8 I 8 . 7 4 . 9
Ui r e l i n e I 7 . 4 3 . 1 II 7 . 5 4 . 2
T u bi n g f 6 . 3 2 . 6 tI 6 . 5 3 . 6
P u n p 3 . 5 1 . 5 I 2 . 6 1 . 5
Su pe r v i s i o n 4 1 . 7 ; 2 1 . 1
Ue l l h e a d 3 . 8 1 . 6 I 3 . 8 2 . 1
Sn u b bi n g Un i tII 3 . 2 1 . 3 I 0 . 0
Co mp l e t i o n F l u i d I 3 . 5 1 . 5 1I I 1 . 8 1.0
T r a n s po r t a t i o n 1 . 3 0.5 1 1 . 1 0 . 6
Ua s t e Di s p o s a l I 1 . 1 0.5 II 1.3 0.7
L oc a t i o n I 0 . 7 0 . 3 I 0 . 9 0 . 5- - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
T ot a l 2 3 9 1 0 0 ~ 1 7 9 1 0 0
Table 3. Mobil’s Lost Hills Diatomite Completion Costs for 1992 and 1993
2 1$%Reduction7
I&3 H 1989 through 1992 cost average/’
“f
. . . . . .. . .. . . . . . .. .
~ ~ ~ ~
1 B
1988 1989 1990 1991 1992 1993
Figure 5. Average Lost Hills completion costs for last 6 years